HL incident on 2017-11-18 — TX

Operator
Kinder Morgan Utopia Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$12,000
Incident datetime
2017-11-18 16:15
Report number
Location
TX
Narrative
This release occurred during the commissioning of the new utopia pipeline. The leak was detected on a section of pipe acquired from eds that previously carried propane, was idled in nitrogen, and was being filled with ethane. On november 18, 2017 a field technician arrived at legacy eds block valve 87 and observed bubbles coming through the soil that were visible due to recent rain causing puddles in the area. Hydrocarbons were detected and the commissioning process was halted while the upstream and downstream valves were used to isolate the valve site. Equipment was brought in to blowdown/flare product from the line segment. The cause and impact of this release are still being assessed. 1/4/2018 update: part a.10: estimated volume of intentional and/or controlled release/blowdown (barrels) revised from 13,516 barrels to 4,898 barrels due to new information from engineering and controls regarding product movement at the time of the incident. 6/14/2018 update (final): pipeline commissioning resumed after valve replacement.
Detailed record list
Report Received Date
2017-12-18 00:00:00
Iyear
2017
Report Number
20170420
Supplemental Number
30506
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Utopia Llc
Operator Street Address
1001 Louisiana St. Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-11-18 16:15:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethane
Unintentional Release Bbls
0.1
Intentional Release Bbls
4897
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-11-18 16:15:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-11-18 16:47:00
Restart Datetime
2017-12-22 12:00:00
On Site Datetime
2017-11-18 16:15:00
Nrc Rpt Datetime
2017-11-18 18:07:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Legacy Eds Bv 87
Segment Name
Legacy Eds Bv 87
Onshore State Abbreviation
Oh
Onshore Postal Code
43402
Onshore City Name
Bowling Green
Onshore County Name
Wood
Designated Location
Milepost/valve Station
Designated Name
Eds Bv 87
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
Unknown
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Installation Year
1974
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
41135
Est Cost Prop Damage
12000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
53135
Accident Psig
450
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
96096
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release from the valve was estimated to be at a rate too low to be detected by the control room.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Preparer Name
K*** M*******
Preparer Title
Pipeline Engineer
Preparer Email
K************@k***********.com
Preparer Telephone
713-420-4454
Prepared Date
2018-06-14 00:00:00
Authorizer Name
B*** F***
Authorizer Telephone
713-369-9454
Authorizer Title
Director Compliance Codes And Standards
Authorizer Email
B********@k***********.com
Narrative
This release occurred during the commissioning of the new utopia pipeline. The leak was detected on a section of pipe acquired from eds that previously carried propane, was idled in nitrogen, and was being filled with ethane. On november 18, 2017 a field technician arrived at legacy eds block valve 87 and observed bubbles coming through the soil that were visible due to recent rain causing puddles in the area. Hydrocarbons were detected and the commissioning process was halted while the upstream and downstream valves were used to isolate the valve site. Equipment was brought in to blowdown/flare product from the line segment. The cause and impact of this release are still being assessed. 1/4/2018 update: part a.10: estimated volume of intentional and/or controlled release/blowdown (barrels) revised from 13,516 barrels to 4,898 barrels due to new information from engineering and controls regarding product movement at the time of the incident. 6/14/2018 update (final): pipeline commissioning resumed after valve replacement.
Report Received Date 2017-12-18 00:00:00
Iyear 2017
Report Number 20170420
Supplemental Number 30506
Report Type Supplemental Final
Operator Id 39518 PHMSA Enforcement
Name Kinder Morgan Utopia Llc
Operator Street Address 1001 Louisiana St. Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-11-18 16:15:00
Location Latitude 41.45722 Google Maps OpenStreetMap
Location Longitude -83.55669 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethane
Unintentional Release Bbls 0.1
Intentional Release Bbls 4897
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-11-18 16:15:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-11-18 16:47:00
Restart Datetime 2017-12-22 12:00:00
On Site Datetime 2017-11-18 16:15:00
Nrc Rpt Datetime 2017-11-18 18:07:00
Nrc Rpt Num 1197651 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Legacy Eds Bv 87
Segment Name Legacy Eds Bv 87
Onshore State Abbreviation Oh
Onshore Postal Code 43402
Onshore City Name Bowling Green
Onshore County Name Wood
Designated Location Milepost/valve Station
Designated Name Eds Bv 87
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover Unknown
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Installation Year 1974
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 41135
Est Cost Prop Damage 12000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 53135
Accident Psig 450
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 96096
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release from the valve was estimated to be at a rate too low to be detected by the control room.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind Yes
Preparer Name K*** M*******
Preparer Title Pipeline Engineer
Preparer Email K************@k***********.com
Preparer Telephone 713-420-4454
Prepared Date 2018-06-14 00:00:00
Authorizer Name B*** F***
Authorizer Telephone 713-369-9454
Authorizer Title Director Compliance Codes And Standards
Authorizer Email B********@k***********.com
Narrative This release occurred during the commissioning of the new utopia pipeline. The leak was detected on a section of pipe acquired from eds that previously carried propane, was idled in nitrogen, and was being filled with ethane. On november 18, 2017 a field technician arrived at legacy eds block valve 87 and observed bubbles coming through the soil that were visible due to recent rain causing puddles in the area. Hydrocarbons were detected and the commissioning process was halted while the upstream and downstream valves were used to isolate the valve site. Equipment was brought in to blowdown/flare product from the line segment. The cause and impact of this release are still being assessed. 1/4/2018 update: part a.10: estimated volume of intentional and/or controlled release/blowdown (barrels) revised from 13,516 barrels to 4,898 barrels due to new information from engineering and controls regarding product movement at the time of the incident. 6/14/2018 update (final): pipeline commissioning resumed after valve replacement.

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