GTG incident on 2018-10-18 — TX

Operator
Energy Transfer Company
Cause
Corrosion Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$250,000
Incident datetime
2018-10-18 11:10
Report number
Location
TX
Narrative
On 10-18-18 at approximately 10:50am, energy transfer experienced a release of natural gas on the 3045 aqua dulce to loma blanca system in kingsville, tx. Energy transfer personnel arrived on site at approximately 11:08 am and identified at 11:10 am that the pipeline belonged to energy transfer. Company personnel immediately proceeded to shut in pipeline by shutting in the upstream mainline valve and downstream mainline valve at 11:35am and 12:07pm respectively. The affected pipe segment was cut out and sent to a laboratory for testing and replaced with pre-tested pipe. Energy transfer ran multiple ili inspection tools to verify pipeline integrity. The pipeline will be brought back to normal service following successful ili inspection. The cause of this release is currently under investigation. 48hr follow up nrc # 1227958. This facility is under the jurisdiction of the texas railroad commission. Update made on 3/29/2019 the cause of this release has been identified as external microbiologically induced corrosion. The pipeline was brought back to service with no pressure restrictions on 3-21-19 following a successful ili assessment. Update made on 9/6/2019 we received a final root cause analysis from a 3rd party contractor. Their analysis attributed the cause of the failure to external corrosion which led to a ductile overload. In an effort to prevent reoccurrence , energy transfer will be conducting additional verification digs on this system and a close interval survey will be conducted in conjunction with the next scheduled in line inspection.
Detailed record list
Report Received Date
2018-11-16 00:00:00
Iyear
2018
Report Number
20180117
Supplemental Number
32673
Report Type
Supplemental Final
Operator Id
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-10-18 10:50:00
Location Latitude
Location Longitude
-97.96194444
Nrc Rpt Num
Nrc Rpt Datetime
2018-10-18 13:26:00
Commodity Released Type
Natural Gas
Unintentional Release
213570
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-10-18 11:35:00
Restart Datetime
2018-11-12 09:00:00
Ignite Ind
Yes
Explode Ind
Yes
Num Pub Evacuated
0
Incident Identified Datetime
2018-10-18 11:10:00
On Site Datetime
2018-10-18 11:08:00
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
78364
Onshore City Name
Kingsville
Onshore County Name
Kleberg
Designated Location
Milepost
Designated Name
498+54
Pipe Fac Name
3045 Aqua Dulce To Loma Blanca
Segment Name
3045 Aqua Dulce To Loma Blanca
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
96
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
16
Pipe Wall Thickness
0.25
Pipe Smys
52000
Pipe Specification
Api 5l
Pipe Seam Type
Other
Pipe Seam Details
Longitudinal Erw - Dc
Pipe Manufacturer
Youngstown Sheet And Tube
Pipe Coating Type
Coal Tar
Installation Year
1964
Manufactured Year
1964
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Circumferential
Rupture Length
16
Rupture Width
21.5
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
425
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
728273
Est Cost Intentional Release
0
Est Cost Prop Damage
250000
Est Cost Emergency
0
Est Cost Other
0
Prpty
978273
Accident Psig
1140
Mop Psig
1170
Mop Cfr Section
192.619(A)(1)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
41554
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Controller Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
2
Num Employees Failed
0
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
General Corrosion
Microbiological Corrosion Ind
Yes
Metallurgical Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1965
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Cp Annual Survey Year
2018
Close Interval Survey Year
2018
Prior Damage
Yes
Collected Data Ind
Yes
Other Tool Tech Ind
Yes
Other Tool
Combination Tool
Other Recent Year
2013
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
A******** A*****
Preparer Title
Regulatory Compliance Engineer
Preparer Email
A***************@e*************.com
Preparer Telephone
713-989-2021
Authorizer Name
D**** N******
Authorizer Title
Sr. Director Of Regulatory Compliance
Authorizer Telephone
713-989-7232
Authorizer Email
D************@e*************.com
Narrative
On 10-18-18 at approximately 10:50am, energy transfer experienced a release of natural gas on the 3045 aqua dulce to loma blanca system in kingsville, tx. Energy transfer personnel arrived on site at approximately 11:08 am and identified at 11:10 am that the pipeline belonged to energy transfer. Company personnel immediately proceeded to shut in pipeline by shutting in the upstream mainline valve and downstream mainline valve at 11:35am and 12:07pm respectively. The affected pipe segment was cut out and sent to a laboratory for testing and replaced with pre-tested pipe. Energy transfer ran multiple ili inspection tools to verify pipeline integrity. The pipeline will be brought back to normal service following successful ili inspection. The cause of this release is currently under investigation. 48hr follow up nrc # 1227958. This facility is under the jurisdiction of the texas railroad commission. Update made on 3/29/2019 the cause of this release has been identified as external microbiologically induced corrosion. The pipeline was brought back to service with no pressure restrictions on 3-21-19 following a successful ili assessment. Update made on 9/6/2019 we received a final root cause analysis from a 3rd party contractor. Their analysis attributed the cause of the failure to external corrosion which led to a ductile overload. In an effort to prevent reoccurrence , energy transfer will be conducting additional verification digs on this system and a close interval survey will be conducted in conjunction with the next scheduled in line inspection.
