GD incident on 2018-01-19 — NY

Operator
Niagara Mohawk Power Corp
Cause
Pipe, Weld, Or Joint Failure
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,800
Incident datetime
2018-01-19 05:53
Report number
Location
NY, ONEIDA
Narrative
5/2/2018 supplemental report issued to reflect date and time of ignition, not identification of incident, and belowground facility (although the incident occurred aboveground). At 08:01 on 1/19/2018 national grid was made aware of a structure and pipeline facility fire at 1700 broad street. Gas was shut off at 13:48 to make the areas safe. The section of pipe was exposed and isolated in order to locate leak and determine the leak cause at approx. 17:50 on 1/19. Nine (9) people from three (3) buildings were evacuated. A small section of pipe was installed 23:00 on 1/19 to restore service via a one-way feed. Upon air test, the source of the leak was determined to be a pl-pl compression coupling on a 4" main, as determined on 1/24. Nrc was notified on 1/23 at 10:45 based on the possibility of exceeding the $50,000 incident criteria.
Detailed record list
Occurred At
2018-01-19 05:53:00
Year
2018
Report Received Date
2018-02-16 00:00:00
Iyear
2018.0
Report Number
20180027.0
Supplemental Number
30260.0
Report Type
Supplemental Final
Operator Id
Name
Niagara Mohawk Power Corp
Operator Street Address
300 Erie Boulevard West
Operator City Name
Syracuse
Operator State Abbreviation
NY
Operator Postal Code
13202
Local Datetime
2018-01-19 05:53:00
Location Street Address
1700 Broad Street
Location City Name
Utica
Location County Name
Oneida
Location State Abbreviation
NY
Location Postal Code
13501
Location Latitude
Location Longitude
Nrc Rpt Datetime
2018-01-23 10:45:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
4863.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
15.0
Incident Identified Datetime
2018-01-19 05:53:00
On Site Datetime
2018-01-19 07:15:00
Federal
No
Location Type
Private Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
42.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1971.0
Pipe Diameter
4.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11
Material Pe Pipe Code
Unknown
Release Type
Leak
Leak Type
Connection Failure
Class Location Type
Class 3 Location
Est Cost Oper Paid
250000.0
Est Cost Prop Damage
5800.0
Est Cost Emergency
27400.0
Est Cost Other
0.0
Est Cost Other Details
Question 2a Is Pending Evaluation By Claims Adjuster.
Est Cost Unintentional Release
13269.0
Prpty
296469.0
Commercial Affected
7.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
23.0
Normal Psig
23.0
Mop Psig
24.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The incident was not the result of any operation that the control room can perform.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Pipe, Weld, Or Joint Failure
Cause Details
Mechanical Joint Failure
Pwjf Failure Type
Mechanical Joint Failure
Mec Fitting Involved
Stab
Mec Manufacturer
Unk
Mec Fitting Material
Other
Mec Fitting Material Detail
Materials Joined: 1st Plastic, 2nd Plastic
Additional Other Ind
Yes
Additional Factor Details
Unknown At The Present Time. Fitting Submitted To Third Party Laboratory For Analysis. Also Do Not Know Cause Of The Fitting Failure (Question 25)
Result Material Ind
Yes
Result Material Subtype
Other
Result Material Details
Unknown At This Time
Hydrotest Conducted Ind
No
Preparer Name
C****** D* B*****
Preparer Title
Prin Program Manager Federal Programs
Preparer Email
C*************@n***********.com
Preparer Telephone
6317703549
Authorizer Name
C****** D* B*****
Authorizer Title
Prin Program Manager Federal Programs
Authorizer Telephone
6317703549
Authorizer Email
C*************@n***********.com
Narrative
5/2/2018 supplemental report issued to reflect date and time of ignition, not identification of incident, and belowground facility (although the incident occurred aboveground). At 08:01 on 1/19/2018 national grid was made aware of a structure and pipeline facility fire at 1700 broad street. Gas was shut off at 13:48 to make the areas safe. The section of pipe was exposed and isolated in order to locate leak and determine the leak cause at approx. 17:50 on 1/19. Nine (9) people from three (3) buildings were evacuated. A small section of pipe was installed 23:00 on 1/19 to restore service via a one-way feed. Upon air test, the source of the leak was determined to be a pl-pl compression coupling on a 4" main, as determined on 1/24. Nrc was notified on 1/23 at 10:45 based on the possibility of exceeding the $50,000 incident criteria.
