GTG incident on 2018-06-07 — TX

Operator
Columbia Gas Transmission, Llc
Cause
Natural Force Damage
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$13,422,000
Incident datetime
2018-06-07 04:37
Report number
Location
TX
Narrative
On june 7th, 2018, an unintended release event of natural gas (material) into the atmosphere was reported to the national response center (nrc). This event took place on the leach express (lex) pipeline that is operated and maintained by columbia gas transmission, llc (columbia). Lex pipeline is a 36 inch diameter natural gas pipeline and is classified as transmission, with a maximum allowable operating pressure of 1,440 psig. Lex is a unidirectional flow pipeline that starts near majorsville , west virginia and terminates at the tie-in with r-system regulator station (ohio). At 04:16 eastern standard time (est), the columbia gas control personnel noted a low pressure scada alarm and columbia operations personnel were dispatched to investigate the event. At 04:37 est, the columbia monitoring center received a call from the marshall county 911 regarding a pipeline failure in marshall county, wv near wv state route 21/1 (nixon ridge road). The failure was within valve section (vs) mainline valve lex-500 to mainline valve lex-600 (isolated segment). The material ignited. Limited damage occurred to vegetation and trees within the area of the pipeline failure site. No structures were identified near the failure site. No fatalities or injuries were reported as a result of this pipeline failure. The failed pipeline section was isolated at approximately 05:20 est. The failed sections of the pipeline were sent to a metallurgical laboratory to determine the probable cause behind the failure of the pipeline. The 48-hr updateto the nrc was completed on june 8th, 2018 with report no. 1214673. The laboratory report identified the incident was caused by a single, overload event. Overloading of the pipeline resulted from what was likely a series of lateral displacements with accompanying bending.
Detailed record list
Report Received Date
2018-06-27 00:00:00
Iyear
2018
Report Number
20180067
Supplemental Number
31416
Report Type
Supplemental Final
Operator Id
Name
Columbia Gas Transmission, Llc
Operator Street Address
700 Louisiana St. Suite 700
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-06-07 04:16:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2018-06-07 06:12:00
Commodity Released Type
Natural Gas
Unintentional Release
165000
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-06-07 05:20:00
Restart Datetime
2018-07-15 14:18:00
Ignite Ind
Yes
Explode Ind
Yes
Num Pub Evacuated
0
Incident Identified Datetime
2018-06-07 04:37:00
On Site Datetime
2018-06-07 06:00:00
On Off Shore
Onshore
Onshore State Abbreviation
Wv
Onshore Postal Code
26041
Onshore City Name
Moundsville
Onshore County Name
Marshall
Designated Location
Milepost
Designated Name
Mp 21.3
Pipe Fac Name
Leach Xpress
Segment Name
Mainline Valve Lex-500 To Mainline Valve Lex-600
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
36
Pipe Wall Thickness
0.515
Pipe Smys
70000
Pipe Specification
Api 5l X70m
Pipe Seam Type
Dsaw
Pipe Manufacturer
Durabond
Pipe Coating Type
Epoxy
Installation Year
2017
Manufactured Year
2015
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Circumferential
Rupture Length
113
Rupture Width
36
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
1056
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
600000
Est Cost Unintentional Release
437250
Est Cost Intentional Release
0
Est Cost Prop Damage
13422000
Est Cost Emergency
0
Est Cost Other
5925384
Est Cost Other Details
Back To Service Sites
Prpty
20384634
Accident Psig
1280
Mop Psig
1440
Mop Cfr Section
192.619(A)(1)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Automatic
Length Segment Isolated
71280
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The control room personnel were not performing any changes to the pipeline system that may have identified as a contributing factor that may have potentially led to the pipeline failure
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Natural Force Damage
Cause Details
Earth Movement, Not Due To Heavy Rains/floods
Natural Force Type
Earth Movement, Not Due To Heavy Rains/floods
Earth Subtype
Subsidence
Nf Extreme Weather Ind
No
Preparer Name
K***** R****** A*******
Preparer Title
Compliance Specialist
Preparer Email
K*************@t**********.com
Preparer Telephone
304-357-2351
Authorizer Name
G***** H*****
Authorizer Title
Manager Us Regulatory Compliance East
Authorizer Telephone
304-357-3728
Authorizer Email
G************@t**********.com
Narrative
On june 7th, 2018, an unintended release event of natural gas (material) into the atmosphere was reported to the national response center (nrc). This event took place on the leach express (lex) pipeline that is operated and maintained by columbia gas transmission, llc (columbia). Lex pipeline is a 36 inch diameter natural gas pipeline and is classified as transmission, with a maximum allowable operating pressure of 1,440 psig. Lex is a unidirectional flow pipeline that starts near majorsville , west virginia and terminates at the tie-in with r-system regulator station (ohio). At 04:16 eastern standard time (est), the columbia gas control personnel noted a low pressure scada alarm and columbia operations personnel were dispatched to investigate the event. At 04:37 est, the columbia monitoring center received a call from the marshall county 911 regarding a pipeline failure in marshall county, wv near wv state route 21/1 (nixon ridge road). The failure was within valve section (vs) mainline valve lex-500 to mainline valve lex-600 (isolated segment). The material ignited. Limited damage occurred to vegetation and trees within the area of the pipeline failure site. No structures were identified near the failure site. No fatalities or injuries were reported as a result of this pipeline failure. The failed pipeline section was isolated at approximately 05:20 est. The failed sections of the pipeline were sent to a metallurgical laboratory to determine the probable cause behind the failure of the pipeline. The 48-hr updateto the nrc was completed on june 8th, 2018 with report no. 1214673. The laboratory report identified the incident was caused by a single, overload event. Overloading of the pipeline resulted from what was likely a series of lateral displacements with accompanying bending.
