GD incident on 2018-08-09 — PA

Operator
Ugi Central Penn Gas, Inc
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$15,500
Incident datetime
2018-08-09 11:05
Report number
Location
PA, LYCOMING
Narrative
**this a supplementary report to update the total damage and repair cost in part d.2. A typo was also found in the 1-call ticket number for the work in part g3.9, the report incorrectly stated 2014062791 when it should have been 2018062791. This supplementary report will be the last report filed for this event. ** a contractor was installing a new gas pipeline to replace an existing gas pipeline. The contractor hit a service line, and pulled the service tap off the existing main. Three houses in the vicinity of the line hit were evacuated and electric power was shut off. Valves could have been closed to promptly isolate the leak, and if this was done, the incident reporting criteria would not have been met. Closing valves would have resulted in loss of gas service to over 2000 customers including 2 hospitals. Ugi made the decision to allow the gas to vent to a safe area while a temporary bypass was installed. The nrc was called when gas loss calculations indicated that over 3000 mcf would be vented. The cost of installing the bypass also exceeded $50,000.
Detailed record list
Occurred At
2018-08-09 11:05:00
Year
2018
Report Received Date
2018-09-07 00:00:00
Iyear
2018.0
Report Number
20180083.0
Supplemental Number
31878.0
Report Type
Supplemental Final
Operator Id
Name
Ugi Central Penn Gas, Inc
Operator Street Address
1 Ugi Drive
Operator City Name
Denver
Operator State Abbreviation
PA
Operator Postal Code
17517
Local Datetime
2018-08-09 11:08:00
Location Street Address
304 Tombs Run Road
Location City Name
Jersey Shore
Location County Name
Lycoming
Location State Abbreviation
PA
Location Postal Code
17740
Location Latitude
Location Longitude
Nrc Rpt Datetime
2018-08-09 15:22:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
15992.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
3.0
Incident Identified Datetime
2018-08-09 11:05:00
On Site Datetime
2018-08-09 11:34:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1961.0
Pipe Diameter
6.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Wt Steel
0.156
Release Type
Leak
Leak Type
Connection Failure
Class Location Type
Class 1 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
15500.0
Est Cost Emergency
187000.0
Est Cost Other
0.0
Est Cost Unintentional Release
37263.0
Prpty
239763.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
1.0
Accident Psig
326.0
Normal Psig
327.0
Mop Psig
350.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Incident was caused by excavation damage and emergency response was promptly handled by ugi's contact center and dispatch. Controller action and control room issues did not create the incident nor impact emergency response.
Employee Drug Test Ind
No
Contractor Drug Test Ind
Yes
Num Contractors Tested
2
Num Contractors Failed
0
Cause
Excavation Damage
Cause Details
Excavation Damage By Operator's Contractor (Second Party)
Ex Party Type
Excavation Damage By Operator's Contractor (Second Party)
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
County Road
Pipeline Easement Row Ind
Yes
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Natural Gas
One Call Notified Ind
Yes
One Call Ticket Num
20181062791
Locator Type
Utility Owner
Visible Marks
Yes
Root Cause Category
Excavation Issue
Root Cause Type
Marks Faded Or Not Maintained
Preparer Name
F**** B******
Preparer Title
Directror Engineering And Technical Services
Preparer Email
F*******@u**.com
Preparer Telephone
6107963567
Authorizer Name
K**** B*****
Authorizer Title
Vp Engineering And Operations Support
Authorizer Telephone
6107963601
Authorizer Email
K******@u**.com
Narrative
**this a supplementary report to update the total damage and repair cost in part d.2. A typo was also found in the 1-call ticket number for the work in part g3.9, the report incorrectly stated 2014062791 when it should have been 2018062791. This supplementary report will be the last report filed for this event. ** a contractor was installing a new gas pipeline to replace an existing gas pipeline. The contractor hit a service line, and pulled the service tap off the existing main. Three houses in the vicinity of the line hit were evacuated and electric power was shut off. Valves could have been closed to promptly isolate the leak, and if this was done, the incident reporting criteria would not have been met. Closing valves would have resulted in loss of gas service to over 2000 customers including 2 hospitals. Ugi made the decision to allow the gas to vent to a safe area while a temporary bypass was installed. The nrc was called when gas loss calculations indicated that over 3000 mcf would be vented. The cost of installing the bypass also exceeded $50,000.
