GD incident on 2018-04-26 — OK

Operator
Cleveland Gas Dept
Cause
Incorrect Operation
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 2 injuries
Property damage (nominal)
$1,000
Incident datetime
2018-04-26 08:00
Report number
Location
OK, PAWNEE
Narrative
The city of cleveland received notification from a public source of the leak on 25 april 18. The leak was located by operator on 25 april 18 at approx. 1600hrs. Leak was deemed as a class 2 leak by the operator on 25 april 18. No cgi readings were taken or migration study done to properly classify the leak. Personnel responded on 26 april 18 at approx. 1300hrs to begin repair operations. No cgi readings were being taken during the repair operations of the pipeline. The leak was excavated by a qualified personnel member. After the steel pipeline and leak was exposed four qualified personnel members began the repair process. Personnel members 1 & 2 were cleaning the coating on the pipeline to prepare for a repair clamp. Personnel member 3 was supervising the repair process. Personnel member 4 was using a steel file to prepare the steel pipeline for cathodic anode installation. The initial attempt to tighten clamp was unsuccessful to seal the leak. Torque wrench was not used in the installation of clamp. Personnel member 3 then changed positions with personnel member 1. While moving clamp in an attempt to seal the leak, ignition of gas occurred. Unknown source caused the ignition of the gas. Personnel member 2 had cell phone on his person near the source of leak. Personnel member 4 had two cell phones near the source of leak. Personnel member 2,3,4 were transported to hospital for burn injuries. Personnel members 2 was treated and released shortly before midnight on 26 april 18. Personnel members 3 and 4 spent several days in burn unit at tulsa hospital. Personnel member 5 who arrived after ignition of gas was sent and checked at local hospital for general sickness. It is apparent the proper procedure for leak classifications was not followed and that repair procedures are inadequate. The city of mannford was called in to assist with the leak repair. The city of mannford has prepared a written statement of their actions taken in the repair of the pipeline. The statement is available upon request.
Detailed record list
Occurred At
2018-04-26 08:00:00
Year
2018
Report Received Date
2018-05-30 00:00:00
Iyear
2018.0
Report Number
20180060.0
Supplemental Number
30463.0
Report Type
Supplemental Final
Operator Id
Name
Cleveland Gas Dept
Operator Street Address
201 N Broadway/po Drawer 190
Operator City Name
Cleveland
Operator State Abbreviation
OK
Operator Postal Code
74020
Local Datetime
2018-04-26 15:40:00
Location Street Address
501 N. Broadway
Location City Name
Cleveland
Location County Name
Pawnee
Location State Abbreviation
OK
Location Postal Code
74020
Location Latitude
Location Longitude
Nrc Rpt Datetime
2018-04-26 21:08:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
67.5
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
2
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
0
Injure
2
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
50.0
Incident Identified Datetime
2018-04-26 08:00:00
On Site Datetime
2018-04-26 08:30:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
84.0
Crossing
No
Pipe Facility Type
Municipally Owned
System Part Involved
Main
Pipe Diameter
2.0
Pipe Specification
Coded
Pipe Manufacturer
Unknown
Material Involved
Steel
Release Type
Leak
Leak Type
Pinhole
Class Location Type
Class 2 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
1000.0
Est Cost Emergency
500.0
Est Cost Other
0.0
Est Cost Other Details
Total Cost Of Repairs And Emergency Personnel.
Est Cost Unintentional Release
270.0
Prpty
1770.0
Commercial Affected
1.0
Industrial Affected
0.0
Residences Affected
1.0
Accident Psig
20.0
Normal Psig
20.0
Mop Psig
25.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Failure To Follow Procedure For Proper Classification Of Leak And Inadequate Repair Procedures.
Related Inadequate Proc Ind
Yes
Related Failure Follow Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
C****** E* S****
Preparer Title
Cheif Of Police
Preparer Email
C*****@c****************.com
Preparer Telephone
918-358-3506
Preparer Fax
918-358-3600
Authorizer Name
E**** S****
Authorizer Title
City Manager
Authorizer Telephone
918-358-3506
Authorizer Email
E*********@h******.com
Narrative
The city of cleveland received notification from a public source of the leak on 25 april 18. The leak was located by operator on 25 april 18 at approx. 1600hrs. Leak was deemed as a class 2 leak by the operator on 25 april 18. No cgi readings were taken or migration study done to properly classify the leak. Personnel responded on 26 april 18 at approx. 1300hrs to begin repair operations. No cgi readings were being taken during the repair operations of the pipeline. The leak was excavated by a qualified personnel member. After the steel pipeline and leak was exposed four qualified personnel members began the repair process. Personnel members 1 & 2 were cleaning the coating on the pipeline to prepare for a repair clamp. Personnel member 3 was supervising the repair process. Personnel member 4 was using a steel file to prepare the steel pipeline for cathodic anode installation. The initial attempt to tighten clamp was unsuccessful to seal the leak. Torque wrench was not used in the installation of clamp. Personnel member 3 then changed positions with personnel member 1. While moving clamp in an attempt to seal the leak, ignition of gas occurred. Unknown source caused the ignition of the gas. Personnel member 2 had cell phone on his person near the source of leak. Personnel member 4 had two cell phones near the source of leak. Personnel member 2,3,4 were transported to hospital for burn injuries. Personnel members 2 was treated and released shortly before midnight on 26 april 18. Personnel members 3 and 4 spent several days in burn unit at tulsa hospital. Personnel member 5 who arrived after ignition of gas was sent and checked at local hospital for general sickness. It is apparent the proper procedure for leak classifications was not followed and that repair procedures are inadequate. The city of mannford was called in to assist with the leak repair. The city of mannford has prepared a written statement of their actions taken in the repair of the pipeline. The statement is available upon request.