Report Received Date 2018-06-27 00:00:00
Iyear 2018
Report Number 20180067
Supplemental Number 31416
Report Type Supplemental Final
Operator Id 2616 PHMSA Enforcement
Name Columbia Gas Transmission, Llc
Operator Street Address 700 Louisiana St. Suite 700
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-06-07 04:16:00
Location Latitude 39.806667 Google Maps OpenStreetMap
Location Longitude -80.759444 Google Maps OpenStreetMap
Nrc Rpt Num 1214458 NRC Report How to search
Nrc Rpt Datetime 2018-06-07 06:12:00
Commodity Released Type Natural Gas
Unintentional Release 165000
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-06-07 05:20:00
Restart Datetime 2018-07-15 14:18:00
Ignite Ind Yes
Explode Ind Yes
Num Pub Evacuated 0
Incident Identified Datetime 2018-06-07 04:37:00
On Site Datetime 2018-06-07 06:00:00
On Off Shore Onshore
Onshore State Abbreviation Wv
Onshore Postal Code 26041
Onshore City Name Moundsville
Onshore County Name Marshall
Designated Location Milepost
Designated Name Mp 21.3
Pipe Fac Name Leach Xpress
Segment Name Mainline Valve Lex-500 To Mainline Valve Lex-600
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 36
Pipe Wall Thickness 0.515
Pipe Smys 70000
Pipe Specification Api 5l X70m
Pipe Seam Type Dsaw
Pipe Manufacturer Durabond
Pipe Coating Type Epoxy
Installation Year 2017
Manufactured Year 2015
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Circumferential
Rupture Length 113
Rupture Width 36
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 1056
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 600000
Est Cost Unintentional Release 437250
Est Cost Intentional Release 0
Est Cost Prop Damage 13422000
Est Cost Emergency 0
Est Cost Other 5925384
Est Cost Other Details Back To Service Sites
Prpty 20384634
Accident Psig 1280
Mop Psig 1440
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Automatic
Length Segment Isolated 71280
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The control room personnel were not performing any changes to the pipeline system that may have identified as a contributing factor that may have potentially led to the pipeline failure
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Natural Force Damage
Cause Details Earth Movement, Not Due To Heavy Rains/floods
Natural Force Type Earth Movement, Not Due To Heavy Rains/floods
Earth Subtype Subsidence
Nf Extreme Weather Ind No
Preparer Name K***** R****** A*******
Preparer Title Compliance Specialist
Preparer Email K*************@t**********.com
Preparer Telephone 304-357-2351
Authorizer Name G***** H*****
Authorizer Title Manager Us Regulatory Compliance East
Authorizer Telephone 304-357-3728
Authorizer Email G************@t**********.com
Narrative On june 7th, 2018, an unintended release event of natural gas (material) into the atmosphere was reported to the national response center (nrc). This event took place on the leach express (lex) pipeline that is operated and maintained by columbia gas transmission, llc (columbia). Lex pipeline is a 36 inch diameter natural gas pipeline and is classified as transmission, with a maximum allowable operating pressure of 1,440 psig. Lex is a unidirectional flow pipeline that starts near majorsville , west virginia and terminates at the tie-in with r-system regulator station (ohio). At 04:16 eastern standard time (est), the columbia gas control personnel noted a low pressure scada alarm and columbia operations personnel were dispatched to investigate the event. At 04:37 est, the columbia monitoring center received a call from the marshall county 911 regarding a pipeline failure in marshall county, wv near wv state route 21/1 (nixon ridge road). The failure was within valve section (vs) mainline valve lex-500 to mainline valve lex-600 (isolated segment). The material ignited. Limited damage occurred to vegetation and trees within the area of the pipeline failure site. No structures were identified near the failure site. No fatalities or injuries were reported as a result of this pipeline failure. The failed pipeline section was isolated at approximately 05:20 est. The failed sections of the pipeline were sent to a metallurgical laboratory to determine the probable cause behind the failure of the pipeline. The 48-hr updateto the nrc was completed on june 8th, 2018 with report no. 1214673. The laboratory report identified the incident was caused by a single, overload event. Overloading of the pipeline resulted from what was likely a series of lateral displacements with accompanying bending.

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