HL incident on 2017-12-02 — TX

Operator
Wyoming Pipeline Company
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2017-12-02 06:00
Report number
Location
TX
Narrative
On december 1st work began on connecting a newly constructed tank to an existing pump and pipeline system. At the end of the work day the final set of flanges to the pump were lined up and studs and nuts were installed, there was some additional work that still needed to be completed to align the pump so these flanges were to be completed the following day.. During the night as the level of the tank rose, the limits on the mov on shell valve on the tank were not set correctly and the valve was not fully seated. As the tank level rose the shell valve began to leak by filling the newly constructed suction piping. When the crude in the new suction line filled to the point of the un-tightened flanges it began to leak into the pump containment. Based on tank gauges and site evaluation, it was determined that 33 barrels of crude was release on and around the pump pad. All free crude was removed from site with a vacuum truck and 2 loads of contaminate soil was removed and will be disposed of properly.
Detailed record list
Report Received Date
2017-12-21 00:00:00
Iyear
2017
Report Number
20170428
Supplemental Number
23047
Report Type
Supplemental Final
Operator Id
Name
Wyoming Pipeline Company
Operator Street Address
825 Town & Country Lane
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77024
Local Datetime
2017-12-02 06:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
33
Recovered Bbls
33
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-12-02 06:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Shut Down Prior To The Release For Maintenance.
On Site Datetime
2017-12-02 06:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Thunder Creek
Segment Name
Thunder Creek Station
Onshore State Abbreviation
Wy
Onshore Postal Code
82701
Onshore City Name
Not Within A Municipality
Onshore County Name
Weston
Designated Location
Milepost/valve Station
Designated Name
Thunder Creek
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Flange Assembly
Installation Year
2017
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
5000
Est Cost Emergency
15000
Est Cost Environmental
0
Est Cost Other
0
Prpty
20000
Accident Psig
5
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
There would have been no indication to the control room that the release occured.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related No Proc Ind
Yes
Category Type
Commissioning
Operator Qualification Ind
No
Preparer Name
M***** E*****
Preparer Title
Logistics Manager
Preparer Email
M******@p*********.com
Preparer Telephone
2192306675
Prepared Date
2018-01-16 00:00:00
Authorizer Name
M***** E*****
Authorizer Telephone
2192306675
Authorizer Title
Logistics Manager
Authorizer Email
M******@p*********.com
Narrative
On december 1st work began on connecting a newly constructed tank to an existing pump and pipeline system. At the end of the work day the final set of flanges to the pump were lined up and studs and nuts were installed, there was some additional work that still needed to be completed to align the pump so these flanges were to be completed the following day.. During the night as the level of the tank rose, the limits on the mov on shell valve on the tank were not set correctly and the valve was not fully seated. As the tank level rose the shell valve began to leak by filling the newly constructed suction piping. When the crude in the new suction line filled to the point of the un-tightened flanges it began to leak into the pump containment. Based on tank gauges and site evaluation, it was determined that 33 barrels of crude was release on and around the pump pad. All free crude was removed from site with a vacuum truck and 2 loads of contaminate soil was removed and will be disposed of properly.
Report Received Date 2017-12-21 00:00:00
Iyear 2017
Report Number 20170428
Supplemental Number 23047
Report Type Supplemental Final
Operator Id 32537 PHMSA Enforcement
Name Wyoming Pipeline Company
Operator Street Address 825 Town & Country Lane
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77024
Local Datetime 2017-12-02 06:00:00
Location Latitude 43.66692 Google Maps OpenStreetMap
Location Longitude -105.06688 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 33
Recovered Bbls 33
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-12-02 06:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Was Shut Down Prior To The Release For Maintenance.
On Site Datetime 2017-12-02 06:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Thunder Creek
Segment Name Thunder Creek Station
Onshore State Abbreviation Wy
Onshore Postal Code 82701
Onshore City Name Not Within A Municipality
Onshore County Name Weston
Designated Location Milepost/valve Station
Designated Name Thunder Creek
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Flange Assembly
Installation Year 2017
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 5000
Est Cost Emergency 15000
Est Cost Environmental 0
Est Cost Other 0
Prpty 20000
Accident Psig 5
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details There would have been no indication to the control room that the release occured.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related No Proc Ind Yes
Category Type Commissioning
Operator Qualification Ind No
Preparer Name M***** E*****
Preparer Title Logistics Manager
Preparer Email M******@p*********.com
Preparer Telephone 2192306675
Prepared Date 2018-01-16 00:00:00
Authorizer Name M***** E*****
Authorizer Telephone 2192306675
Authorizer Title Logistics Manager
Authorizer Email M******@p*********.com
Narrative On december 1st work began on connecting a newly constructed tank to an existing pump and pipeline system. At the end of the work day the final set of flanges to the pump were lined up and studs and nuts were installed, there was some additional work that still needed to be completed to align the pump so these flanges were to be completed the following day.. During the night as the level of the tank rose, the limits on the mov on shell valve on the tank were not set correctly and the valve was not fully seated. As the tank level rose the shell valve began to leak by filling the newly constructed suction piping. When the crude in the new suction line filled to the point of the un-tightened flanges it began to leak into the pump containment. Based on tank gauges and site evaluation, it was determined that 33 barrels of crude was release on and around the pump pad. All free crude was removed from site with a vacuum truck and 2 loads of contaminate soil was removed and will be disposed of properly.

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