GTG incident on 2018-11-08 — TX

Operator
Anr Pipeline Co
Cause
Material Failure Of Pipe Or Weld
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$138,000
Incident datetime
2018-11-08 10:25
Report number
Location
TX
Narrative
On 8 november 2018 at 10:25 ct, a contract employee, while conducting a close interval survey, observed bubbling from the ground above the anr lateral 703 south jennings line. Upon discovery of the condition, the employee contacted the area office, who dispatched a qualified technician to shut in valves to the 703 lateral and investigate the source of the leak. The initial field investigation determined that the source of the bubbling was due to leak on the pipeline. At 12:05 ct, an incident was reported into the national response center (report #1229862). A courtesy call was also placed the PHMSA accident investigation division (aid) to inform the division of the incident. Following the discovery of the leak, actions included the reduction of pipeline pressure from discovery pressure of 976psig to 100psig, completed . On 12 november 2018, repair crews arrived at the site to repair the pipeline. On november 13 prior to excavation, pipeline pressure was reduced to 20psig. On 15 november the pipeline was exposed, the coating was examined, and a defect was found on the girth weld. It was determined to repair the leak by placing a type-b pressure contain sleeve across the defect. On 16 november, the type-b sleeve was welded onto the pipeline and the repair was completed. The defect was limited to a single pin hole located at the 06:00 position on the weld with no anomalies observed near the girth weld. The pipeline was purged, loaded, and returned to service at 14:00 on november 17, 2018.
Detailed record list
Report Received Date
2018-12-07 00:00:00
Iyear
2018
Report Number
20180126
Supplemental Number
31294
Report Type
Original Final
Operator Id
Name
Anr Pipeline Co
Operator Street Address
700 Louisiana Street Suite 700
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-11-08 10:25:00
Location Latitude
Location Longitude
-92.66840188
Nrc Rpt Num
Nrc Rpt Datetime
2018-11-08 12:05:00
Commodity Released Type
Natural Gas
Unintentional Release
1
Intentional Release
312
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-11-08 10:51:00
Restart Datetime
2018-11-17 14:00:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2018-11-08 10:25:00
On Site Datetime
2018-11-08 10:45:00
On Off Shore
Onshore
Onshore State Abbreviation
La
Onshore Postal Code
70546
Onshore City Name
Not Within A Municipality
Onshore County Name
Jefferson Davis
Designated Location
Survey Station No.
Designated Name
10+18
Pipe Fac Name
Anr Lateral 703 South Jennings
Segment Name
Route Id: 8001703
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
60
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Weld/fusion, Including Heat-Affected Zone
Pipe Diameter
12
Pipe Wall Thickness
0.25
Pipe Smys
42000
Pipe Specification
Api 5lx
Pipe Seam Type
Longitudinal Erw - Low Frequency
Pipe Manufacturer
Lonestar
Pipe Coating Type
Coal Tar
Weld Subtype
Pipe Girth Weld
Installation Year
1956
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
328
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
12000
Est Cost Unintentional Release
1
Est Cost Intentional Release
12000
Est Cost Prop Damage
138000
Est Cost Emergency
0
Est Cost Other
0
Prpty
162001
Accident Psig
796
Mop Psig
1050
Mop Cfr Section
192.619(A)(1)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
7387
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
Pipeline Was Installed Prior To Design Requirements For Internal Inspection Tools
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The minimal amount of gas loss was not detectable due to the small size of the leak.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Pwjf Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind
Yes
Other Factor
Yes
Other Factor Details
Construction-Related
Additional Lack Fusion Ind
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1982
Hydrtst Most Rcnt Pressure
1638
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
R**** S*****
Preparer Title
Compliance Specialist
Preparer Email
R***********@t**********.com
Preparer Telephone
615-465-5123
Authorizer Name
R**** S*****
Authorizer Title
Compliance Specialist
Authorizer Telephone
615-465-5123
Authorizer Email
R***********@t**********.com
Narrative
On 8 november 2018 at 10:25 ct, a contract employee, while conducting a close interval survey, observed bubbling from the ground above the anr lateral 703 south jennings line. Upon discovery of the condition, the employee contacted the area office, who dispatched a qualified technician to shut in valves to the 703 lateral and investigate the source of the leak. The initial field investigation determined that the source of the bubbling was due to leak on the pipeline. At 12:05 ct, an incident was reported into the national response center (report #1229862). A courtesy call was also placed the PHMSA accident investigation division (aid) to inform the division of the incident. Following the discovery of the leak, actions included the reduction of pipeline pressure from discovery pressure of 976psig to 100psig, completed . On 12 november 2018, repair crews arrived at the site to repair the pipeline. On november 13 prior to excavation, pipeline pressure was reduced to 20psig. On 15 november the pipeline was exposed, the coating was examined, and a defect was found on the girth weld. It was determined to repair the leak by placing a type-b pressure contain sleeve across the defect. On 16 november, the type-b sleeve was welded onto the pipeline and the repair was completed. The defect was limited to a single pin hole located at the 06:00 position on the weld with no anomalies observed near the girth weld. The pipeline was purged, loaded, and returned to service at 14:00 on november 17, 2018.
