GD incident on 2018-07-28 — CA

Operator
Pacific Gas & Electric Co
Cause
Other Outside Force Damage
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$229,000
Incident datetime
2018-07-28 10:10
Report number
Location
CA, SHASTA
Narrative
On july 26, 2018 at 0900 hours (operational at 1400 hours), the north valley operations emergency center (oec) was activated to support the carr fire in redding. During the night of july 25-26, the fire increased in size. Gas emergency center (gec) was activated to support the event. As of 7/27/18 at 1300 hours, 468 gas customers were proactively shut in. During the night of july 27-28, crews continued to assess additional areas. As of 7/28/18 at 0600 hours, the crew shut-in an additional 71 gas customer services and cut-off 17 gas services. As of 7/29/18 at 1500 hours, all known pressurized risers without a home have been cut-off. Pg&e crews cut off risers without homes in the depressurized zones. Restoration and subsequent relights were completed for homes that were able to be restored by 8/5/18. 32 remaining customers were left a service report advising them to call the contact center to be restored at their convenience. There were approximately 614 customers who had their gas service impacted. As the evacuation covered a vast area of shasta-trinity county and the evacuation total is undetermined at the time of this report. There were no reported injuries or fatalities involving natural gas. Pg&e reported this incident to the DOT and cpuc due to the unintentional release of gas and estimated repair costs greater than $50k. This was determined on 7/28/18 at 1010 hours. An update was provided to the DOT (1219914) on 7/30/18 at 0922 hours.
Detailed record list
Occurred At
2018-07-28 10:10:00
Year
2018
Report Received Date
2018-08-23 00:00:00
Iyear
2018.0
Report Number
20180078.0
Supplemental Number
30847.0
Report Type
Original Final
Operator Id
Name
Pacific Gas & Electric Co
Operator Street Address
6121 Bollinger Canyon Rd.
Operator City Name
San Ramon
Operator State Abbreviation
CA
Operator Postal Code
94583
Local Datetime
2018-07-26 09:00:00
Location Street Address
4245 Wayshara Ave.
Location City Name
Redding
Location County Name
Shasta
Location State Abbreviation
CA
Location Postal Code
96001
Location Latitude
Location Longitude
Nrc Rpt Datetime
2018-07-28 10:50:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
740.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
614.0
Incident Identified Datetime
2018-07-28 10:10:00
On Site Datetime
2018-07-27 01:45:00
Federal
No
Location Type
Private Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Service Riser
Installation Year
1971.0
Material Involved
Plastic
Plastic Type
Unknown
Wt Plastic Unknown Ind
Unknown
Release Type
Leak
Leak Type
Other
Leak Type Other
Found 4 Meters Melted
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
229000.0
Est Cost Emergency
810000.0
Est Cost Other
0.0
Est Cost Other Details
Costs Are For The Emergency Response For The Entire Shasta County.
Est Cost Unintentional Release
2220.0
Prpty
1041220.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
614.0
Accident Psig
55.0
Normal Psig
55.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The incident was due to a wildfire beyond operators control.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Outside Force Type
Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Preparer Name
E*** B******
Preparer Title
Regulatory Compliance
Preparer Email
E***@p**.com
Preparer Telephone
925-357-7889
Authorizer Name
S**** R*******
Authorizer Title
Regulatory Compliance Manager
Authorizer Telephone
925-786-0267
Authorizer Email
G***@p**.com
Narrative
On july 26, 2018 at 0900 hours (operational at 1400 hours), the north valley operations emergency center (oec) was activated to support the carr fire in redding. During the night of july 25-26, the fire increased in size. Gas emergency center (gec) was activated to support the event. As of 7/27/18 at 1300 hours, 468 gas customers were proactively shut in. During the night of july 27-28, crews continued to assess additional areas. As of 7/28/18 at 0600 hours, the crew shut-in an additional 71 gas customer services and cut-off 17 gas services. As of 7/29/18 at 1500 hours, all known pressurized risers without a home have been cut-off. Pg&e crews cut off risers without homes in the depressurized zones. Restoration and subsequent relights were completed for homes that were able to be restored by 8/5/18. 32 remaining customers were left a service report advising them to call the contact center to be restored at their convenience. There were approximately 614 customers who had their gas service impacted. As the evacuation covered a vast area of shasta-trinity county and the evacuation total is undetermined at the time of this report. There were no reported injuries or fatalities involving natural gas. Pg&e reported this incident to the DOT and cpuc due to the unintentional release of gas and estimated repair costs greater than $50k. This was determined on 7/28/18 at 1010 hours. An update was provided to the DOT (1219914) on 7/30/18 at 0922 hours.