Report Received Date 2018-11-16 00:00:00
Iyear 2018
Report Number 20180117
Supplemental Number 32673
Report Type Supplemental Final
Operator Id 32099 PHMSA Enforcement
Name Energy Transfer Company
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-10-18 10:50:00
Location Latitude 27.52888889 Google Maps OpenStreetMap
Location Longitude -97.96194444 Google Maps OpenStreetMap
Nrc Rpt Num 1227857 NRC Report How to search
Nrc Rpt Datetime 2018-10-18 13:26:00
Commodity Released Type Natural Gas
Unintentional Release 213570
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-10-18 11:35:00
Restart Datetime 2018-11-12 09:00:00
Ignite Ind Yes
Explode Ind Yes
Num Pub Evacuated 0
Incident Identified Datetime 2018-10-18 11:10:00
On Site Datetime 2018-10-18 11:08:00
On Off Shore Onshore
Onshore State Abbreviation Tx
Onshore Postal Code 78364
Onshore City Name Kingsville
Onshore County Name Kleberg
Designated Location Milepost
Designated Name 498+54
Pipe Fac Name 3045 Aqua Dulce To Loma Blanca
Segment Name 3045 Aqua Dulce To Loma Blanca
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 96
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 16
Pipe Wall Thickness 0.25
Pipe Smys 52000
Pipe Specification Api 5l
Pipe Seam Type Other
Pipe Seam Details Longitudinal Erw - Dc
Pipe Manufacturer Youngstown Sheet And Tube
Pipe Coating Type Coal Tar
Installation Year 1964
Manufactured Year 1964
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Circumferential
Rupture Length 16
Rupture Width 21.5
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 425
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 728273
Est Cost Intentional Release 0
Est Cost Prop Damage 250000
Est Cost Emergency 0
Est Cost Other 0
Prpty 978273
Accident Psig 1140
Mop Psig 1170
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 41554
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Controller Ind Yes
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 2
Num Employees Failed 0
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results General Corrosion
Microbiological Corrosion Ind Yes
Metallurgical Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1965
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Close Interval Survey Ind Yes
Cp Annual Survey Year 2018
Close Interval Survey Year 2018
Prior Damage Yes
Collected Data Ind Yes
Other Tool Tech Ind Yes
Other Tool Combination Tool
Other Recent Year 2013
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name A******** A*****
Preparer Title Regulatory Compliance Engineer
Preparer Email A***************@e*************.com
Preparer Telephone 713-989-2021
Authorizer Name D**** N******
Authorizer Title Sr. Director Of Regulatory Compliance
Authorizer Telephone 713-989-7232
Authorizer Email D************@e*************.com
Narrative On 10-18-18 at approximately 10:50am, energy transfer experienced a release of natural gas on the 3045 aqua dulce to loma blanca system in kingsville, tx. Energy transfer personnel arrived on site at approximately 11:08 am and identified at 11:10 am that the pipeline belonged to energy transfer. Company personnel immediately proceeded to shut in pipeline by shutting in the upstream mainline valve and downstream mainline valve at 11:35am and 12:07pm respectively. The affected pipe segment was cut out and sent to a laboratory for testing and replaced with pre-tested pipe. Energy transfer ran multiple ili inspection tools to verify pipeline integrity. The pipeline will be brought back to normal service following successful ili inspection. The cause of this release is currently under investigation. 48hr follow up nrc # 1227958. This facility is under the jurisdiction of the texas railroad commission. Update made on 3/29/2019 the cause of this release has been identified as external microbiologically induced corrosion. The pipeline was brought back to service with no pressure restrictions on 3-21-19 following a successful ili assessment. Update made on 9/6/2019 we received a final root cause analysis from a 3rd party contractor. Their analysis attributed the cause of the failure to external corrosion which led to a ductile overload. In an effort to prevent reoccurrence , energy transfer will be conducting additional verification digs on this system and a close interval survey will be conducted in conjunction with the next scheduled in line inspection.

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