HL incident on 2017-11-16 — TX

Operator
Tc Oil Pipeline Operations Inc
Cause
Material Failure Of Pipe Or Weld
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,682,477
Incident datetime
2017-11-16 05:36
Report number
Location
TX
Narrative
On 16 nov, 2017, at 05:34 cst, a pressure drop was experienced on keystone approximately 17.4 miles downstream of ludden pump station, resulting in the pipeline being shut down. At 09:15, technicians confirmed oil on the ground. At 10:13 cst, the nrc was called, and a report generated (1197446) and distributed at 10:26. Contact with PHMSA accident investigation division made at 1025; PHMSA on site from 17 to 28 nov. Pipeline was subsequently restarted on 29 nov after replacement of failed section. Metallurgical testing being performed by the national transportation safety board; results pending. Regarding part d, 1a., there one bird and one raccoon were lost. 20180315 supplemental report: updated commodity released and recovered, costs associated with the accident, and cause of the failure (second party damage) as derived from the national transportation safety board (ntsb) draft metallurgic report, and confirmed by a mutually agreed upon third party contractor, keifner and associates. 20180810 supplemental report: final costs received and vetted through leadership on 20180724, with approval on 20180801. 20180822 - updated part g apparent cause to a g5 from a g8, and part e for controller investigation. 20181109 - updated part a volume released to 6,592 bbls; volume derived through pipe integrity calculation based on exact location, depth of cover, actual shutdown times, and position of the rupture.
Detailed record list
Report Received Date
2017-12-16 00:00:00
Iyear
2017
Report Number
20170417
Supplemental Number
31163
Report Type
Supplemental Final
Operator Id
Name
Tc Oil Pipeline Operations Inc
Operator Street Address
Bank Of America Center - 700 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002-2700
Local Datetime
2017-11-16 05:33:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
6592
Recovered Bbls
6592
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2017-11-16 05:36:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-11-16 05:33:00
Restart Datetime
2017-11-29 10:00:00
On Site Datetime
2017-11-16 09:15:00
Nrc Rpt Datetime
2017-11-16 10:13:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Keystone Pipeline
Segment Name
Ks6
Onshore State Abbreviation
Sd
Onshore Postal Code
57421
Onshore City Name
Not Within A Municipality
Onshore County Name
Marshall County
Designated Location
Milepost/valve Station
Designated Name
Mp 234.3
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
30
Pipe Wall Thickness
0.386
Pipe Smys
70000
Pipe Specification
Api 5l
Pipe Seam Type
Dsaw
Pipe Manufacturer
Berg
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
2008
Manufactured Year
2007
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Longitudinal
Rupture Width
11.3
Rupture Length
52
Wildlife Impact Ind
Yes
Birds Impact Ind
Yes
Terrestrial Impact Ind
Yes
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Vegetation Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
823400
Est Cost Gas Released
583560
Est Cost Prop Damage
5682477
Est Cost Emergency
6042594
Est Cost Environmental
31677529
Est Cost Other
0
Est Cost Other Details
All Costs Are Final As Of 20180724.
Prpty
44809560
Accident Psig
1067
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
125664
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Fatigue Vibr Related
Yes
Failure Subtype
Pressure-Related
Additional Gouge Ind
Yes
Additional Crack Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Other Tool Tech Ind
Yes
Axial Recent Year
2016
Geometry Recent Year
2016
Other Tool
Acoustic Leak Detection
Other Recent Year
2017
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
E*** H*****
Preparer Title
Us Regulatory Compliance Manager
Preparer Email
E**********@t**********.com
Preparer Telephone
4024907253
Prepared Date
2018-11-09 00:00:00
Authorizer Name
S**** K****
Authorizer Telephone
4039207255
Authorizer Title
Vice President - Safety Quality And Compliance
Authorizer Email
S**********@t**********.com
Narrative
On 16 nov, 2017, at 05:34 cst, a pressure drop was experienced on keystone approximately 17.4 miles downstream of ludden pump station, resulting in the pipeline being shut down. At 09:15, technicians confirmed oil on the ground. At 10:13 cst, the nrc was called, and a report generated (1197446) and distributed at 10:26. Contact with PHMSA accident investigation division made at 1025; PHMSA on site from 17 to 28 nov. Pipeline was subsequently restarted on 29 nov after replacement of failed section. Metallurgical testing being performed by the national transportation safety board; results pending. Regarding part d, 1a., there one bird and one raccoon were lost. 20180315 supplemental report: updated commodity released and recovered, costs associated with the accident, and cause of the failure (second party damage) as derived from the national transportation safety board (ntsb) draft metallurgic report, and confirmed by a mutually agreed upon third party contractor, keifner and associates. 20180810 supplemental report: final costs received and vetted through leadership on 20180724, with approval on 20180801. 20180822 - updated part g apparent cause to a g5 from a g8, and part e for controller investigation. 20181109 - updated part a volume released to 6,592 bbls; volume derived through pipe integrity calculation based on exact location, depth of cover, actual shutdown times, and position of the rupture.