Occurred At 2018-07-28 10:10:00
Year 2018
Report Received Date 2018-08-23 00:00:00
Iyear 2018.0
Report Number 20180078.0
Supplemental Number 30847.0
Report Type Original Final
Operator Id 15007 PHMSA Enforcement
Name Pacific Gas & Electric Co
Operator Street Address 6121 Bollinger Canyon Rd.
Operator City Name San Ramon
Operator State Abbreviation CA
Operator Postal Code 94583
Local Datetime 2018-07-26 09:00:00
Location Street Address 4245 Wayshara Ave.
Location City Name Redding
Location County Name Shasta
Location State Abbreviation CA
Location Postal Code 96001
Location Latitude 40.57992 Google Maps OpenStreetMap
Location Longitude -122.427875 Google Maps OpenStreetMap
Nrc Rpt Datetime 2018-07-28 10:50:00
Nrc Rpt Num 1219782 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 740.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 614.0
Incident Identified Datetime 2018-07-28 10:10:00
On Site Datetime 2018-07-27 01:45:00
Federal No
Location Type Private Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Service Riser
Installation Year 1971.0
Material Involved Plastic
Plastic Type Unknown
Wt Plastic Unknown Ind Unknown
Release Type Leak
Leak Type Other
Leak Type Other Found 4 Meters Melted
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 229000.0
Est Cost Emergency 810000.0
Est Cost Other 0.0
Est Cost Other Details Costs Are For The Emergency Response For The Entire Shasta County.
Est Cost Unintentional Release 2220.0
Prpty 1041220.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 614.0
Accident Psig 55.0
Normal Psig 55.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The incident was due to a wildfire beyond operators control.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Outside Force Type Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Preparer Name E*** B******
Preparer Title Regulatory Compliance
Preparer Email E***@p**.com
Preparer Telephone 925-357-7889
Authorizer Name S**** R*******
Authorizer Title Regulatory Compliance Manager
Authorizer Telephone 925-786-0267
Authorizer Email G***@p**.com
Narrative On july 26, 2018 at 0900 hours (operational at 1400 hours), the north valley operations emergency center (oec) was activated to support the carr fire in redding. During the night of july 25-26, the fire increased in size. Gas emergency center (gec) was activated to support the event. As of 7/27/18 at 1300 hours, 468 gas customers were proactively shut in. During the night of july 27-28, crews continued to assess additional areas. As of 7/28/18 at 0600 hours, the crew shut-in an additional 71 gas customer services and cut-off 17 gas services. As of 7/29/18 at 1500 hours, all known pressurized risers without a home have been cut-off. Pg&e crews cut off risers without homes in the depressurized zones. Restoration and subsequent relights were completed for homes that were able to be restored by 8/5/18. 32 remaining customers were left a service report advising them to call the contact center to be restored at their convenience. There were approximately 614 customers who had their gas service impacted. As the evacuation covered a vast area of shasta-trinity county and the evacuation total is undetermined at the time of this report. There were no reported injuries or fatalities involving natural gas. Pg&e reported this incident to the DOT and cpuc due to the unintentional release of gas and estimated repair costs greater than $50k. This was determined on 7/28/18 at 1010 hours. An update was provided to the DOT (1219914) on 7/30/18 at 0922 hours.

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