GD incident on 2018-11-24 — CA

Operator
Southern California Gas Co
Cause
Pipe, Weld, Or Joint Failure
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 3 injuries
Property damage (nominal)
$38,963
Incident datetime
2018-11-24 17:41
Report number
Location
CA, VENTURA
Narrative
On saturday, november 24, 2018, socalgas was notified by ventura county fire department (ventura county fire) of a structure fire and explosion at 493 lemar ave, oxnard. The cause of the incident is unknown; initial information provided by ventura county fire suggested possible propane involvement. There were three injuries that were transported to local hospital as a result of this incident. Damages associated with this incident exceeds $50,000. Although the gas meter assembly (msa) did not sustain damage from the fire, ventura county fire requested the service be abandoned due to extensive property damage and the potential of the weakened structure falling onto the msa. Later on november 24, 2018, once the area around the incident was safe and accessible, a socalgas crew began abandoning the service. In the process, the crew found a small leak at the service-to-main-connection (smc), which is located across the street (cortez street). The crew then proceeded to conduct leak survey and bar hole survey of the general area. Through these activities, the crew located a second leak on a 2-inch plastic main installed under lemar avenue. The crew isolated approximately 100 feet of the main to cut-off supply to that portion of the main. On monday, november 26, 2018, pipeline safety, compliance and emergency management department from socalgas became aware that natural gas indications were identified near the incident. Although the incident remains under investigation and no cause has been determined, a pipeline safety, compliance and emergency management representative notified the department of transportation and reported the incident to the cpuc. Investigation into the cause of the incident is ongoing. Tentatively, socalgas is coordinating with various parties involved to conduct a pressure test of the houseline on january 11, 2019, and an inspection of the socalgas components on january 18, 2019. For any further questions, contact khoa le at (626) 893-4536 update 2/21/19: on 1-11-2019, a site inspection was conducted at the address in question. Ha nguyen from cpuc was present. Experts representing the home insurance and socalgas were present. A pressure test of the houseline was conducted. During the test, a breach was found near the wall furnace at the houseline. A crack on a nipple and elbow of the houseline was found. Experts removed that part of the houseline and retested the remaining houseline. A couple of other leaks were found: one at the meter set assembly at a union fitting. Another leak was found at a line valve located in the garage. After the retest of houseline test, we discussed the next phase of inspecting the main line set for 1-18-2019. On 1-18-2019, another site inspection was conducted to examine the gas main pipe. Esi hosted the site inspection in irvine. All experts were present, including durga shrestha from the cpuc. Photos were taken by all parties, including digitally magnified images of the pipe surface. Discussion of future testing were pending. On 2-14-2019, another site inspection was conducted to examine the house's concrete foundation. All experts were present, including ha nguyen from the cpuc. Arrangements have been made to perform additional testing on the pipe on 3/26/19; cpuc is aware. 06-05-2019 update: - the section of main was inspected on 3/26/2019 at a 3rd party laboratory (vollmer gray laboratories in signal hills, ca). Sample was visually inspected, pressure tested and bend back tested. The identified leak cause was excessive stress, other than pressure (point load), in the vicinity of underground tree roots. After performing investigations, socalgas concludes that the cause of the explosion is undetermined.
Detailed record list
Occurred At
2018-11-24 17:41:00
Year
2018
Report Received Date
2018-12-23 00:00:00
Iyear
2018.0
Report Number
20180123.0
Supplemental Number
32262.0
Report Type
Supplemental Final
Operator Id
Name
Southern California Gas Co
Operator Street Address
555 West Fifth Street
Operator City Name
Los Angeles
Operator State Abbreviation
CA
Operator Postal Code
90013
Local Datetime
2018-11-24 08:34:00
Location Street Address
493 Lemar Avenue
Location City Name
Oxnard
Location County Name
Ventura
Location State Abbreviation
CA
Location Postal Code
93036-0000
Location Latitude
Location Longitude
Nrc Rpt Datetime
2018-11-26 08:14:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
139.0
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
3
Injure
3
Ignite Ind
Yes
Explode Ind
Yes
Num Pub Evacuated
12.0
Incident Identified Datetime
2018-11-24 17:41:00
On Site Datetime
2018-11-24 08:51:00
Federal
No
Location Type
Private Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
