GTG incident on 2018-03-01 — TX

Operator
Tennessee Gas Pipeline Company
Cause
Equipment Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$608
Incident datetime
2018-03-01 20:03
Report number
Location
TX
Narrative
On 3/1/18 at approximately 7:31 pm a compressor on unit 2 in the compressor building had an issue whereby the compressor rod packing began leaking causing the gas detector to sense 40% lel which initiated a station hazard atmosphere alarm and caused emergency shut down (esd). At 8:00pm an erl call was sent out. At 8:03 local operating personnel identified that the station esd valve was still venting gas beyond the typical station blow down time. Upon further investigation personnel found that station discharge valve (a2-d1) did not fully closed as required with an esd event. Personnel identified that the supply gas tubing to the station discharge valve's actuator came dislodged during the initiation of the esd process which prevent the full closure of this valve. Personnel isolated the supply gas and then reconnected it to the actuator. Once reconnected the gas supply was opened again and the station discharge valve closed as required. This stopped the venting of natural gas from the station's esd valve.
Detailed record list
Report Received Date
2018-03-29 00:00:00
Iyear
2018
Report Number
20180035
Supplemental Number
30176
Report Type
Supplemental Final
Operator Id
Name
Tennessee Gas Pipeline Company
Operator Street Address
1001 Louisiana St
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-03-01 19:31:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2018-03-01 20:28:00
Commodity Released Type
Natural Gas
Unintentional Release
24118
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
No
Shutdown Explain
The Esd Happened Before The Incident.
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2018-03-01 20:03:00
On Site Datetime
2018-03-01 20:03:00
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
78330
Onshore City Name
Agua Dulce
Onshore County Name
Nueces
Designated Location
Milepost
Designated Name
Valve A2-D1
Pipe Fac Name
Compressore Station # 1
Segment Name
Gas Suppy Tubing To Valve A2-D1
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Compressor Station Equipment And Piping
Item Involved
Tubing
Installation Year
1999
Material Involved
Material Other Than Carbon Steel Or Plastic
Material Details
Stainless Steel
Release Type
Other
Release Type Details
The Supply Gas Tubing To The Station Discharge Valve's Actuator Came Dislodged During An Esd Event Which Kept The Valve From Going Fully Closed.
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
481
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
65118
Est Cost Intentional Release
0
Est Cost Prop Damage
608
Est Cost Emergency
0
Est Cost Other
0
Prpty
65726
Accident Psig
845
Mop Psig
860
Mop Cfr Section
192.619(A)(1)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Accident Identifier
Other
Accident Details
Local Operating Personnel Including Contractors.
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This was a manned facility and the gas control or scada was not responsible for the events that occurred at the compressor station.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Additional Vibration Ind
Yes
Preparer Name
K**** B******
Preparer Title
Pipeline Engineer - Compliance-Codes And Standards
Preparer Email
K************@k***********.com
Preparer Telephone
3616886492
Authorizer Name
J**** H********
Authorizer Title
Director - Compliance - Codes And Standards
Authorizer Telephone
7133699443
Authorizer Email
J**************@k***********.com
Narrative
On 3/1/18 at approximately 7:31 pm a compressor on unit 2 in the compressor building had an issue whereby the compressor rod packing began leaking causing the gas detector to sense 40% lel which initiated a station hazard atmosphere alarm and caused emergency shut down (esd). At 8:00pm an erl call was sent out. At 8:03 local operating personnel identified that the station esd valve was still venting gas beyond the typical station blow down time. Upon further investigation personnel found that station discharge valve (a2-d1) did not fully closed as required with an esd event. Personnel identified that the supply gas tubing to the station discharge valve's actuator came dislodged during the initiation of the esd process which prevent the full closure of this valve. Personnel isolated the supply gas and then reconnected it to the actuator. Once reconnected the gas supply was opened again and the station discharge valve closed as required. This stopped the venting of natural gas from the station's esd valve.
Report Received Date 2018-03-29 00:00:00
Iyear 2018
Report Number 20180035
Supplemental Number 30176
Report Type Supplemental Final
Operator Id 19160 PHMSA Enforcement
Name Tennessee Gas Pipeline Company
Operator Street Address 1001 Louisiana St
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-03-01 19:31:00
Location Latitude 27.7484 Google Maps OpenStreetMap
Location Longitude -97.8569 Google Maps OpenStreetMap
Nrc Rpt Num 1205581 NRC Report How to search
Nrc Rpt Datetime 2018-03-01 20:28:00
Commodity Released Type Natural Gas
Unintentional Release 24118
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind No
Shutdown Explain The Esd Happened Before The Incident.
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2018-03-01 20:03:00
On Site Datetime 2018-03-01 20:03:00
On Off Shore Onshore
Onshore State Abbreviation Tx
Onshore Postal Code 78330
Onshore City Name Agua Dulce
Onshore County Name Nueces
Designated Location Milepost
Designated Name Valve A2-D1
Pipe Fac Name Compressore Station # 1
Segment Name Gas Suppy Tubing To Valve A2-D1
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Compressor Station Equipment And Piping
Item Involved Tubing
Installation Year 1999
Material Involved Material Other Than Carbon Steel Or Plastic
Material Details Stainless Steel
Release Type Other
Release Type Details The Supply Gas Tubing To The Station Discharge Valve's Actuator Came Dislodged During An Esd Event Which Kept The Valve From Going Fully Closed.
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 481
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 65118
Est Cost Intentional Release 0
Est Cost Prop Damage 608
Est Cost Emergency 0
Est Cost Other 0
Prpty 65726
Accident Psig 845
Mop Psig 860
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Accident Identifier Other
Accident Details Local Operating Personnel Including Contractors.
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This was a manned facility and the gas control or scada was not responsible for the events that occurred at the compressor station.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Defective Or Loose Tubing Or Fitting
Eq Failure Type Defective Or Loose Tubing Or Fitting
Additional Vibration Ind Yes
Preparer Name K**** B******
Preparer Title Pipeline Engineer - Compliance-Codes And Standards
Preparer Email K************@k***********.com
Preparer Telephone 3616886492
Authorizer Name J**** H********
Authorizer Title Director - Compliance - Codes And Standards
Authorizer Telephone 7133699443
Authorizer Email J**************@k***********.com
Narrative On 3/1/18 at approximately 7:31 pm a compressor on unit 2 in the compressor building had an issue whereby the compressor rod packing began leaking causing the gas detector to sense 40% lel which initiated a station hazard atmosphere alarm and caused emergency shut down (esd). At 8:00pm an erl call was sent out. At 8:03 local operating personnel identified that the station esd valve was still venting gas beyond the typical station blow down time. Upon further investigation personnel found that station discharge valve (a2-d1) did not fully closed as required with an esd event. Personnel identified that the supply gas tubing to the station discharge valve's actuator came dislodged during the initiation of the esd process which prevent the full closure of this valve. Personnel isolated the supply gas and then reconnected it to the actuator. Once reconnected the gas supply was opened again and the station discharge valve closed as required. This stopped the venting of natural gas from the station's esd valve.

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