HL incident on 2017-11-19 — TX

Operator
Equistar Chemicals, L.p.
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$200
Incident datetime
2017-11-19 22:18
Report number
Location
TX
Narrative
Equistar pipeline control center received lel alarm at the tivoli pump station on the cross country system 31 vidauri to ps2 (tivoli). The pump station emergency shut-down (esd) activated per design, the pump station valves aligned to by-pass the station and the pressure within the pump station was sent to the flare. On-call technicians were dispatched to investigate the alarm and esd. At 1:05am on 11/20/2017, the technicians discovered a 3/8in stainless steel tubing to a pressure transmitter had failed on the pump discharge. The tubing was replaced and subsequently the pump station was brought back online. The investigation revealed the tubing failure was due to high cycle, low stress mechanical fatigue suggesting high-frequency vibration as the likely cause. The tubing was connected to a pressure transmitter which was mounted in a manner that amplified vibrations transferred from the pump discharge piping. To prevent recurrence the pressure transmitter will be remounted to address high frequency vibration and the investigation findings and corrective action will be communicated to employees.
Detailed record list
Report Received Date
2017-12-14 00:00:00
Iyear
2017
Report Number
20170414
Supplemental Number
30691
Report Type
Supplemental Final
Operator Id
Name
Equistar Chemicals, L.p.
Operator Street Address
16055 Space Center Blvd., Ste. 350
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77062
Local Datetime
2017-11-19 22:18:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethylene
Unintentional Release Bbls
9.78
Intentional Release Bbls
38.41
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Controller
Operator Type
Operator Employee
Incident Identified Datetime
2017-11-19 22:18:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-11-19 22:18:00
Restart Datetime
2017-11-20 15:42:00
On Site Datetime
2017-11-20 01:05:00
Nrc Rpt Datetime
2017-11-20 02:55:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
31_cross Country System
Segment Name
Cc19_vidauri To Tivoli Ps; Pes Id# 75190
Onshore State Abbreviation
Tx
Onshore Postal Code
77990
Onshore City Name
Tivoli
Onshore County Name
Refugio
Designated Location
Milepost/valve Station
Designated Name
64.1
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tubing
Installation Year
2015
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Rupture
Rupture Orient
Circumferential
Rupture Width
0.4
Rupture Length
1.2
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
452
Est Cost Prop Damage
200
Est Cost Emergency
2400
Est Cost Environmental
0
Est Cost Other
0
Prpty
3052
Accident Psig
1741
Mop Psig
2500
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Station was operating within limits at the time of the automated station shutdown. All pump and station controls where in automatic at the time of the shutdown.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Additional Vibration Ind
Yes
Additional Installation Ind
Yes
Preparer Name
G****** L* L******
Preparer Title
Principle Environmental Engineer
Preparer Email
G**************@l**.com
Preparer Telephone
281-709-0703
Preparer Fax
281-709-0759
Prepared Date
2018-07-25 00:00:00
Authorizer Name
M****** S* C*****
Authorizer Telephone
281-709-0626
Authorizer Title
Technical Manager
Authorizer Email
M*************@l**.com
Narrative
Equistar pipeline control center received lel alarm at the tivoli pump station on the cross country system 31 vidauri to ps2 (tivoli). The pump station emergency shut-down (esd) activated per design, the pump station valves aligned to by-pass the station and the pressure within the pump station was sent to the flare. On-call technicians were dispatched to investigate the alarm and esd. At 1:05am on 11/20/2017, the technicians discovered a 3/8in stainless steel tubing to a pressure transmitter had failed on the pump discharge. The tubing was replaced and subsequently the pump station was brought back online. The investigation revealed the tubing failure was due to high cycle, low stress mechanical fatigue suggesting high-frequency vibration as the likely cause. The tubing was connected to a pressure transmitter which was mounted in a manner that amplified vibrations transferred from the pump discharge piping. To prevent recurrence the pressure transmitter will be remounted to address high frequency vibration and the investigation findings and corrective action will be communicated to employees.
Report Received Date 2017-12-14 00:00:00
Iyear 2017
Report Number 20170414
Supplemental Number 30691
Report Type Supplemental Final
Operator Id 25146 PHMSA Enforcement
Name Equistar Chemicals, L.p.
Operator Street Address 16055 Space Center Blvd., Ste. 350
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77062
Local Datetime 2017-11-19 22:18:00
Location Latitude 28.466611 Google Maps OpenStreetMap
Location Longitude -96.932756 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethylene
Unintentional Release Bbls 9.78
Intentional Release Bbls 38.41
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Controller
Operator Type Operator Employee
Incident Identified Datetime 2017-11-19 22:18:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-11-19 22:18:00
Restart Datetime 2017-11-20 15:42:00
On Site Datetime 2017-11-20 01:05:00
Nrc Rpt Datetime 2017-11-20 02:55:00
Nrc Rpt Num 1197724 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name 31_cross Country System
Segment Name Cc19_vidauri To Tivoli Ps; Pes Id# 75190
Onshore State Abbreviation Tx
Onshore Postal Code 77990
Onshore City Name Tivoli
Onshore County Name Refugio
Designated Location Milepost/valve Station
Designated Name 64.1
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Tubing
Installation Year 2015
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Rupture
Rupture Orient Circumferential
Rupture Width 0.4
Rupture Length 1.2
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 452
Est Cost Prop Damage 200
Est Cost Emergency 2400
Est Cost Environmental 0
Est Cost Other 0
Prpty 3052
Accident Psig 1741
Mop Psig 2500
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Station was operating within limits at the time of the automated station shutdown. All pump and station controls where in automatic at the time of the shutdown.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Defective Or Loose Tubing Or Fitting
Eq Failure Type Defective Or Loose Tubing Or Fitting
Additional Vibration Ind Yes
Additional Installation Ind Yes
Preparer Name G****** L* L******
Preparer Title Principle Environmental Engineer
Preparer Email G**************@l**.com
Preparer Telephone 281-709-0703
Preparer Fax 281-709-0759
Prepared Date 2018-07-25 00:00:00
Authorizer Name M****** S* C*****
Authorizer Telephone 281-709-0626
Authorizer Title Technical Manager
Authorizer Email M*************@l**.com
Narrative Equistar pipeline control center received lel alarm at the tivoli pump station on the cross country system 31 vidauri to ps2 (tivoli). The pump station emergency shut-down (esd) activated per design, the pump station valves aligned to by-pass the station and the pressure within the pump station was sent to the flare. On-call technicians were dispatched to investigate the alarm and esd. At 1:05am on 11/20/2017, the technicians discovered a 3/8in stainless steel tubing to a pressure transmitter had failed on the pump discharge. The tubing was replaced and subsequently the pump station was brought back online. The investigation revealed the tubing failure was due to high cycle, low stress mechanical fatigue suggesting high-frequency vibration as the likely cause. The tubing was connected to a pressure transmitter which was mounted in a manner that amplified vibrations transferred from the pump discharge piping. To prevent recurrence the pressure transmitter will be remounted to address high frequency vibration and the investigation findings and corrective action will be communicated to employees.

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