GD incident on 2018-02-23 — TX

Operator
Atmos Energy Corporation - Mid-Tex
Cause
Miscellaneous Root Causes
Commodity
Natural Gas
Program
GD
Damage and Injuries
1 fatality 0 injuries
Property damage (nominal)
$13,835
Incident datetime
2018-02-23 06:42
Report number
Location
TX, DALLAS
Narrative
On 2/23/2018, a natural gas explosion occurred at 3534 espanola drive, dallas, texas at 6:38 a.M. Multiple 911 calls came into the dallas fire-rescue dispatch center reporting the explosion. Five family members were in the house at the time of the accident. One resident's injuries were fatal. The other four residents sustained non-life-threatening injuries. At the time of the explosion, atmos personnel were in the area working to repair a non-hazardous leak in the 3500 block of espanola. An atmos operations supervisor heard the explosion and took immediate action to protect lives and make the area safe. He directed his crew to start evacuating a two-block area, north and south of the accident house. Firefighters and atmos crews went door-to-door advising residents to evacuate and to refrain from starting cars or switching on lights. The evacuation was completed in 12-15 minutes with the assistance of dallas fire-rescue. The atmos onsite operations supervisor, working with the operations manager and the director of operations, coordinated the shut-down of the main line in the alley behind 3534 espanola. The national transportation safety board (ntsb) arrived onsite on 2/25/2018. Atmos energy, the texas railroad commission (rrc), pipeline & hazardous materials safety administration (PHMSA), and dallas fire - rescue assisted with the ntsb's investigation. The probable cause of the explosion at 3534 espanola drive was the ignition of an accumulation of natural gas that leaked from the gas main that was damaged during a sewer replacement project 23 years earlier. Post-accident excavation confirmed the 2" main was cracked in the area it had been gouged, bent, and dented by mechanized equipment. The third-party damage was never reported to atmos.
Detailed record list
Occurred At
2018-02-23 06:42:00
Year
2018
Report Received Date
2018-03-23 00:00:00
Iyear
2018.0
Report Number
20180034.0
Supplemental Number
35120.0
Report Type
Supplemental Final
Operator Id
Name
Atmos Energy Corporation - Mid-Tex
Operator Street Address
5420 Lbj Freeway Suite 1800
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75240
Local Datetime
2018-02-23 06:38:00
Time Zone
Central
Daylight Savings Ind
No
Location Street Address
3534 Espanola Dr.
Location City Name
Dallas
Location County Name
Dallas
Location State Abbreviation
TX
Location Postal Code
75220
Location Latitude
Location Longitude
Flow Cont Main Valve Ind
Yes
Nrc Rpt Datetime
2018-02-23 07:34:00
Nrc Rpt Num
Additional Nrc Report Numbers
1205177
Commodity Released Type
Natural Gas
Unintentional Release
1.14
Intentional Release
0.04
Fatality Ind
Yes
Num Emp Fatalities
0
Num Contr Fatalities
0
Num Er Fatalities
0
Num Worker Fatalities
0
Num Gp Fatalities
1
Fatal
1
Injury Ind
No
Injure
0
Ignite Ind
Yes
Ignite Datetime
2018-02-23 06:38:00
How Extinguished
Other
How Extinguished Other Detail
A Fire Did Not Occur, And We Are Unable To Accurately Estimate Volume Of Gas Consumed By The Fire.
