GD incident on 2017-12-28 — CA

Operator
Southern California Gas Co
Cause
Other Outside Force Damage
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,882
Incident datetime
2017-12-28 07:16
Report number
Location
CA, RIVERSIDE
Narrative
On december 28th, socalgas responded to a structure fire at a single-family home located at 41140 nona court in the city of hemet. Upon arrival crews found the ignited gas blowing from the riser and the home engulfed in flames. The gas release was controlled by pinching 2' plastic main. No injuries or further damage resulted from this incident. Repairs to the damaged riser were completed and it was left clamped and plugged at the service valve. Investigation of the incident showed that the meter for this customer had been removed on april 15, 2014 due to non-payment. The service valve was left in a locked closed position. At some point after the meter was removed the customer tampered with the service valve and installed a bypass and regulator to supply gas to the houseline. This incident was reported due to media coverage damages in excess of $50,000. This incident was also reported to the cpuc.
Detailed record list
Occurred At
2017-12-28 07:16:00
Year
2017
Report Received Date
2018-01-26 00:00:00
Iyear
2017.0
Report Number
20180016.0
Supplemental Number
16770.0
Report Type
Original Final
Operator Id
Name
Southern California Gas Co
Operator Street Address
555 West Fifth Street
Operator City Name
Los Angeles
Operator State Abbreviation
CA
Operator Postal Code
90013
Local Datetime
2017-12-28 05:01:00
Location Street Address
41140 Nona Court
Location City Name
Hemet
Location County Name
Riverside
Location State Abbreviation
CA
Location Postal Code
92544-0000
Location Latitude
Location Longitude
Nrc Rpt Datetime
2017-12-28 09:34:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
11.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
12.0
Incident Identified Datetime
2017-12-28 07:16:00
On Site Datetime
2017-12-28 07:16:00
Federal
No
Location Type
Private Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Service Riser
Installation Year
1984.0
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Other
Release Type Details
Failed Illegal Bypass
Class Location Type
Class 3 Location
Est Cost Oper Paid
250000.0
Est Cost Prop Damage
1882.0
Est Cost Emergency
200.0
Est Cost Other
0.0
Est Cost Unintentional Release
66.0
Prpty
252148.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
7.0
Accident Psig
54.0
Normal Psig
54.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Intentional Damage
Outside Force Type
Intentional Damage
Intentional Subtype
Theft Of Transported Commodity
Preparer Name
M****** B********
Preparer Title
Pipeline Safety And Compliance Advisor
Preparer Email
M*********@s**************.com
Preparer Telephone
7144780745
Authorizer Name
M****** B********
Authorizer Title
Pipeline Safety And Compliance Advisor
Authorizer Telephone
7144780745
Authorizer Email
M*********@s**************.com
Narrative
On december 28th, socalgas responded to a structure fire at a single-family home located at 41140 nona court in the city of hemet. Upon arrival crews found the ignited gas blowing from the riser and the home engulfed in flames. The gas release was controlled by pinching 2' plastic main. No injuries or further damage resulted from this incident. Repairs to the damaged riser were completed and it was left clamped and plugged at the service valve. Investigation of the incident showed that the meter for this customer had been removed on april 15, 2014 due to non-payment. The service valve was left in a locked closed position. At some point after the meter was removed the customer tampered with the service valve and installed a bypass and regulator to supply gas to the houseline. This incident was reported due to media coverage damages in excess of $50,000. This incident was also reported to the cpuc.
Occurred At 2017-12-28 07:16:00
Year 2017
Report Received Date 2018-01-26 00:00:00
Iyear 2017.0
Report Number 20180016.0
Supplemental Number 16770.0
Report Type Original Final
Operator Id 18484 PHMSA Enforcement
Name Southern California Gas Co
Operator Street Address 555 West Fifth Street
Operator City Name Los Angeles
Operator State Abbreviation CA
Operator Postal Code 90013
Local Datetime 2017-12-28 05:01:00
Location Street Address 41140 Nona Court
Location City Name Hemet
Location County Name Riverside
Location State Abbreviation CA
Location Postal Code 92544-0000
Location Latitude 33.72657 Google Maps OpenStreetMap
Location Longitude -116.943 Google Maps OpenStreetMap
Nrc Rpt Datetime 2017-12-28 09:34:00
Nrc Rpt Num 1200667 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 11.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 12.0
Incident Identified Datetime 2017-12-28 07:16:00
On Site Datetime 2017-12-28 07:16:00
Federal No
Location Type Private Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Service Riser
Installation Year 1984.0
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Release Type Other
Release Type Details Failed Illegal Bypass
Class Location Type Class 3 Location
Est Cost Oper Paid 250000.0
Est Cost Prop Damage 1882.0
Est Cost Emergency 200.0
Est Cost Other 0.0
Est Cost Unintentional Release 66.0
Prpty 252148.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 7.0
Accident Psig 54.0
Normal Psig 54.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Intentional Damage
Outside Force Type Intentional Damage
Intentional Subtype Theft Of Transported Commodity
Preparer Name M****** B********
Preparer Title Pipeline Safety And Compliance Advisor
Preparer Email M*********@s**************.com
Preparer Telephone 7144780745
Authorizer Name M****** B********
Authorizer Title Pipeline Safety And Compliance Advisor
Authorizer Telephone 7144780745
Authorizer Email M*********@s**************.com
Narrative On december 28th, socalgas responded to a structure fire at a single-family home located at 41140 nona court in the city of hemet. Upon arrival crews found the ignited gas blowing from the riser and the home engulfed in flames. The gas release was controlled by pinching 2' plastic main. No injuries or further damage resulted from this incident. Repairs to the damaged riser were completed and it was left clamped and plugged at the service valve. Investigation of the incident showed that the meter for this customer had been removed on april 15, 2014 due to non-payment. The service valve was left in a locked closed position. At some point after the meter was removed the customer tampered with the service valve and installed a bypass and regulator to supply gas to the houseline. This incident was reported due to media coverage damages in excess of $50,000. This incident was also reported to the cpuc.

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