Report Received Date 2018-12-07 00:00:00
Iyear 2018
Report Number 20180126
Supplemental Number 31294
Report Type Original Final
Operator Id 405 PHMSA Enforcement
Name Anr Pipeline Co
Operator Street Address 700 Louisiana Street Suite 700
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-11-08 10:25:00
Location Latitude 30.17631158 Google Maps OpenStreetMap
Location Longitude -92.66840188 Google Maps OpenStreetMap
Nrc Rpt Num 1229862 NRC Report How to search
Nrc Rpt Datetime 2018-11-08 12:05:00
Commodity Released Type Natural Gas
Unintentional Release 1
Intentional Release 312
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-11-08 10:51:00
Restart Datetime 2018-11-17 14:00:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2018-11-08 10:25:00
On Site Datetime 2018-11-08 10:45:00
On Off Shore Onshore
Onshore State Abbreviation La
Onshore Postal Code 70546
Onshore City Name Not Within A Municipality
Onshore County Name Jefferson Davis
Designated Location Survey Station No.
Designated Name 10+18
Pipe Fac Name Anr Lateral 703 South Jennings
Segment Name Route Id: 8001703
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 60
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Weld/fusion, Including Heat-Affected Zone
Pipe Diameter 12
Pipe Wall Thickness 0.25
Pipe Smys 42000
Pipe Specification Api 5lx
Pipe Seam Type Longitudinal Erw - Low Frequency
Pipe Manufacturer Lonestar
Pipe Coating Type Coal Tar
Weld Subtype Pipe Girth Weld
Installation Year 1956
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 328
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 12000
Est Cost Unintentional Release 1
Est Cost Intentional Release 12000
Est Cost Prop Damage 138000
Est Cost Emergency 0
Est Cost Other 0
Prpty 162001
Accident Psig 796
Mop Psig 1050
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 7387
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details Pipeline Was Installed Prior To Design Requirements For Internal Inspection Tools
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The minimal amount of gas loss was not detectable due to the small size of the leak.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Pwjf Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind Yes
Other Factor Yes
Other Factor Details Construction-Related
Additional Lack Fusion Ind Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1982
Hydrtst Most Rcnt Pressure 1638
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name R**** S*****
Preparer Title Compliance Specialist
Preparer Email R***********@t**********.com
Preparer Telephone 615-465-5123
Authorizer Name R**** S*****
Authorizer Title Compliance Specialist
Authorizer Telephone 615-465-5123
Authorizer Email R***********@t**********.com
Narrative On 8 november 2018 at 10:25 ct, a contract employee, while conducting a close interval survey, observed bubbling from the ground above the anr lateral 703 south jennings line. Upon discovery of the condition, the employee contacted the area office, who dispatched a qualified technician to shut in valves to the 703 lateral and investigate the source of the leak. The initial field investigation determined that the source of the bubbling was due to leak on the pipeline. At 12:05 ct, an incident was reported into the national response center (report #1229862). A courtesy call was also placed the PHMSA accident investigation division (aid) to inform the division of the incident. Following the discovery of the leak, actions included the reduction of pipeline pressure from discovery pressure of 976psig to 100psig, completed . On 12 november 2018, repair crews arrived at the site to repair the pipeline. On november 13 prior to excavation, pipeline pressure was reduced to 20psig. On 15 november the pipeline was exposed, the coating was examined, and a defect was found on the girth weld. It was determined to repair the leak by placing a type-b pressure contain sleeve across the defect. On 16 november, the type-b sleeve was welded onto the pipeline and the repair was completed. The defect was limited to a single pin hole located at the 06:00 position on the weld with no anomalies observed near the girth weld. The pipeline was purged, loaded, and returned to service at 14:00 on november 17, 2018.

All rights reserved. Copyright © by ClearPHMSA