Incident details
Operator, cause, commodity and consequences with raw source fields.
GD incident on 2018-05-12 — MI
Operator
Dte Gas Company
Cause
Other Outside Force Damage
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities
1 injury
Property damage (nominal)
$77,258
Incident datetime
2018-05-12 05:00
Report number
Location
MI, WAYNE COUNTY
Narrative
Dte gas received a call from trenton fire department of a vehicle hit of a gas line at 6:12am. Dte gas was onsite at 6:51pm. Once dte gas first responders were on seen it was confirmed that a driver had hit the high-head extension at the location. There was a leak as a result of the incident. The driver was taken to the hospital and drug & alcohol testing was performed. Result. This leak impacted 3 businesses. The mpsc was contacted at 11:33am once it was realized that the repair was going to be approximately $10,000. Gas was off at 15:03pm on 5/12/18 with a release of gas of 13 mcf. On august 3rd, 2018, the repair cost report was received and was $96,988. The nrc was contacted at on 8/3/18 at 10:33am to report the incident based on cost to the operator.
Detailed record list
Occurred At
2018-05-12 05:00:00
Year
2018
Report Received Date
2018-09-02 00:00:00
Iyear
2018.0
Report Number
20180081.0
Supplemental Number
30886.0
Report Type
Original Final
Operator Id
12408
Name
Dte Gas Company
Operator Street Address
1 Energy Plaza
Operator City Name
Detroit
Operator State Abbreviation
MI
Operator Postal Code
48226
Local Datetime
2018-05-12 05:00:00
Location Street Address
4695 W Jefferson
Location City Name
Trenton
Location County Name
Wayne County
Location State Abbreviation
MI
Location Postal Code
48183
Location Latitude
42.122087
Location Longitude
-83.179768
Nrc Rpt Datetime
2018-08-03 10:33:00
Nrc Rpt Num
1220406
Commodity Released Type
Natural Gas
Unintentional Release
13.0
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
1
Injure
1
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2018-05-12 05:00:00
On Site Datetime
2018-05-12 05:28:00
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Other
System Part Details
High-Head Extension Equipment
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Leak
Leak Type
Connection Failure
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
77258.0
Est Cost Emergency
19693.0
Est Cost Other
0.0
Est Cost Unintentional Release
37.0
Prpty
96988.0
Commercial Affected
0.0
Industrial Affected
3.0
Residences Affected
0.0
Accident Psig
145.0
Normal Psig
145.0
Mop Psig
150.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype
Third Party
Preparer Name
F***** F* S****
Preparer Title
Manager
Preparer Email
F***********@d********.com
Preparer Telephone
313-389-7762
Preparer Fax
313-389-7755
Authorizer Name
F***** F* S****
Authorizer Title
Manager
Authorizer Telephone
313-460-1681
Authorizer Email
F***********@d********.com
Narrative
Dte gas received a call from trenton fire department of a vehicle hit of a gas line at 6:12am. Dte gas was onsite at 6:51pm. Once dte gas first responders were on seen it was confirmed that a driver had hit the high-head extension at the location. There was a leak as a result of the incident. The driver was taken to the hospital and drug & alcohol testing was performed. Result. This leak impacted 3 businesses. The mpsc was contacted at 11:33am once it was realized that the repair was going to be approximately $10,000. Gas was off at 15:03pm on 5/12/18 with a release of gas of 13 mcf. On august 3rd, 2018, the repair cost report was received and was $96,988. The nrc was contacted at on 8/3/18 at 10:33am to report the incident based on cost to the operator.
| Occurred At | 2018-05-12 05:00:00 |
|---|---|
| Year | 2018 |
| Report Received Date | 2018-09-02 00:00:00 |
| Iyear | 2018.0 |
| Report Number | 20180081.0 |
| Supplemental Number | 30886.0 |
| Report Type | Original Final |
| Operator Id | 12408 PHMSA Enforcement |
| Name | Dte Gas Company |
| Operator Street Address | 1 Energy Plaza |
| Operator City Name | Detroit |
| Operator State Abbreviation | MI |
| Operator Postal Code | 48226 |
| Local Datetime | 2018-05-12 05:00:00 |
| Location Street Address | 4695 W Jefferson |
| Location City Name | Trenton |
| Location County Name | Wayne County |
| Location State Abbreviation | MI |
| Location Postal Code | 48183 |
| Location Latitude | 42.122087 Google Maps OpenStreetMap |
| Location Longitude | -83.179768 Google Maps OpenStreetMap |
| Nrc Rpt Datetime | 2018-08-03 10:33:00 |
| Nrc Rpt Num | 1220406 NRC Report How to search |
| Commodity Released Type | Natural Gas |
| Unintentional Release | 13.0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | Yes |
| Num Emp Injuries | 0 |
| Num Contr Injuries | 0 |
| Num Er Injuries | 0 |
| Num Worker Injuries | 0 |
| Num Gp Injuries | 1 |
| Injure | 1 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0.0 |
| Incident Identified Datetime | 2018-05-12 05:00:00 |
| On Site Datetime | 2018-05-12 05:28:00 |
| Federal | No |
| Location Type | Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set) |
| Crossing | No |
| Pipe Facility Type | Privately Owned |
| System Part Involved | Other |
| System Part Details | High-Head Extension Equipment |
| Material Involved | Steel |
| Steel Seam Type | Other |
| Steel Seam Type Details | Unknown |
| Release Type | Leak |
| Leak Type | Connection Failure |
| Class Location Type | Class 3 Location |
| Est Cost Oper Paid | 0.0 |
| Est Cost Prop Damage | 77258.0 |
| Est Cost Emergency | 19693.0 |
| Est Cost Other | 0.0 |
| Est Cost Unintentional Release | 37.0 |
| Prpty | 96988.0 |
| Commercial Affected | 0.0 |
| Industrial Affected | 3.0 |
| Residences Affected | 0.0 |
| Accident Psig | 145.0 |
| Normal Psig | 145.0 |
| Mop Psig | 150.0 |
| Accident Pressure | Pressure Did Not Exceed Maop |
| Scada In Place Ind | No |
| Accident Identifier | Notification From Emergency Responder |
| Investigation Status | No, the facility was not monitored by a controller(s) at the time of the incident |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Other Outside Force Damage |
| Cause Details | Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation |
| Outside Force Type | Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation |
| Vehicle Subtype | Third Party |
| Preparer Name | F***** F* S**** |
| Preparer Title | Manager |
| Preparer Email | F***********@d********.com |
| Preparer Telephone | 313-389-7762 |
| Preparer Fax | 313-389-7755 |
| Authorizer Name | F***** F* S**** |
| Authorizer Title | Manager |
| Authorizer Telephone | 313-460-1681 |
| Authorizer Email | F***********@d********.com |
| Narrative | Dte gas received a call from trenton fire department of a vehicle hit of a gas line at 6:12am. Dte gas was onsite at 6:51pm. Once dte gas first responders were on seen it was confirmed that a driver had hit the high-head extension at the location. There was a leak as a result of the incident. The driver was taken to the hospital and drug & alcohol testing was performed. Result. This leak impacted 3 businesses. The mpsc was contacted at 11:33am once it was realized that the repair was going to be approximately $10,000. Gas was off at 15:03pm on 5/12/18 with a release of gas of 13 mcf. On august 3rd, 2018, the repair cost report was received and was $96,988. The nrc was contacted at on 8/3/18 at 10:33am to report the incident based on cost to the operator. |
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