HL incident on 2018-04-26 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Excavation Issue
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$20,000
Incident datetime
2018-04-26 09:00
Report number
Location
OK
Narrative
On 4/26/18, a pipeline rehab crew was excavating an dig location near mp 167.7 on the tcs tulsa to sheldon #3-12". The dig was located between a mainline gate valve and a road way. The inline inspection data indicated fittings were located on each side of the mainline gate valve. The fitting on the south side was located and exposed while performing the excavation. Since the anomaly was located south of the valve, no excavation activity was planned on the north side of the valve. The tracked excavator was staged on the north side of the mainline gate valve, with the excavator tracks perpendicular to the line to allow access to the excavation. At the time of excavation, soil conditions were wet. As the excavator was digging, the excavator slid on the soft soil and either displaced soil or made direct contact with the fitting on the north side of the valve causing the release. The vertical fitting was found to be comprised of multiple components and failed at the threaded fitting of one of the components. The chief inspector notified operations control and a code red was issued. Personnel were dispatched to close mainline gate valves and isolate the line section. Soil berms were placed in the roadway ditch to prevent the release from migrating. Emergency responders arrived and closed the highway. Vac trucks recovered free product from the area and impacted soil was excavated and properly disposed. 400 cubic yards of soil were hauled to the waste management non-hazardous landfill in tulsa, ok. The damaged fitting was removed from the pipeline and a thread-o-ring nipple was installed.
Detailed record list
Report Received Date
2018-05-24 00:00:00
Iyear
2018
Report Number
20180144
Supplemental Number
30390
Report Type
Original Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2018-04-26 09:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
110
Recovered Bbls
110
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2018-04-26 09:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-04-26 09:00:00
Restart Datetime
2018-04-27 16:02:00
On Site Datetime
2018-04-26 09:00:00
Nrc Rpt Datetime
2018-04-26 09:26:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Ok-Ks State Line No. 3-12 (Tcs)
Segment Name
6420
Onshore State Abbreviation
Ok
Onshore Postal Code
74369
Onshore City Name
Not Within A Municipality
Onshore County Name
Craig
Designated Location
Milepost/valve Station
Designated Name
167.71
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
18
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
2' Attachment
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
2000
Est Cost Gas Released
13860
Est Cost Prop Damage
20000
Est Cost Emergency
92000
Est Cost Environmental
0
Est Cost Other
0
Prpty
127860
Accident Psig
360
Mop Psig
560
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
58787
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Based on 2nd party notification of cause, it was immediately apparent that the controller did not cause or contribute to the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
Yes
Num Contractors Tested
2
Num Contractors Failed
0
Cause
Excavation Damage
Cause Details
Excavation Damage By Operator's Contractor (Second Party)
Ex Party Type
Excavation Damage By Operator's Contractor (Second Party)
Notify Cga Dirt
Yes
Private Row Ind
Yes
Private Subtype
Private Landowner
Pipeline Easement Row Ind
Yes
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Liquid Pipeline
One Call Notified Ind
Yes
One Call Ticket Num
1.80417e+13
Locator Type
Contract Locator
Visible Marks
Data Not Collected
Service Interruption
Yes
Service Interruption Hours
31
Root Cause Category
Excavation Issue
Root Cause Type
Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
918-574-7327
Preparer Fax
918-574-7316
Prepared Date
2018-05-24 00:00:00
Authorizer Name
S****** L******
Authorizer Telephone
918-574-7327
Authorizer Title
Ai Analyst
Authorizer Email
S**************@m*********.com
Narrative
On 4/26/18, a pipeline rehab crew was excavating an dig location near mp 167.7 on the tcs tulsa to sheldon #3-12". The dig was located between a mainline gate valve and a road way. The inline inspection data indicated fittings were located on each side of the mainline gate valve. The fitting on the south side was located and exposed while performing the excavation. Since the anomaly was located south of the valve, no excavation activity was planned on the north side of the valve. The tracked excavator was staged on the north side of the mainline gate valve, with the excavator tracks perpendicular to the line to allow access to the excavation. At the time of excavation, soil conditions were wet. As the excavator was digging, the excavator slid on the soft soil and either displaced soil or made direct contact with the fitting on the north side of the valve causing the release. The vertical fitting was found to be comprised of multiple components and failed at the threaded fitting of one of the components. The chief inspector notified operations control and a code red was issued. Personnel were dispatched to close mainline gate valves and isolate the line section. Soil berms were placed in the roadway ditch to prevent the release from migrating. Emergency responders arrived and closed the highway. Vac trucks recovered free product from the area and impacted soil was excavated and properly disposed. 400 cubic yards of soil were hauled to the waste management non-hazardous landfill in tulsa, ok. The damaged fitting was removed from the pipeline and a thread-o-ring nipple was installed.
