GTG incident on 2018-09-06 — NE

Operator
Northern Natural Gas Co
Cause
Equipment Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$300
Incident datetime
2018-09-06 05:30
Report number
Location
NE
Narrative
On september 6, 2018 at 0657 - operations at beatrice reported blowing gas at the beatrice station. Operations discovered a broken valve nipple on the 1-inch diameter m590 c to d discharge line. The line connects the 24-inch diameter manifold to the 590c mainline. The segment was isolated and nipple, valve and plug were installed at 0930 on september 6, 2018. Fisher valve stated the noise and vibration exceeded the recommended levels on the control valve at the cross-over. Fisher valve will make recommendations to rectify the problem.
Detailed record list
Report Received Date
2018-09-17 00:00:00
Iyear
2018
Report Number
20180094
Supplemental Number
31814
Report Type
Supplemental Final
Operator Id
Name
Northern Natural Gas Co
Operator Street Address
1111 South 103rd Street
Operator City Name
Omaha
Operator State Abbreviation
NE
Operator Postal Code
68124
Local Datetime
2018-09-06 05:30:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2018-09-06 13:05:00
Commodity Released Type
Natural Gas
Unintentional Release
3685
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
No
Shutdown Explain
Pressure Reduced Between Two Cross-Over Valves
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2018-09-06 05:30:00
On Site Datetime
2018-09-06 06:00:00
On Off Shore
Onshore
Onshore State Abbreviation
Ne
Onshore Postal Code
68310
Onshore City Name
Not Within A Municipality
Onshore County Name
Gage Count
Designated Location
Survey Station No.
Designated Name
Beatrice
Pipe Fac Name
Beatrice Station
Segment Name
179m590d
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Other
Item Involved Details
1-Inch Nipple Broke From A Cross-Over Lo
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
1-Inch Nipple To A Cross-Over Valve With Regulator Broke. The Cross-Over Valve Is Between Two Pipelines. The Regulator Remained Functional.
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
607
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
8055
Est Cost Intentional Release
0
Est Cost Prop Damage
300
Est Cost Emergency
2500
Est Cost Other
0
Prpty
10855
Accident Psig
800
Mop Psig
860
Mop Cfr Section
192.619(A)(1)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Internal Inspection Ind
No
Tight Mitered Ind
Yes
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
Cross-0ver Section
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Eq Failure Details
1-Inch Nipple Broke Between Cross-Over Valves With Regulator On Cross-Over.
Additional Vibration Ind
Yes
Preparer Name
K** A*******
Preparer Title
Senior Internal Corrosion Engineer
Preparer Email
K***********@n****.com
Preparer Telephone
402-398-7617
Authorizer Name
K** A*******
Authorizer Title
Senior Internal Corrosion Engineer
Authorizer Telephone
402-398-7617
Authorizer Email
K************@n****.com
Narrative
On september 6, 2018 at 0657 - operations at beatrice reported blowing gas at the beatrice station. Operations discovered a broken valve nipple on the 1-inch diameter m590 c to d discharge line. The line connects the 24-inch diameter manifold to the 590c mainline. The segment was isolated and nipple, valve and plug were installed at 0930 on september 6, 2018. Fisher valve stated the noise and vibration exceeded the recommended levels on the control valve at the cross-over. Fisher valve will make recommendations to rectify the problem.
Report Received Date 2018-09-17 00:00:00
Iyear 2018
Report Number 20180094
Supplemental Number 31814
Report Type Supplemental Final
Operator Id 13750 PHMSA Enforcement
Name Northern Natural Gas Co
Operator Street Address 1111 South 103rd Street
Operator City Name Omaha
Operator State Abbreviation NE
Operator Postal Code 68124
Local Datetime 2018-09-06 05:30:00
Location Latitude 40.2205 Google Maps OpenStreetMap
Location Longitude -96.7408 Google Maps OpenStreetMap
Nrc Rpt Num 1223813 NRC Report How to search
Nrc Rpt Datetime 2018-09-06 13:05:00
Commodity Released Type Natural Gas
Unintentional Release 3685
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind No
Shutdown Explain Pressure Reduced Between Two Cross-Over Valves
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2018-09-06 05:30:00
On Site Datetime 2018-09-06 06:00:00
On Off Shore Onshore
Onshore State Abbreviation Ne
Onshore Postal Code 68310
Onshore City Name Not Within A Municipality
Onshore County Name Gage Count
Designated Location Survey Station No.
Designated Name Beatrice
Pipe Fac Name Beatrice Station
Segment Name 179m590d
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Other
Item Involved Details 1-Inch Nipple Broke From A Cross-Over Lo
Installation Year Unknown
Material Involved Carbon Steel
Release Type Other
Release Type Details 1-Inch Nipple To A Cross-Over Valve With Regulator Broke. The Cross-Over Valve Is Between Two Pipelines. The Regulator Remained Functional.
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 607
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 8055
Est Cost Intentional Release 0
Est Cost Prop Damage 300
Est Cost Emergency 2500
Est Cost Other 0
Prpty 10855
Accident Psig 800
Mop Psig 860
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Internal Inspection Ind No
Tight Mitered Ind Yes
Operation Complications Ind Yes
Other Complications Ind Yes
Inspect Comp Details Cross-0ver Section
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Eq Failure Details 1-Inch Nipple Broke Between Cross-Over Valves With Regulator On Cross-Over.
Additional Vibration Ind Yes
Preparer Name K** A*******
Preparer Title Senior Internal Corrosion Engineer
Preparer Email K***********@n****.com
Preparer Telephone 402-398-7617
Authorizer Name K** A*******
Authorizer Title Senior Internal Corrosion Engineer
Authorizer Telephone 402-398-7617
Authorizer Email K************@n****.com
Narrative On september 6, 2018 at 0657 - operations at beatrice reported blowing gas at the beatrice station. Operations discovered a broken valve nipple on the 1-inch diameter m590 c to d discharge line. The line connects the 24-inch diameter manifold to the 590c mainline. The segment was isolated and nipple, valve and plug were installed at 0930 on september 6, 2018. Fisher valve stated the noise and vibration exceeded the recommended levels on the control valve at the cross-over. Fisher valve will make recommendations to rectify the problem.

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