GD incident on 2018-05-12 — MI

Operator
Dte Gas Company
Cause
Other Outside Force Damage
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 1 injury
Property damage (nominal)
$77,258
Incident datetime
2018-05-12 05:00
Report number
Location
MI, WAYNE COUNTY
Narrative
Dte gas received a call from trenton fire department of a vehicle hit of a gas line at 6:12am. Dte gas was onsite at 6:51pm. Once dte gas first responders were on seen it was confirmed that a driver had hit the high-head extension at the location. There was a leak as a result of the incident. The driver was taken to the hospital and drug & alcohol testing was performed. Result. This leak impacted 3 businesses. The mpsc was contacted at 11:33am once it was realized that the repair was going to be approximately $10,000. Gas was off at 15:03pm on 5/12/18 with a release of gas of 13 mcf. On august 3rd, 2018, the repair cost report was received and was $96,988. The nrc was contacted at on 8/3/18 at 10:33am to report the incident based on cost to the operator.
Detailed record list
Occurred At
2018-05-12 05:00:00
Year
2018
Report Received Date
2018-09-02 00:00:00
Iyear
2018.0
Report Number
20180081.0
Supplemental Number
30886.0
Report Type
Original Final
Operator Id
Name
Dte Gas Company
Operator Street Address
1 Energy Plaza
Operator City Name
Detroit
Operator State Abbreviation
MI
Operator Postal Code
48226
Local Datetime
2018-05-12 05:00:00
Location Street Address
4695 W Jefferson
Location City Name
Trenton
Location County Name
Wayne County
Location State Abbreviation
MI
Location Postal Code
48183
Location Latitude
Location Longitude
Nrc Rpt Datetime
2018-08-03 10:33:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
13.0
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
1
Injure
1
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2018-05-12 05:00:00
On Site Datetime
2018-05-12 05:28:00
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Other
System Part Details
High-Head Extension Equipment
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Leak
Leak Type
Connection Failure
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
77258.0
Est Cost Emergency
19693.0
Est Cost Other
0.0
Est Cost Unintentional Release
37.0
Prpty
96988.0
Commercial Affected
0.0
Industrial Affected
3.0
Residences Affected
0.0
Accident Psig
145.0
Normal Psig
145.0
Mop Psig
150.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype
Third Party
Preparer Name
F***** F* S****
Preparer Title
Manager
Preparer Email
F***********@d********.com
Preparer Telephone
313-389-7762
Preparer Fax
313-389-7755
Authorizer Name
F***** F* S****
Authorizer Title
Manager
Authorizer Telephone
313-460-1681
Authorizer Email
F***********@d********.com
Narrative
Dte gas received a call from trenton fire department of a vehicle hit of a gas line at 6:12am. Dte gas was onsite at 6:51pm. Once dte gas first responders were on seen it was confirmed that a driver had hit the high-head extension at the location. There was a leak as a result of the incident. The driver was taken to the hospital and drug & alcohol testing was performed. Result. This leak impacted 3 businesses. The mpsc was contacted at 11:33am once it was realized that the repair was going to be approximately $10,000. Gas was off at 15:03pm on 5/12/18 with a release of gas of 13 mcf. On august 3rd, 2018, the repair cost report was received and was $96,988. The nrc was contacted at on 8/3/18 at 10:33am to report the incident based on cost to the operator.
Occurred At 2018-05-12 05:00:00
Year 2018
Report Received Date 2018-09-02 00:00:00
Iyear 2018.0
Report Number 20180081.0
Supplemental Number 30886.0
Report Type Original Final
Operator Id 12408 PHMSA Enforcement
Name Dte Gas Company
Operator Street Address 1 Energy Plaza
Operator City Name Detroit
Operator State Abbreviation MI
Operator Postal Code 48226
Local Datetime 2018-05-12 05:00:00
Location Street Address 4695 W Jefferson
Location City Name Trenton
Location County Name Wayne County
Location State Abbreviation MI
Location Postal Code 48183
Location Latitude 42.122087 Google Maps OpenStreetMap
Location Longitude -83.179768 Google Maps OpenStreetMap
Nrc Rpt Datetime 2018-08-03 10:33:00
Nrc Rpt Num 1220406 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 13.0
Fatality Ind No
Fatal 0
Injury Ind Yes
Num Emp Injuries 0
Num Contr Injuries 0
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 1
Injure 1
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2018-05-12 05:00:00
On Site Datetime 2018-05-12 05:28:00
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Other
System Part Details High-Head Extension Equipment
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Release Type Leak
Leak Type Connection Failure
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 77258.0
Est Cost Emergency 19693.0
Est Cost Other 0.0
Est Cost Unintentional Release 37.0
Prpty 96988.0
Commercial Affected 0.0
Industrial Affected 3.0
Residences Affected 0.0
Accident Psig 145.0
Normal Psig 145.0
Mop Psig 150.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype Third Party
Preparer Name F***** F* S****
Preparer Title Manager
Preparer Email F***********@d********.com
Preparer Telephone 313-389-7762
Preparer Fax 313-389-7755
Authorizer Name F***** F* S****
Authorizer Title Manager
Authorizer Telephone 313-460-1681
Authorizer Email F***********@d********.com
Narrative Dte gas received a call from trenton fire department of a vehicle hit of a gas line at 6:12am. Dte gas was onsite at 6:51pm. Once dte gas first responders were on seen it was confirmed that a driver had hit the high-head extension at the location. There was a leak as a result of the incident. The driver was taken to the hospital and drug & alcohol testing was performed. Result. This leak impacted 3 businesses. The mpsc was contacted at 11:33am once it was realized that the repair was going to be approximately $10,000. Gas was off at 15:03pm on 5/12/18 with a release of gas of 13 mcf. On august 3rd, 2018, the repair cost report was received and was $96,988. The nrc was contacted at on 8/3/18 at 10:33am to report the incident based on cost to the operator.

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