Report Received Date 2018-05-24 00:00:00
Iyear 2018
Report Number 20180144
Supplemental Number 30390
Report Type Original Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2018-04-26 09:00:00
Location Latitude 36.873453 Google Maps OpenStreetMap
Location Longitude -95.240464 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 110
Recovered Bbls 110
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2018-04-26 09:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-04-26 09:00:00
Restart Datetime 2018-04-27 16:02:00
On Site Datetime 2018-04-26 09:00:00
Nrc Rpt Datetime 2018-04-26 09:26:00
Nrc Rpt Num 1210358 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Ok-Ks State Line No. 3-12 (Tcs)
Segment Name 6420
Onshore State Abbreviation Ok
Onshore Postal Code 74369
Onshore City Name Not Within A Municipality
Onshore County Name Craig
Designated Location Milepost/valve Station
Designated Name 167.71
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 18
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details 2' Attachment
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 2000
Est Cost Gas Released 13860
Est Cost Prop Damage 20000
Est Cost Emergency 92000
Est Cost Environmental 0
Est Cost Other 0
Prpty 127860
Accident Psig 360
Mop Psig 560
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 58787
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind Yes
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Based on 2nd party notification of cause, it was immediately apparent that the controller did not cause or contribute to the incident
Employee Drug Test Ind No
Contractor Drug Test Ind Yes
Num Contractors Tested 2
Num Contractors Failed 0
Cause Excavation Damage
Cause Details Excavation Damage By Operator's Contractor (Second Party)
Ex Party Type Excavation Damage By Operator's Contractor (Second Party)
Notify Cga Dirt Yes
Private Row Ind Yes
Private Subtype Private Landowner
Pipeline Easement Row Ind Yes
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Liquid Pipeline
One Call Notified Ind Yes
One Call Ticket Num 1.80417e+13
Locator Type Contract Locator
Visible Marks Data Not Collected
Service Interruption Yes
Service Interruption Hours 31
Root Cause Category Excavation Issue
Root Cause Type Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name S****** L******
Preparer Title Ai Analyst
Preparer Email S**************@m*********.com
Preparer Telephone 918-574-7327
Preparer Fax 918-574-7316
Prepared Date 2018-05-24 00:00:00
Authorizer Name S****** L******
Authorizer Telephone 918-574-7327
Authorizer Title Ai Analyst
Authorizer Email S**************@m*********.com
Narrative On 4/26/18, a pipeline rehab crew was excavating an dig location near mp 167.7 on the tcs tulsa to sheldon #3-12". The dig was located between a mainline gate valve and a road way. The inline inspection data indicated fittings were located on each side of the mainline gate valve. The fitting on the south side was located and exposed while performing the excavation. Since the anomaly was located south of the valve, no excavation activity was planned on the north side of the valve. The tracked excavator was staged on the north side of the mainline gate valve, with the excavator tracks perpendicular to the line to allow access to the excavation. At the time of excavation, soil conditions were wet. As the excavator was digging, the excavator slid on the soft soil and either displaced soil or made direct contact with the fitting on the north side of the valve causing the release. The vertical fitting was found to be comprised of multiple components and failed at the threaded fitting of one of the components. The chief inspector notified operations control and a code red was issued. Personnel were dispatched to close mainline gate valves and isolate the line section. Soil berms were placed in the roadway ditch to prevent the release from migrating. Emergency responders arrived and closed the highway. Vac trucks recovered free product from the area and impacted soil was excavated and properly disposed. 400 cubic yards of soil were hauled to the waste management non-hazardous landfill in tulsa, ok. The damaged fitting was removed from the pipeline and a thread-o-ring nipple was installed.

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