GD incident on 2018-11-19 — CA

Operator
Pacific Gas & Electric Co
Cause
Locating Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2018-11-19 14:04
Report number
Location
CA, MARIN
Narrative
On monday, november 19, 2018 at 14:04 hours, pg&e was notified of a third party dig in at 104 somerset dr, in the city of novato. A third party contractor, fiberco, struck a 4" distribution plastic main while directional boring causing a gas release. There was a valid USA ticket (x831002460) and the locator failed to mark the 4" plastic gas main. The repair crew arrived on-site at 14:20 hours and stopped the flow of gas by closing two valves and squeezing a 6" steel main by 19:15 hours. Service was impacted to 16 gas customers. Repairs were completed on 11/20/18 at 15:30 hours. Fire department was reported onsite. There were no police, injuries, fatalities, media or ignition associated with this incident. The incident was reported to the DOT and cpuc due to the estimated property damage exceeding $50,000 which was determined at approximately 23:00 hours on november 19, 2018.
Detailed record list
Occurred At
2018-11-19 14:04:00
Year
2018
Report Received Date
2018-12-19 00:00:00
Iyear
2018.0
Report Number
20180120.0
Supplemental Number
31397.0
Report Type
Supplemental Final
Operator Id
Name
Pacific Gas & Electric Co
Operator Street Address
6121 Bollinger Canyon Rd.
Operator City Name
San Ramon
Operator State Abbreviation
CA
Operator Postal Code
94583
Local Datetime
2018-11-19 14:04:00
Location Street Address
104 Somerset Dr
Location City Name
Novato
Location County Name
Marin
Location State Abbreviation
CA
Location Postal Code
94945
Location Latitude
Location Longitude
Nrc Rpt Datetime
2018-11-19 23:22:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
1330.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
16.0
Incident Identified Datetime
2018-11-19 14:04:00
On Site Datetime
2018-11-19 14:20:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
49.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1990.0
Pipe Diameter
4.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Plastic
Plastic Type
Unknown
Wt Plastic Unknown Ind
Unknown
Release Type
Mechanical Puncture
Puncture Axial
2.0
Puncture Circum
1.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
50000.0
Est Cost Prop Damage
0.0
Est Cost Emergency
0.0
Est Cost Other
0.0
Est Cost Unintentional Release
4000.0
Prpty
54000.0
Commercial Affected
1.0
Industrial Affected
0.0
Residences Affected
15.0
Accident Psig
50.0
Normal Psig
50.0
Mop Psig
56.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
City Street
Excavator Type
Contractor
Excavator Equipment
Drilling
Work Performed
Telecommunications
One Call Notified Ind
Yes
One Call Ticket Num
831002460
Locator Type
Utility Owner
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
21.0
Root Cause Category
Locating Issue
Root Cause Type
Facility Not Marked Due To Incomplete Marks At Damage Location
Preparer Name
E*** B******
Preparer Title
Program Manager
Preparer Email
E***@p**.com
Authorizer Name
S**** R*******
Authorizer Title
Manager Of Gas Operations Compliance And Risk
Authorizer Telephone
925-328-5776
Authorizer Email
G***@p**.com
Narrative
On monday, november 19, 2018 at 14:04 hours, pg&e was notified of a third party dig in at 104 somerset dr, in the city of novato. A third party contractor, fiberco, struck a 4" distribution plastic main while directional boring causing a gas release. There was a valid USA ticket (x831002460) and the locator failed to mark the 4" plastic gas main. The repair crew arrived on-site at 14:20 hours and stopped the flow of gas by closing two valves and squeezing a 6" steel main by 19:15 hours. Service was impacted to 16 gas customers. Repairs were completed on 11/20/18 at 15:30 hours. Fire department was reported onsite. There were no police, injuries, fatalities, media or ignition associated with this incident. The incident was reported to the DOT and cpuc due to the estimated property damage exceeding $50,000 which was determined at approximately 23:00 hours on november 19, 2018.
Occurred At 2018-11-19 14:04:00
Year 2018
Report Received Date 2018-12-19 00:00:00
Iyear 2018.0
Report Number 20180120.0
Supplemental Number 31397.0
Report Type Supplemental Final
Operator Id 15007 PHMSA Enforcement
Name Pacific Gas & Electric Co
Operator Street Address 6121 Bollinger Canyon Rd.
Operator City Name San Ramon
Operator State Abbreviation CA
Operator Postal Code 94583
Local Datetime 2018-11-19 14:04:00
Location Street Address 104 Somerset Dr
Location City Name Novato
Location County Name Marin
Location State Abbreviation CA
Location Postal Code 94945
Location Latitude 38.120566 Google Maps OpenStreetMap
Location Longitude -122.579743 Google Maps OpenStreetMap
Nrc Rpt Datetime 2018-11-19 23:22:00
Nrc Rpt Num 1230868 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 1330.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 16.0
Incident Identified Datetime 2018-11-19 14:04:00
On Site Datetime 2018-11-19 14:20:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 49.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1990.0
Pipe Diameter 4.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Plastic
Plastic Type Unknown
Wt Plastic Unknown Ind Unknown
Release Type Mechanical Puncture
Puncture Axial 2.0
Puncture Circum 1.0
Class Location Type Class 3 Location
Est Cost Oper Paid 50000.0
Est Cost Prop Damage 0.0
Est Cost Emergency 0.0
Est Cost Other 0.0
Est Cost Unintentional Release 4000.0
Prpty 54000.0
Commercial Affected 1.0
Industrial Affected 0.0
Residences Affected 15.0
Accident Psig 50.0
Normal Psig 50.0
Mop Psig 56.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype City Street
Excavator Type Contractor
Excavator Equipment Drilling
Work Performed Telecommunications
One Call Notified Ind Yes
One Call Ticket Num 831002460
Locator Type Utility Owner
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 21.0
Root Cause Category Locating Issue
Root Cause Type Facility Not Marked Due To Incomplete Marks At Damage Location
Preparer Name E*** B******
Preparer Title Program Manager
Preparer Email E***@p**.com
Authorizer Name S**** R*******
Authorizer Title Manager Of Gas Operations Compliance And Risk
Authorizer Telephone 925-328-5776
Authorizer Email G***@p**.com
Narrative On monday, november 19, 2018 at 14:04 hours, pg&e was notified of a third party dig in at 104 somerset dr, in the city of novato. A third party contractor, fiberco, struck a 4" distribution plastic main while directional boring causing a gas release. There was a valid USA ticket (x831002460) and the locator failed to mark the 4" plastic gas main. The repair crew arrived on-site at 14:20 hours and stopped the flow of gas by closing two valves and squeezing a 6" steel main by 19:15 hours. Service was impacted to 16 gas customers. Repairs were completed on 11/20/18 at 15:30 hours. Fire department was reported onsite. There were no police, injuries, fatalities, media or ignition associated with this incident. The incident was reported to the DOT and cpuc due to the estimated property damage exceeding $50,000 which was determined at approximately 23:00 hours on november 19, 2018.

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