Occurred At 2018-04-26 08:00:00
Year 2018
Report Received Date 2018-05-30 00:00:00
Iyear 2018.0
Report Number 20180060.0
Supplemental Number 30463.0
Report Type Supplemental Final
Operator Id 2492 PHMSA Enforcement
Name Cleveland Gas Dept
Operator Street Address 201 N Broadway/po Drawer 190
Operator City Name Cleveland
Operator State Abbreviation OK
Operator Postal Code 74020
Local Datetime 2018-04-26 15:40:00
Location Street Address 501 N. Broadway
Location City Name Cleveland
Location County Name Pawnee
Location State Abbreviation OK
Location Postal Code 74020
Location Latitude 36.31315 Google Maps OpenStreetMap
Location Longitude -96.463191 Google Maps OpenStreetMap
Nrc Rpt Datetime 2018-04-26 21:08:00
Nrc Rpt Num 1210439 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 67.5
Fatality Ind No
Fatal 0
Injury Ind Yes
Num Emp Injuries 2
Num Contr Injuries 0
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 0
Injure 2
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 50.0
Incident Identified Datetime 2018-04-26 08:00:00
On Site Datetime 2018-04-26 08:30:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 84.0
Crossing No
Pipe Facility Type Municipally Owned
System Part Involved Main
Pipe Diameter 2.0
Pipe Specification Coded
Pipe Manufacturer Unknown
Material Involved Steel
Release Type Leak
Leak Type Pinhole
Class Location Type Class 2 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 1000.0
Est Cost Emergency 500.0
Est Cost Other 0.0
Est Cost Other Details Total Cost Of Repairs And Emergency Personnel.
Est Cost Unintentional Release 270.0
Prpty 1770.0
Commercial Affected 1.0
Industrial Affected 0.0
Residences Affected 1.0
Accident Psig 20.0
Normal Psig 20.0
Mop Psig 25.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Public
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Failure To Follow Procedure For Proper Classification Of Leak And Inadequate Repair Procedures.
Related Inadequate Proc Ind Yes
Related Failure Follow Ind Yes
Category Type Other Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name C****** E* S****
Preparer Title Cheif Of Police
Preparer Email C*****@c****************.com
Preparer Telephone 918-358-3506
Preparer Fax 918-358-3600
Authorizer Name E**** S****
Authorizer Title City Manager
Authorizer Telephone 918-358-3506
Authorizer Email E*********@h******.com
Narrative The city of cleveland received notification from a public source of the leak on 25 april 18. The leak was located by operator on 25 april 18 at approx. 1600hrs. Leak was deemed as a class 2 leak by the operator on 25 april 18. No cgi readings were taken or migration study done to properly classify the leak. Personnel responded on 26 april 18 at approx. 1300hrs to begin repair operations. No cgi readings were being taken during the repair operations of the pipeline. The leak was excavated by a qualified personnel member. After the steel pipeline and leak was exposed four qualified personnel members began the repair process. Personnel members 1 & 2 were cleaning the coating on the pipeline to prepare for a repair clamp. Personnel member 3 was supervising the repair process. Personnel member 4 was using a steel file to prepare the steel pipeline for cathodic anode installation. The initial attempt to tighten clamp was unsuccessful to seal the leak. Torque wrench was not used in the installation of clamp. Personnel member 3 then changed positions with personnel member 1. While moving clamp in an attempt to seal the leak, ignition of gas occurred. Unknown source caused the ignition of the gas. Personnel member 2 had cell phone on his person near the source of leak. Personnel member 4 had two cell phones near the source of leak. Personnel member 2,3,4 were transported to hospital for burn injuries. Personnel members 2 was treated and released shortly before midnight on 26 april 18. Personnel members 3 and 4 spent several days in burn unit at tulsa hospital. Personnel member 5 who arrived after ignition of gas was sent and checked at local hospital for general sickness. It is apparent the proper procedure for leak classifications was not followed and that repair procedures are inadequate. The city of mannford was called in to assist with the leak repair. The city of mannford has prepared a written statement of their actions taken in the repair of the pipeline. The statement is available upon request.

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