Gas Consumed By Fire In Mcf
1
Explode Ind
Yes
Num Pub Evacuated
42.0
Incident Identified Datetime
2018-02-23 06:42:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2018-02-23 06:42:00
On Site Datetime
2018-02-23 06:42:00
Federal
No
Location Type
Private Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48.0
Other Underground Facilities
Yes
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1946.0
Pipe Diameter
2.0
Pipe Specification
Api 5l
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Wt Steel
0.15
Release Type
Leak
Leak Type
Crack
Class Location Type
Class 3 Location
Est Cost Oper Paid
199000.0
Est Cost Prop Damage
13835.0
Est Cost Emergency
1353.0
Est Cost Other
0.0
Gas Cost In Mcf
7.19
Est Cost Unintentional Release
8.0
Est Cost Intentional Release
0.0
Prpty
214196.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
42.0
Num Persons Hosp Not Ovnght
4.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
42.0
Num Business Building Affctd
0.0
Accident Psig
25.0
Normal Psig
25.0
Mop Psig
55.0
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1946-01-01 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Level
5
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No abnormal changes in pressure
Employee Drug Test Ind
Yes
Num Employees Tested
31
Num Employees Failed
0
Contractor Drug Test Ind
Yes
Num Contractors Tested
12
Num Contractors Failed
0
Cause
Excavation Damage
Cause Details
Previous Damage Due To Excavation Activity
Ex Party Type
Previous Damage Due To Excavation Activity
Ex Hydrotest Leak Survey Date
2017-03-07 00:00:00
Ex Hydrotest Conducted Ind
No
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
Other
Excavator Type
Municipality
Excavator Equipment
Backhoe/trackhoe
Work Performed
Sewer (Sanitary/storm)
One Call Notified Ind
No
Service Interruption
Data Not Collected
Root Cause Category
Miscellaneous Root Causes
Root Cause Type
Previous Damage
Preparer Name
B*** B*****
Preparer Title
Director Regulatory And Compliance
Preparer Email
B**********@a**********.com
Preparer Telephone
806-787-9422
Local Contact Name
T**** L*****
Local Contact Email
T***********@a**********.com
Local Contact Telephone
469-261-7387
Authorizer Name
M**** S*****
Authorizer Title
Vice President Technical Services
Authorizer Telephone
214-206-2033
Authorizer Email
M***********@a**********.com
Narrative
On 2/23/2018, a natural gas explosion occurred at 3534 espanola drive, dallas, texas at 6:38 a.M. Multiple 911 calls came into the dallas fire-rescue dispatch center reporting the explosion. Five family members were in the house at the time of the accident. One resident's injuries were fatal. The other four residents sustained non-life-threatening injuries. At the time of the explosion, atmos personnel were in the area working to repair a non-hazardous leak in the 3500 block of espanola. An atmos operations supervisor heard the explosion and took immediate action to protect lives and make the area safe. He directed his crew to start evacuating a two-block area, north and south of the accident house. Firefighters and atmos crews went door-to-door advising residents to evacuate and to refrain from starting cars or switching on lights. The evacuation was completed in 12-15 minutes with the assistance of dallas fire-rescue. The atmos onsite operations supervisor, working with the operations manager and the director of operations, coordinated the shut-down of the main line in the alley behind 3534 espanola. The national transportation safety board (ntsb) arrived onsite on 2/25/2018. Atmos energy, the texas railroad commission (rrc), pipeline & hazardous materials safety administration (PHMSA), and dallas fire - rescue assisted with the ntsb's investigation. The probable cause of the explosion at 3534 espanola drive was the ignition of an accumulation of natural gas that leaked from the gas main that was damaged during a sewer replacement project 23 years earlier. Post-accident excavation confirmed the 2" main was cracked in the area it had been gouged, bent, and dented by mechanized equipment. The third-party damage was never reported to atmos.
Occurred At 2018-02-23 06:42:00
Year 2018
Report Received Date 2018-03-23 00:00:00
Iyear 2018.0
Report Number 20180034.0
Supplemental Number 35120.0
Report Type Supplemental Final
Operator Id 31348 PHMSA Enforcement
Name Atmos Energy Corporation - Mid-Tex
Operator Street Address 5420 Lbj Freeway Suite 1800
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75240
Local Datetime 2018-02-23 06:38:00
Time Zone Central
Daylight Savings Ind No
Location Street Address 3534 Espanola Dr.
Location City Name Dallas
Location County Name Dallas
Location State Abbreviation TX
Location Postal Code 75220
Location Latitude 32.868106 Google Maps OpenStreetMap
Location Longitude -96.859732 Google Maps OpenStreetMap
Flow Cont Main Valve Ind Yes
Nrc Rpt Datetime 2018-02-23 07:34:00
Nrc Rpt Num 1205026 NRC Report How to search
Additional Nrc Report Numbers 1205177
Commodity Released Type Natural Gas
Unintentional Release 1.14
Intentional Release 0.04
Fatality Ind Yes
Num Emp Fatalities 0
Num Contr Fatalities 0
Num Er Fatalities 0
Num Worker Fatalities 0
Num Gp Fatalities 1
Fatal 1
Injury Ind No
Injure 0
Ignite Ind Yes
Ignite Datetime 2018-02-23 06:38:00
How Extinguished Other
How Extinguished Other Detail A Fire Did Not Occur, And We Are Unable To Accurately Estimate Volume Of Gas Consumed By The Fire.
