GD incident on 2018-06-16 — MD

Operator
Baltimore Gas And Electric Company
Cause
Pipe, Weld, Or Joint Failure
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 1 injury
Property damage (nominal)
$5,000
Incident datetime
2018-06-16 13:55
Report number
Location
MD, BALTIMORE CITY IS NOT WITHIN BALTIMORE COUNTY
Narrative
On 6/9/2018 a bge contractor paving crew was installing thermoplastic marker traffic lines on a baltimore city street surface using a heat torch (in order for the thermoplastic lines to adhere to the surface). When performing this function near a baltimore city manhole, an ignition occurred which caused the manhole lid to raise and strike the contractor employee, resulting in an injury requiring an overnight hospital stay. The exact composition of the ignition source (in the manhole) was later confirmed as natural gas, but the source of the gas was undetermined at the time of the initial emergency response. Following continuing gas leak area surveys, a gas main leak was identified and a cast iron joint was subsequently repaired. The apparent gas levels in the subject manhole were reduced. Thus the source at the time of ignition was undetermined but by june 16, the correlation of the repair and the gas levels measured in the manhole was the basis for the nrc notice determination.
Detailed record list
Occurred At
2018-06-16 13:55:00
Year
2018
Report Received Date
2018-07-10 00:00:00
Iyear
2018.0
Report Number
20180068.0
Supplemental Number
31254.0
Report Type
Supplemental Final
Operator Id
Name
Baltimore Gas And Electric Company
Operator Street Address
110 W Fayette St
Operator City Name
Baltimore
Operator State Abbreviation
MD
Operator Postal Code
21201
Local Datetime
2018-06-09 13:55:00
Location Street Address
1500 Riverside Ave
Location City Name
Baltimore
Location County Name
Baltimore City Is Not Within Baltimore County
Location State Abbreviation
MD
Location Postal Code
21230
Location Latitude
Location Longitude
Nrc Rpt Datetime
2018-06-16 15:21:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
0.01
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
1
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
0
Injure
1
Ignite Ind
Yes
Explode Ind
Yes
Num Pub Evacuated
0.0
Incident Identified Datetime
2018-06-16 13:55:00
On Site Datetime
2018-06-16 13:55:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Other
Incident Area Details
Public Works Manhole - Non-Utility Strut
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1903.0
Pipe Diameter
12.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Cast/wrought Iron
Release Type
Leak
Leak Type
Seal Or Packing
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
5000.0
Est Cost Emergency
500.0
Est Cost Other
0.0
Est Cost Other Details
Emergency Response Personnel.
Est Cost Unintentional Release
10.0
Prpty
5510.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
5.95
Normal Psig
5.95
Mop Psig
10.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Pipe, Weld, Or Joint Failure
Cause Details
Other Pipe, Weld, Or Joint Failure
Pwjf Failure Type
Other Pipe, Weld, Or Joint Failure
Pwjf Failure Details
Cast Iron Joint Failure
Additional Other Ind
Yes
Additional Factor Details
Cast Iron Joint Leak
Result Material Ind
Yes
Result Material Subtype
Other
Result Material Details
Cast Iron Joint
Hydrotest Conducted Ind
No
Preparer Name
S**** T****
Preparer Title
Manager - Gas Engineering And Asset Performance
Preparer Email
S**********@b**.com
Preparer Telephone
4104709560
Preparer Fax
4104709549
Authorizer Name
S**** T****
Authorizer Title
Manager - Gas Engineering And Asset Performance
Authorizer Telephone
4104709560
Authorizer Email
S**********@b**.com
Narrative
On 6/9/2018 a bge contractor paving crew was installing thermoplastic marker traffic lines on a baltimore city street surface using a heat torch (in order for the thermoplastic lines to adhere to the surface). When performing this function near a baltimore city manhole, an ignition occurred which caused the manhole lid to raise and strike the contractor employee, resulting in an injury requiring an overnight hospital stay. The exact composition of the ignition source (in the manhole) was later confirmed as natural gas, but the source of the gas was undetermined at the time of the initial emergency response. Following continuing gas leak area surveys, a gas main leak was identified and a cast iron joint was subsequently repaired. The apparent gas levels in the subject manhole were reduced. Thus the source at the time of ignition was undetermined but by june 16, the correlation of the repair and the gas levels measured in the manhole was the basis for the nrc notice determination.
