GD incident on 2018-11-20 — TX

Operator
Atmos Energy Corporation - Mid-Tex
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$45,000
Incident datetime
2018-11-20 13:10
Report number
Location
TX, DALLAS
Narrative
Additional nrc report no. 1231039 on november 20, 2018, a 3rd party contractor was moving dirt off of atmos energy's row to use as fill dirt for a concrete project nearby. Atmos energy had received a locate ticket from a different contractor that included the area where the damage occurred and the scope of the ticket was marked properly. However, the contractor that caused the damage did not request a locate for the excavation that resulted in this incident. This row contains a high pressure distribution 16 inch pipeline with operating pressure of approx. 300 pounds. The contractor's employee operating the bobcat skid steer within the marked tolerance zone hit the atmos energy c-16 pipeline with the bucket tooth and damaged the line, which resulted in an indention in the pipe with a small crack within the indention where gas was released. The contractor notified atmos energy of the incident at 13:10, and atmos crews arrived at the site at 13:57. A permanent repair was made on november 29 by installing 5' of 16" steel pipe.
Detailed record list
Occurred At
2018-11-20 13:10:00
Year
2018
Report Received Date
2018-12-20 00:00:00
Iyear
2018.0
Report Number
20180121.0
Supplemental Number
31957.0
Report Type
Supplemental Final
Operator Id
Name
Atmos Energy Corporation - Mid-Tex
Operator Street Address
5430 Lbj Freeway Suite 1800
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75240
Local Datetime
2018-11-20 16:30:00
Location Street Address
5250 Frye Rd.
Location City Name
Irving
Location County Name
Dallas
Location State Abbreviation
TX
Location Postal Code
75061
Location Latitude
Location Longitude
-97.02651041
Nrc Rpt Datetime
2018-11-20 15:49:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
416.06
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2018-11-20 13:10:00
On Site Datetime
2018-11-20 13:57:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
24.0
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Other
System Part Details
Distribution/transmission Line
Installation Year
1979.0
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Straight Seam
Wt Steel
0.25
Release Type
Mechanical Puncture
Puncture Axial
1.5
Puncture Circum
0.1
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
45000.0
Est Cost Emergency
8793.0
Est Cost Other
0.0
Est Cost Unintentional Release
2158.0
Prpty
55951.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
285.0
Normal Psig
300.0
Mop Psig
325.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Easement
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Site Development
One Call Notified Ind
No
Root Cause Category
Excavation Issue
Root Cause Type
Improper Backfilling Practices
Preparer Name
R****** V****
Preparer Title
Operations Supervisor
Preparer Email
R************@a**********.com
Preparer Telephone
469-261-2140
Authorizer Name
E*** R*******
Authorizer Title
Director Regulatory And Compliance
Authorizer Telephone
214-206-2726
Authorizer Email
E************@a**********.com
Narrative
Additional nrc report no. 1231039 on november 20, 2018, a 3rd party contractor was moving dirt off of atmos energy's row to use as fill dirt for a concrete project nearby. Atmos energy had received a locate ticket from a different contractor that included the area where the damage occurred and the scope of the ticket was marked properly. However, the contractor that caused the damage did not request a locate for the excavation that resulted in this incident. This row contains a high pressure distribution 16 inch pipeline with operating pressure of approx. 300 pounds. The contractor's employee operating the bobcat skid steer within the marked tolerance zone hit the atmos energy c-16 pipeline with the bucket tooth and damaged the line, which resulted in an indention in the pipe with a small crack within the indention where gas was released. The contractor notified atmos energy of the incident at 13:10, and atmos crews arrived at the site at 13:57. A permanent repair was made on november 29 by installing 5' of 16" steel pipe.
Occurred At 2018-11-20 13:10:00
Year 2018
Report Received Date 2018-12-20 00:00:00
Iyear 2018.0
Report Number 20180121.0
Supplemental Number 31957.0
Report Type Supplemental Final
Operator Id 31348 PHMSA Enforcement
Name Atmos Energy Corporation - Mid-Tex
Operator Street Address 5430 Lbj Freeway Suite 1800
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75240
Local Datetime 2018-11-20 16:30:00
Location Street Address 5250 Frye Rd.
Location City Name Irving
Location County Name Dallas
Location State Abbreviation TX
Location Postal Code 75061
Location Latitude 32.82089613 Google Maps OpenStreetMap
Location Longitude -97.02651041 Google Maps OpenStreetMap
Nrc Rpt Datetime 2018-11-20 15:49:00
Nrc Rpt Num 1230923 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 416.06
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2018-11-20 13:10:00
On Site Datetime 2018-11-20 13:57:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 24.0
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Other
System Part Details Distribution/transmission Line
Installation Year 1979.0
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Straight Seam
Wt Steel 0.25
Release Type Mechanical Puncture
Puncture Axial 1.5
Puncture Circum 0.1
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 45000.0
Est Cost Emergency 8793.0
Est Cost Other 0.0
Est Cost Unintentional Release 2158.0
Prpty 55951.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 285.0
Normal Psig 300.0
Mop Psig 325.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
Notify Cga Dirt No
Private Row Ind Yes
Private Subtype Private Easement
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Site Development
One Call Notified Ind No
Root Cause Category Excavation Issue
Root Cause Type Improper Backfilling Practices
Preparer Name R****** V****
Preparer Title Operations Supervisor
Preparer Email R************@a**********.com
Preparer Telephone 469-261-2140
Authorizer Name E*** R*******
Authorizer Title Director Regulatory And Compliance
Authorizer Telephone 214-206-2726
Authorizer Email E************@a**********.com
Narrative Additional nrc report no. 1231039 on november 20, 2018, a 3rd party contractor was moving dirt off of atmos energy's row to use as fill dirt for a concrete project nearby. Atmos energy had received a locate ticket from a different contractor that included the area where the damage occurred and the scope of the ticket was marked properly. However, the contractor that caused the damage did not request a locate for the excavation that resulted in this incident. This row contains a high pressure distribution 16 inch pipeline with operating pressure of approx. 300 pounds. The contractor's employee operating the bobcat skid steer within the marked tolerance zone hit the atmos energy c-16 pipeline with the bucket tooth and damaged the line, which resulted in an indention in the pipe with a small crack within the indention where gas was released. The contractor notified atmos energy of the incident at 13:10, and atmos crews arrived at the site at 13:57. A permanent repair was made on november 29 by installing 5' of 16" steel pipe.

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