34.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1969.0
Pipe Diameter
2.0
Pipe Specification
Astm D2513
Pipe Manufacturer
Dupont
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11
Material Pe Pipe Code
2306
Release Type
Leak
Leak Type
Crack
Class Location Type
Class 3 Location
Est Cost Oper Paid
500000.0
Est Cost Prop Damage
38963.0
Est Cost Emergency
200.0
Est Cost Other
0.0
Est Cost Unintentional Release
834.0
Prpty
539997.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
1.0
Accident Psig
45.0
Normal Psig
45.0
Mop Psig
50.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Pipe, Weld, Or Joint Failure
Cause Details
Body Of Pipe
Pwjf Failure Type
Body Of Pipe
Pipe Body Subtype
Crack
Additional Crack Ind
Yes
Result Material Ind
Yes
Result Material Subtype
Other
Result Material Details
Axial Crack On Underside Of Main With Tree Route In Vicinity
Hydrotest Conducted Ind
No
Preparer Name
A******** H*****
Preparer Title
Pipeline Safety And Compliance Advisor
Preparer Email
A******@s**************.com
Preparer Telephone
9496972539
Authorizer Name
K*** L*
Authorizer Title
Sr Pipeline Safety And Compliance Advisor
Authorizer Telephone
6268934536
Authorizer Email
K***@s**************.com
Narrative
On saturday, november 24, 2018, socalgas was notified by ventura county fire department (ventura county fire) of a structure fire and explosion at 493 lemar ave, oxnard. The cause of the incident is unknown; initial information provided by ventura county fire suggested possible propane involvement. There were three injuries that were transported to local hospital as a result of this incident. Damages associated with this incident exceeds $50,000. Although the gas meter assembly (msa) did not sustain damage from the fire, ventura county fire requested the service be abandoned due to extensive property damage and the potential of the weakened structure falling onto the msa. Later on november 24, 2018, once the area around the incident was safe and accessible, a socalgas crew began abandoning the service. In the process, the crew found a small leak at the service-to-main-connection (smc), which is located across the street (cortez street). The crew then proceeded to conduct leak survey and bar hole survey of the general area. Through these activities, the crew located a second leak on a 2-inch plastic main installed under lemar avenue. The crew isolated approximately 100 feet of the main to cut-off supply to that portion of the main. On monday, november 26, 2018, pipeline safety, compliance and emergency management department from socalgas became aware that natural gas indications were identified near the incident. Although the incident remains under investigation and no cause has been determined, a pipeline safety, compliance and emergency management representative notified the department of transportation and reported the incident to the cpuc. Investigation into the cause of the incident is ongoing. Tentatively, socalgas is coordinating with various parties involved to conduct a pressure test of the houseline on january 11, 2019, and an inspection of the socalgas components on january 18, 2019. For any further questions, contact khoa le at (626) 893-4536 update 2/21/19: on 1-11-2019, a site inspection was conducted at the address in question. Ha nguyen from cpuc was present. Experts representing the home insurance and socalgas were present. A pressure test of the houseline was conducted. During the test, a breach was found near the wall furnace at the houseline. A crack on a nipple and elbow of the houseline was found. Experts removed that part of the houseline and retested the remaining houseline. A couple of other leaks were found: one at the meter set assembly at a union fitting. Another leak was found at a line valve located in the garage. After the retest of houseline test, we discussed the next phase of inspecting the main line set for 1-18-2019. On 1-18-2019, another site inspection was conducted to examine the gas main pipe. Esi hosted the site inspection in irvine. All experts were present, including durga shrestha from the cpuc. Photos were taken by all parties, including digitally magnified images of the pipe surface. Discussion of future testing were pending. On 2-14-2019, another site inspection was conducted to examine the house's concrete foundation. All experts were present, including ha nguyen from the cpuc. Arrangements have been made to perform additional testing on the pipe on 3/26/19; cpuc is aware. 06-05-2019 update: - the section of main was inspected on 3/26/2019 at a 3rd party laboratory (vollmer gray laboratories in signal hills, ca). Sample was visually inspected, pressure tested and bend back tested. The identified leak cause was excessive stress, other than pressure (point load), in the vicinity of underground tree roots. After performing investigations, socalgas concludes that the cause of the explosion is undetermined.