Report Received Date 2017-12-16 00:00:00
Iyear 2017
Report Number 20170417
Supplemental Number 31163
Report Type Supplemental Final
Operator Id 32334 PHMSA Enforcement
Name Tc Oil Pipeline Operations Inc
Operator Street Address Bank Of America Center - 700 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002-2700
Local Datetime 2017-11-16 05:33:00
Location Latitude 45.709444 Google Maps OpenStreetMap
Location Longitude -97.876944 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 6592
Recovered Bbls 6592
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2017-11-16 05:36:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-11-16 05:33:00
Restart Datetime 2017-11-29 10:00:00
On Site Datetime 2017-11-16 09:15:00
Nrc Rpt Datetime 2017-11-16 10:13:00
Nrc Rpt Num 1197446 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Keystone Pipeline
Segment Name Ks6
Onshore State Abbreviation Sd
Onshore Postal Code 57421
Onshore City Name Not Within A Municipality
Onshore County Name Marshall County
Designated Location Milepost/valve Station
Designated Name Mp 234.3
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 30
Pipe Wall Thickness 0.386
Pipe Smys 70000
Pipe Specification Api 5l
Pipe Seam Type Dsaw
Pipe Manufacturer Berg
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year 2008
Manufactured Year 2007
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Longitudinal
Rupture Width 11.3
Rupture Length 52
Wildlife Impact Ind Yes
Birds Impact Ind Yes
Terrestrial Impact Ind Yes
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Vegetation Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 823400
Est Cost Gas Released 583560
Est Cost Prop Damage 5682477
Est Cost Emergency 6042594
Est Cost Environmental 31677529
Est Cost Other 0
Est Cost Other Details All Costs Are Final As Of 20180724.
Prpty 44809560
Accident Psig 1067
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 125664
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind Yes
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind Yes
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Fatigue Vibr Related Yes
Failure Subtype Pressure-Related
Additional Gouge Ind Yes
Additional Crack Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Other Tool Tech Ind Yes
Axial Recent Year 2016
Geometry Recent Year 2016
Other Tool Acoustic Leak Detection
Other Recent Year 2017
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name E*** H*****
Preparer Title Us Regulatory Compliance Manager
Preparer Email E**********@t**********.com
Preparer Telephone 4024907253
Prepared Date 2018-11-09 00:00:00
Authorizer Name S**** K****
Authorizer Telephone 4039207255
Authorizer Title Vice President - Safety Quality And Compliance
Authorizer Email S**********@t**********.com
Narrative On 16 nov, 2017, at 05:34 cst, a pressure drop was experienced on keystone approximately 17.4 miles downstream of ludden pump station, resulting in the pipeline being shut down. At 09:15, technicians confirmed oil on the ground. At 10:13 cst, the nrc was called, and a report generated (1197446) and distributed at 10:26. Contact with PHMSA accident investigation division made at 1025; PHMSA on site from 17 to 28 nov. Pipeline was subsequently restarted on 29 nov after replacement of failed section. Metallurgical testing being performed by the national transportation safety board; results pending. Regarding part d, 1a., there one bird and one raccoon were lost. 20180315 supplemental report: updated commodity released and recovered, costs associated with the accident, and cause of the failure (second party damage) as derived from the national transportation safety board (ntsb) draft metallurgic report, and confirmed by a mutually agreed upon third party contractor, keifner and associates. 20180810 supplemental report: final costs received and vetted through leadership on 20180724, with approval on 20180801. 20180822 - updated part g apparent cause to a g5 from a g8, and part e for controller investigation. 20181109 - updated part a volume released to 6,592 bbls; volume derived through pipe integrity calculation based on exact location, depth of cover, actual shutdown times, and position of the rupture.

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