Occurred At 2018-08-09 11:05:00
Year 2018
Report Received Date 2018-09-07 00:00:00
Iyear 2018.0
Report Number 20180083.0
Supplemental Number 31878.0
Report Type Supplemental Final
Operator Id 31467 PHMSA Enforcement
Name Ugi Central Penn Gas, Inc
Operator Street Address 1 Ugi Drive
Operator City Name Denver
Operator State Abbreviation PA
Operator Postal Code 17517
Local Datetime 2018-08-09 11:08:00
Location Street Address 304 Tombs Run Road
Location City Name Jersey Shore
Location County Name Lycoming
Location State Abbreviation PA
Location Postal Code 17740
Location Latitude 41.25732 Google Maps OpenStreetMap
Location Longitude -77.27101 Google Maps OpenStreetMap
Nrc Rpt Datetime 2018-08-09 15:22:00
Nrc Rpt Num 1221035 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 15992.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 3.0
Incident Identified Datetime 2018-08-09 11:05:00
On Site Datetime 2018-08-09 11:34:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1961.0
Pipe Diameter 6.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Wt Steel 0.156
Release Type Leak
Leak Type Connection Failure
Class Location Type Class 1 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 15500.0
Est Cost Emergency 187000.0
Est Cost Other 0.0
Est Cost Unintentional Release 37263.0
Prpty 239763.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 1.0
Accident Psig 326.0
Normal Psig 327.0
Mop Psig 350.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Incident was caused by excavation damage and emergency response was promptly handled by ugi's contact center and dispatch. Controller action and control room issues did not create the incident nor impact emergency response.
Employee Drug Test Ind No
Contractor Drug Test Ind Yes
Num Contractors Tested 2
Num Contractors Failed 0
Cause Excavation Damage
Cause Details Excavation Damage By Operator's Contractor (Second Party)
Ex Party Type Excavation Damage By Operator's Contractor (Second Party)
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype County Road
Pipeline Easement Row Ind Yes
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Natural Gas
One Call Notified Ind Yes
One Call Ticket Num 20181062791
Locator Type Utility Owner
Visible Marks Yes
Root Cause Category Excavation Issue
Root Cause Type Marks Faded Or Not Maintained
Preparer Name F**** B******
Preparer Title Directror Engineering And Technical Services
Preparer Email F*******@u**.com
Preparer Telephone 6107963567
Authorizer Name K**** B*****
Authorizer Title Vp Engineering And Operations Support
Authorizer Telephone 6107963601
Authorizer Email K******@u**.com
Narrative **this a supplementary report to update the total damage and repair cost in part d.2. A typo was also found in the 1-call ticket number for the work in part g3.9, the report incorrectly stated 2014062791 when it should have been 2018062791. This supplementary report will be the last report filed for this event. ** a contractor was installing a new gas pipeline to replace an existing gas pipeline. The contractor hit a service line, and pulled the service tap off the existing main. Three houses in the vicinity of the line hit were evacuated and electric power was shut off. Valves could have been closed to promptly isolate the leak, and if this was done, the incident reporting criteria would not have been met. Closing valves would have resulted in loss of gas service to over 2000 customers including 2 hospitals. Ugi made the decision to allow the gas to vent to a safe area while a temporary bypass was installed. The nrc was called when gas loss calculations indicated that over 3000 mcf would be vented. The cost of installing the bypass also exceeded $50,000.

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