Occurred At 2018-06-16 13:55:00
Year 2018
Report Received Date 2018-07-10 00:00:00
Iyear 2018.0
Report Number 20180068.0
Supplemental Number 31254.0
Report Type Supplemental Final
Operator Id 1088 PHMSA Enforcement
Name Baltimore Gas And Electric Company
Operator Street Address 110 W Fayette St
Operator City Name Baltimore
Operator State Abbreviation MD
Operator Postal Code 21201
Local Datetime 2018-06-09 13:55:00
Location Street Address 1500 Riverside Ave
Location City Name Baltimore
Location County Name Baltimore City Is Not Within Baltimore County
Location State Abbreviation MD
Location Postal Code 21230
Location Latitude 39.272676 Google Maps OpenStreetMap
Location Longitude -76.608326 Google Maps OpenStreetMap
Nrc Rpt Datetime 2018-06-16 15:21:00
Nrc Rpt Num 1215480 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 0.01
Fatality Ind No
Fatal 0
Injury Ind Yes
Num Emp Injuries 0
Num Contr Injuries 1
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 0
Injure 1
Ignite Ind Yes
Explode Ind Yes
Num Pub Evacuated 0.0
Incident Identified Datetime 2018-06-16 13:55:00
On Site Datetime 2018-06-16 13:55:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Other
Incident Area Details Public Works Manhole - Non-Utility Strut
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1903.0
Pipe Diameter 12.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Cast/wrought Iron
Release Type Leak
Leak Type Seal Or Packing
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 5000.0
Est Cost Emergency 500.0
Est Cost Other 0.0
Est Cost Other Details Emergency Response Personnel.
Est Cost Unintentional Release 10.0
Prpty 5510.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 5.95
Normal Psig 5.95
Mop Psig 10.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Pipe, Weld, Or Joint Failure
Cause Details Other Pipe, Weld, Or Joint Failure
Pwjf Failure Type Other Pipe, Weld, Or Joint Failure
Pwjf Failure Details Cast Iron Joint Failure
Additional Other Ind Yes
Additional Factor Details Cast Iron Joint Leak
Result Material Ind Yes
Result Material Subtype Other
Result Material Details Cast Iron Joint
Hydrotest Conducted Ind No
Preparer Name S**** T****
Preparer Title Manager - Gas Engineering And Asset Performance
Preparer Email S**********@b**.com
Preparer Telephone 4104709560
Preparer Fax 4104709549
Authorizer Name S**** T****
Authorizer Title Manager - Gas Engineering And Asset Performance
Authorizer Telephone 4104709560
Authorizer Email S**********@b**.com
Narrative On 6/9/2018 a bge contractor paving crew was installing thermoplastic marker traffic lines on a baltimore city street surface using a heat torch (in order for the thermoplastic lines to adhere to the surface). When performing this function near a baltimore city manhole, an ignition occurred which caused the manhole lid to raise and strike the contractor employee, resulting in an injury requiring an overnight hospital stay. The exact composition of the ignition source (in the manhole) was later confirmed as natural gas, but the source of the gas was undetermined at the time of the initial emergency response. Following continuing gas leak area surveys, a gas main leak was identified and a cast iron joint was subsequently repaired. The apparent gas levels in the subject manhole were reduced. Thus the source at the time of ignition was undetermined but by june 16, the correlation of the repair and the gas levels measured in the manhole was the basis for the nrc notice determination.

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