GTG incident on 2018-11-22 — NY

Operator
National Fuel Gas Supply Corp
Cause
Equipment Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$200
Incident datetime
2018-11-22 21:47
Report number
Location
NY
Narrative
National fuel gas supply corporation has reported a natural gas incident as a result of an unintentional release of natural gas estimated at greater than three (3) million cubic feet, that occurred at 7700 ferrier rd. In the town of evans, erie county, ny. National fuel confirmed discovery of the incident on wednesday november 28, 2018 after completing a comprehensive flow analysis of gas lost during a relief valve release that occurred from approximately 9:23 pm to 11:33 pm on thursday november 22nd, 2018. The probable cause of the incident was equipment failure of a restrictor valve for a relief valve control that caused the device to fail in an open position. There were no injuries or property damage. The updated nrc report number 1231680.
Detailed record list
Report Received Date
2018-12-20 00:00:00
Iyear
2018
Report Number
20180134
Supplemental Number
31360
Report Type
Original Final
Operator Id
Name
National Fuel Gas Supply Corp
Operator Street Address
6363 Main Street
Operator City Name
Williamsville
Operator State Abbreviation
NY
Operator Postal Code
14221-5887
Local Datetime
2018-11-22 21:23:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2018-11-28 11:29:00
Commodity Released Type
Natural Gas
Unintentional Release
5300
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
No
Shutdown Explain
Relief Valve Repair Did Not Require Shutdown Of The Pipeline.
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2018-11-22 21:47:00
On Site Datetime
2018-11-22 21:59:00
On Off Shore
Onshore
Onshore State Abbreviation
Ny
Onshore Postal Code
14006
Onshore City Name
Town Of Evans
Onshore County Name
Erie
Designated Location
Milepost
Designated Name
Relief Valve
Pipe Fac Name
Line Rm32/ferrier Rd. Station
Segment Name
Station Eve 47
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Regulator/metering Station Equipment And Piping
Item Involved
Other
Item Involved Details
Relief Valve Controls
Installation Year
2001
Material Involved
Material Other Than Carbon Steel Or Plastic
Material Details
Stainless Steel
Release Type
Other
Release Type Details
Relief Valve Release
Class Location Type
Class 2 Location
Could Be Hca
No
Pir Radius
74
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
16000
Est Cost Intentional Release
0
Est Cost Prop Damage
200
Est Cost Emergency
2100
Est Cost Other
0
Prpty
18300
Accident Psig
317
Mop Psig
320
Mop Cfr Section
Mop Cfr Section Details
System Maximum Operating Pressure
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The facility is connected to a pipeline that was monitored and controlled through scada by the controllers within parameters. The cause of the incident was not due to controller action nor was the incident negatively affected by controller action or lack of action.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Relief Valve Ind
Yes
Other Control Relief Ind
Yes
Other Control Relief Details
Relief Valve Pilot Gas Control Flow Restrictor.
Eq Additional Other Ind
Yes
Eq Additional Other Details
Component Failure
Preparer Name
J*** S*****
Preparer Title
Pipeline Integrity Engineer
Preparer Email
S******@n******.com
Preparer Telephone
716-857-7899
Preparer Fax
716-857-7508
Authorizer Name
W****** S*****
Authorizer Title
Operations Superintendent
Authorizer Telephone
716-827-2327
Authorizer Email
S******@n******.com
Narrative
National fuel gas supply corporation has reported a natural gas incident as a result of an unintentional release of natural gas estimated at greater than three (3) million cubic feet, that occurred at 7700 ferrier rd. In the town of evans, erie county, ny. National fuel confirmed discovery of the incident on wednesday november 28, 2018 after completing a comprehensive flow analysis of gas lost during a relief valve release that occurred from approximately 9:23 pm to 11:33 pm on thursday november 22nd, 2018. The probable cause of the incident was equipment failure of a restrictor valve for a relief valve control that caused the device to fail in an open position. There were no injuries or property damage. The updated nrc report number 1231680.
Report Received Date 2018-12-20 00:00:00
Iyear 2018
Report Number 20180134
Supplemental Number 31360
Report Type Original Final
Operator Id 13063 PHMSA Enforcement
Name National Fuel Gas Supply Corp
Operator Street Address 6363 Main Street
Operator City Name Williamsville
Operator State Abbreviation NY
Operator Postal Code 14221-5887
Local Datetime 2018-11-22 21:23:00
Location Latitude 42.676346 Google Maps OpenStreetMap
Location Longitude -78.944289 Google Maps OpenStreetMap
Nrc Rpt Num 1231490 NRC Report How to search
Nrc Rpt Datetime 2018-11-28 11:29:00
Commodity Released Type Natural Gas
Unintentional Release 5300
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind No
Shutdown Explain Relief Valve Repair Did Not Require Shutdown Of The Pipeline.
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2018-11-22 21:47:00
On Site Datetime 2018-11-22 21:59:00
On Off Shore Onshore
Onshore State Abbreviation Ny
Onshore Postal Code 14006
Onshore City Name Town Of Evans
Onshore County Name Erie
Designated Location Milepost
Designated Name Relief Valve
Pipe Fac Name Line Rm32/ferrier Rd. Station
Segment Name Station Eve 47
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Regulator/metering Station Equipment And Piping
Item Involved Other
Item Involved Details Relief Valve Controls
Installation Year 2001
Material Involved Material Other Than Carbon Steel Or Plastic
Material Details Stainless Steel
Release Type Other
Release Type Details Relief Valve Release
Class Location Type Class 2 Location
Could Be Hca No
Pir Radius 74
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 16000
Est Cost Intentional Release 0
Est Cost Prop Damage 200
Est Cost Emergency 2100
Est Cost Other 0
Prpty 18300
Accident Psig 317
Mop Psig 320
Mop Cfr Section Other View CFR 49 §192
Mop Cfr Section Details System Maximum Operating Pressure
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The facility is connected to a pipeline that was monitored and controlled through scada by the controllers within parameters. The cause of the incident was not due to controller action nor was the incident negatively affected by controller action or lack of action.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Relief Valve Ind Yes
Other Control Relief Ind Yes
Other Control Relief Details Relief Valve Pilot Gas Control Flow Restrictor.
Eq Additional Other Ind Yes
Eq Additional Other Details Component Failure
Preparer Name J*** S*****
Preparer Title Pipeline Integrity Engineer
Preparer Email S******@n******.com
Preparer Telephone 716-857-7899
Preparer Fax 716-857-7508
Authorizer Name W****** S*****
Authorizer Title Operations Superintendent
Authorizer Telephone 716-827-2327
Authorizer Email S******@n******.com
Narrative National fuel gas supply corporation has reported a natural gas incident as a result of an unintentional release of natural gas estimated at greater than three (3) million cubic feet, that occurred at 7700 ferrier rd. In the town of evans, erie county, ny. National fuel confirmed discovery of the incident on wednesday november 28, 2018 after completing a comprehensive flow analysis of gas lost during a relief valve release that occurred from approximately 9:23 pm to 11:33 pm on thursday november 22nd, 2018. The probable cause of the incident was equipment failure of a restrictor valve for a relief valve control that caused the device to fail in an open position. There were no injuries or property damage. The updated nrc report number 1231680.

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