Gas Consumed By Fire In Mcf 1
Explode Ind Yes
Num Pub Evacuated 42.0
Incident Identified Datetime 2018-02-23 06:42:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2018-02-23 06:42:00
On Site Datetime 2018-02-23 06:42:00
Federal No
Location Type Private Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48.0
Other Underground Facilities Yes
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1946.0
Pipe Diameter 2.0
Pipe Specification Api 5l
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Wt Steel 0.15
Release Type Leak
Leak Type Crack
Class Location Type Class 3 Location
Est Cost Oper Paid 199000.0
Est Cost Prop Damage 13835.0
Est Cost Emergency 1353.0
Est Cost Other 0.0
Gas Cost In Mcf 7.19
Est Cost Unintentional Release 8.0
Est Cost Intentional Release 0.0
Prpty 214196.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 42.0
Num Persons Hosp Not Ovnght 4.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 42.0
Num Business Building Affctd 0.0
Accident Psig 25.0
Normal Psig 25.0
Mop Psig 55.0
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 1946-01-01 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Injection Pump
Gas Odorized Level 5
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No abnormal changes in pressure
Employee Drug Test Ind Yes
Num Employees Tested 31
Num Employees Failed 0
Contractor Drug Test Ind Yes
Num Contractors Tested 12
Num Contractors Failed 0
Cause Excavation Damage
Cause Details Previous Damage Due To Excavation Activity
Ex Party Type Previous Damage Due To Excavation Activity
Ex Hydrotest Leak Survey Date 2017-03-07 00:00:00
Ex Hydrotest Conducted Ind No
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype Other
Excavator Type Municipality
Excavator Equipment Backhoe/trackhoe
Work Performed Sewer (Sanitary/storm)
One Call Notified Ind No
Service Interruption Data Not Collected
Root Cause Category Miscellaneous Root Causes
Root Cause Type Previous Damage
Preparer Name B*** B*****
Preparer Title Director Regulatory And Compliance
Preparer Email B**********@a**********.com
Preparer Telephone 806-787-9422
Local Contact Name T**** L*****
Local Contact Email T***********@a**********.com
Local Contact Telephone 469-261-7387
Authorizer Name M**** S*****
Authorizer Title Vice President Technical Services
Authorizer Telephone 214-206-2033
Authorizer Email M***********@a**********.com
Narrative On 2/23/2018, a natural gas explosion occurred at 3534 espanola drive, dallas, texas at 6:38 a.M. Multiple 911 calls came into the dallas fire-rescue dispatch center reporting the explosion. Five family members were in the house at the time of the accident. One resident's injuries were fatal. The other four residents sustained non-life-threatening injuries. At the time of the explosion, atmos personnel were in the area working to repair a non-hazardous leak in the 3500 block of espanola. An atmos operations supervisor heard the explosion and took immediate action to protect lives and make the area safe. He directed his crew to start evacuating a two-block area, north and south of the accident house. Firefighters and atmos crews went door-to-door advising residents to evacuate and to refrain from starting cars or switching on lights. The evacuation was completed in 12-15 minutes with the assistance of dallas fire-rescue. The atmos onsite operations supervisor, working with the operations manager and the director of operations, coordinated the shut-down of the main line in the alley behind 3534 espanola. The national transportation safety board (ntsb) arrived onsite on 2/25/2018. Atmos energy, the texas railroad commission (rrc), pipeline & hazardous materials safety administration (PHMSA), and dallas fire - rescue assisted with the ntsb's investigation. The probable cause of the explosion at 3534 espanola drive was the ignition of an accumulation of natural gas that leaked from the gas main that was damaged during a sewer replacement project 23 years earlier. Post-accident excavation confirmed the 2" main was cracked in the area it had been gouged, bent, and dented by mechanized equipment. The third-party damage was never reported to atmos.

All rights reserved. Copyright © by ClearPHMSA