Occurred At 2018-11-24 17:41:00
Year 2018
Report Received Date 2018-12-23 00:00:00
Iyear 2018.0
Report Number 20180123.0
Supplemental Number 32262.0
Report Type Supplemental Final
Operator Id 18484 PHMSA Enforcement
Name Southern California Gas Co
Operator Street Address 555 West Fifth Street
Operator City Name Los Angeles
Operator State Abbreviation CA
Operator Postal Code 90013
Local Datetime 2018-11-24 08:34:00
Location Street Address 493 Lemar Avenue
Location City Name Oxnard
Location County Name Ventura
Location State Abbreviation CA
Location Postal Code 93036-0000
Location Latitude 34.242078 Google Maps OpenStreetMap
Location Longitude -119.157956 Google Maps OpenStreetMap
Nrc Rpt Datetime 2018-11-26 08:14:00
Nrc Rpt Num 1231360 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 139.0
Fatality Ind No
Fatal 0
Injury Ind Yes
Num Emp Injuries 0
Num Contr Injuries 0
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 3
Injure 3
Ignite Ind Yes
Explode Ind Yes
Num Pub Evacuated 12.0
Incident Identified Datetime 2018-11-24 17:41:00
On Site Datetime 2018-11-24 08:51:00
Federal No
Location Type Private Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 34.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1969.0
Pipe Diameter 2.0
Pipe Specification Astm D2513
Pipe Manufacturer Dupont
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 11
Material Pe Pipe Code 2306
Release Type Leak
Leak Type Crack
Class Location Type Class 3 Location
Est Cost Oper Paid 500000.0
Est Cost Prop Damage 38963.0
Est Cost Emergency 200.0
Est Cost Other 0.0
Est Cost Unintentional Release 834.0
Prpty 539997.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 1.0
Accident Psig 45.0
Normal Psig 45.0
Mop Psig 50.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Pipe, Weld, Or Joint Failure
Cause Details Body Of Pipe
Pwjf Failure Type Body Of Pipe
Pipe Body Subtype Crack
Additional Crack Ind Yes
Result Material Ind Yes
Result Material Subtype Other
Result Material Details Axial Crack On Underside Of Main With Tree Route In Vicinity
Hydrotest Conducted Ind No
Preparer Name A******** H*****
Preparer Title Pipeline Safety And Compliance Advisor
Preparer Email A******@s**************.com
Preparer Telephone 9496972539
Authorizer Name K*** L*
Authorizer Title Sr Pipeline Safety And Compliance Advisor
Authorizer Telephone 6268934536
Authorizer Email K***@s**************.com
Narrative On saturday, november 24, 2018, socalgas was notified by ventura county fire department (ventura county fire) of a structure fire and explosion at 493 lemar ave, oxnard. The cause of the incident is unknown; initial information provided by ventura county fire suggested possible propane involvement. There were three injuries that were transported to local hospital as a result of this incident. Damages associated with this incident exceeds $50,000. Although the gas meter assembly (msa) did not sustain damage from the fire, ventura county fire requested the service be abandoned due to extensive property damage and the potential of the weakened structure falling onto the msa. Later on november 24, 2018, once the area around the incident was safe and accessible, a socalgas crew began abandoning the service. In the process, the crew found a small leak at the service-to-main-connection (smc), which is located across the street (cortez street). The crew then proceeded to conduct leak survey and bar hole survey of the general area. Through these activities, the crew located a second leak on a 2-inch plastic main installed under lemar avenue. The crew isolated approximately 100 feet of the main to cut-off supply to that portion of the main. On monday, november 26, 2018, pipeline safety, compliance and emergency management department from socalgas became aware that natural gas indications were identified near the incident. Although the incident remains under investigation and no cause has been determined, a pipeline safety, compliance and emergency management representative notified the department of transportation and reported the incident to the cpuc. Investigation into the cause of the incident is ongoing. Tentatively, socalgas is coordinating with various parties involved to conduct a pressure test of the houseline on january 11, 2019, and an inspection of the socalgas components on january 18, 2019. For any further questions, contact khoa le at (626) 893-4536 update 2/21/19: on 1-11-2019, a site inspection was conducted at the address in question. Ha nguyen from cpuc was present. Experts representing the home insurance and socalgas were present. A pressure test of the houseline was conducted. During the test, a breach was found near the wall furnace at the houseline. A crack on a nipple and elbow of the houseline was found. Experts removed that part of the houseline and retested the remaining houseline. A couple of other leaks were found: one at the meter set assembly at a union fitting. Another leak was found at a line valve located in the garage. After the retest of houseline test, we discussed the next phase of inspecting the main line set for 1-18-2019. On 1-18-2019, another site inspection was conducted to examine the gas main pipe. Esi hosted the site inspection in irvine. All experts were present, including durga shrestha from the cpuc. Photos were taken by all parties, including digitally magnified images of the pipe surface. Discussion of future testing were pending. On 2-14-2019, another site inspection was conducted to examine the house's concrete foundation. All experts were present, including ha nguyen from the cpuc. Arrangements have been made to perform additional testing on the pipe on 3/26/19; cpuc is aware. 06-05-2019 update: - the section of main was inspected on 3/26/2019 at a 3rd party laboratory (vollmer gray laboratories in signal hills, ca). Sample was visually inspected, pressure tested and bend back tested. The identified leak cause was excessive stress, other than pressure (point load), in the vicinity of underground tree roots. After performing investigations, socalgas concludes that the cause of the explosion is undetermined.

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