Occurred At 2018-01-19 05:53:00
Year 2018
Report Received Date 2018-02-16 00:00:00
Iyear 2018.0
Report Number 20180027.0
Supplemental Number 30260.0
Report Type Supplemental Final
Operator Id 13480 PHMSA Enforcement
Name Niagara Mohawk Power Corp
Operator Street Address 300 Erie Boulevard West
Operator City Name Syracuse
Operator State Abbreviation NY
Operator Postal Code 13202
Local Datetime 2018-01-19 05:53:00
Location Street Address 1700 Broad Street
Location City Name Utica
Location County Name Oneida
Location State Abbreviation NY
Location Postal Code 13501
Location Latitude 43.0955314 Google Maps OpenStreetMap
Location Longitude -75.1975277 Google Maps OpenStreetMap
Nrc Rpt Datetime 2018-01-23 10:45:00
Nrc Rpt Num 1202624 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 4863.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 15.0
Incident Identified Datetime 2018-01-19 05:53:00
On Site Datetime 2018-01-19 07:15:00
Federal No
Location Type Private Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 42.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1971.0
Pipe Diameter 4.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 11
Material Pe Pipe Code Unknown
Release Type Leak
Leak Type Connection Failure
Class Location Type Class 3 Location
Est Cost Oper Paid 250000.0
Est Cost Prop Damage 5800.0
Est Cost Emergency 27400.0
Est Cost Other 0.0
Est Cost Other Details Question 2a Is Pending Evaluation By Claims Adjuster.
Est Cost Unintentional Release 13269.0
Prpty 296469.0
Commercial Affected 7.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 23.0
Normal Psig 23.0
Mop Psig 24.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The incident was not the result of any operation that the control room can perform.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Pipe, Weld, Or Joint Failure
Cause Details Mechanical Joint Failure
Pwjf Failure Type Mechanical Joint Failure
Mec Fitting Involved Stab
Mec Manufacturer Unk
Mec Fitting Material Other
Mec Fitting Material Detail Materials Joined: 1st Plastic, 2nd Plastic
Additional Other Ind Yes
Additional Factor Details Unknown At The Present Time. Fitting Submitted To Third Party Laboratory For Analysis. Also Do Not Know Cause Of The Fitting Failure (Question 25)
Result Material Ind Yes
Result Material Subtype Other
Result Material Details Unknown At This Time
Hydrotest Conducted Ind No
Preparer Name C****** D* B*****
Preparer Title Prin Program Manager Federal Programs
Preparer Email C*************@n***********.com
Preparer Telephone 6317703549
Authorizer Name C****** D* B*****
Authorizer Title Prin Program Manager Federal Programs
Authorizer Telephone 6317703549
Authorizer Email C*************@n***********.com
Narrative 5/2/2018 supplemental report issued to reflect date and time of ignition, not identification of incident, and belowground facility (although the incident occurred aboveground). At 08:01 on 1/19/2018 national grid was made aware of a structure and pipeline facility fire at 1700 broad street. Gas was shut off at 13:48 to make the areas safe. The section of pipe was exposed and isolated in order to locate leak and determine the leak cause at approx. 17:50 on 1/19. Nine (9) people from three (3) buildings were evacuated. A small section of pipe was installed 23:00 on 1/19 to restore service via a one-way feed. Upon air test, the source of the leak was determined to be a pl-pl compression coupling on a 4" main, as determined on 1/24. Nrc was notified on 1/23 at 10:45 based on the possibility of exceeding the $50,000 incident criteria.

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