HL incident on 2017-11-20 — TX

Operator
Sfpp, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2017-11-20 11:20
Report number
Location
TX
Narrative
At approximately, 1120 on november 20, 2017, the concord operator discovered that the plains all american (customer incoming transfer line) incoming sample tube coming from the pipeline into sample house had separated and diesel was flowing from 3/8" tubing onto the sample house floor and flowing off onto adjacent soil. The valve from the tubing was immediately closed and the pipeline shutdown. Telephonic notifications were made. The release resulted in impacted/stained soil 10 feet long by 2 feet wide. Approximately 1.5 feet of impacted soil was removed down to a clay bottom with diesel product sitting on top of the clay which was removed via absorbents. Subsequent investigation determined the release amount to be 14.5 gallons (0.35 bbl) all of which was recovered. The 3/8-inch stainless steel tubing separated at the nut and bulk-head fitting at the sample house. Inspection of the nut, ferrule and the bulkhead showed signs of wear due, most likely, to incorrect installation. Vibration due to the loose ferrule on the tubing contributed to the failure. Note: part c, 4. Year item involved in accident was installed: tubing/fitting installed as part of a larger project in the mid-eighties. We are not exactly sure when this particular system was added.
Detailed record list
Report Received Date
2017-12-13 00:00:00
Iyear
2017
Report Number
20170412
Supplemental Number
22939
Report Type
Original Final
Operator Id
Name
Sfpp, Lp
Operator Street Address
1001 Louisiana St., Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-11-20 11:20:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.35
Recovered Bbls
0.35
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-11-20 11:20:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-11-20 11:40:00
Restart Datetime
2017-11-20 14:24:00
On Site Datetime
2017-11-20 11:20:00
Nrc Rpt Datetime
2017-11-20 11:48:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Concord Station
Segment Name
In-Station
Onshore State Abbreviation
Ca
Onshore Postal Code
94520
Onshore City Name
Concord
Onshore County Name
Contra Costa
Designated Location
Survey Station No.
Designated Name
In-Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Fitting/tubing Connection (Sample Shed)
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Installation Year
1985
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
28
Est Cost Prop Damage
500
Est Cost Emergency
3870
Est Cost Environmental
0
Est Cost Other
0
Prpty
4398
Accident Psig
50
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The system is independent of the scada system and therefore, not under the control of the operator.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Additional Installation Ind
Yes
Preparer Name
S**** M*******
Preparer Title
Mgr Ccs - Pacific
Preparer Email
S*************@k***********.com
Preparer Telephone
909-873-5146
Preparer Fax
303-984-3620
Prepared Date
2017-12-13 00:00:00
Authorizer Name
E***** A* F***
Authorizer Telephone
713-369-9454
Authorizer Title
Director Ccs
Authorizer Email
B********@k***********.com
Narrative
At approximately, 1120 on november 20, 2017, the concord operator discovered that the plains all american (customer incoming transfer line) incoming sample tube coming from the pipeline into sample house had separated and diesel was flowing from 3/8" tubing onto the sample house floor and flowing off onto adjacent soil. The valve from the tubing was immediately closed and the pipeline shutdown. Telephonic notifications were made. The release resulted in impacted/stained soil 10 feet long by 2 feet wide. Approximately 1.5 feet of impacted soil was removed down to a clay bottom with diesel product sitting on top of the clay which was removed via absorbents. Subsequent investigation determined the release amount to be 14.5 gallons (0.35 bbl) all of which was recovered. The 3/8-inch stainless steel tubing separated at the nut and bulk-head fitting at the sample house. Inspection of the nut, ferrule and the bulkhead showed signs of wear due, most likely, to incorrect installation. Vibration due to the loose ferrule on the tubing contributed to the failure. Note: part c, 4. Year item involved in accident was installed: tubing/fitting installed as part of a larger project in the mid-eighties. We are not exactly sure when this particular system was added.
Report Received Date 2017-12-13 00:00:00
Iyear 2017
Report Number 20170412
Supplemental Number 22939
Report Type Original Final
Operator Id 18092 PHMSA Enforcement
Name Sfpp, Lp
Operator Street Address 1001 Louisiana St., Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-11-20 11:20:00
Location Latitude 38.003958 Google Maps OpenStreetMap
Location Longitude -122.055376 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.35
Recovered Bbls 0.35
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-11-20 11:20:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-11-20 11:40:00
Restart Datetime 2017-11-20 14:24:00
On Site Datetime 2017-11-20 11:20:00
Nrc Rpt Datetime 2017-11-20 11:48:00
Nrc Rpt Num 1197772 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Concord Station
Segment Name In-Station
Onshore State Abbreviation Ca
Onshore Postal Code 94520
Onshore City Name Concord
Onshore County Name Contra Costa
Designated Location Survey Station No.
Designated Name In-Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Other
Incident Area Details Fitting/tubing Connection (Sample Shed)
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Installation Year 1985
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 28
Est Cost Prop Damage 500
Est Cost Emergency 3870
Est Cost Environmental 0
Est Cost Other 0
Prpty 4398
Accident Psig 50
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The system is independent of the scada system and therefore, not under the control of the operator.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Defective Or Loose Tubing Or Fitting
Eq Failure Type Defective Or Loose Tubing Or Fitting
Additional Installation Ind Yes
Preparer Name S**** M*******
Preparer Title Mgr Ccs - Pacific
Preparer Email S*************@k***********.com
Preparer Telephone 909-873-5146
Preparer Fax 303-984-3620
Prepared Date 2017-12-13 00:00:00
Authorizer Name E***** A* F***
Authorizer Telephone 713-369-9454
Authorizer Title Director Ccs
Authorizer Email B********@k***********.com
Narrative At approximately, 1120 on november 20, 2017, the concord operator discovered that the plains all american (customer incoming transfer line) incoming sample tube coming from the pipeline into sample house had separated and diesel was flowing from 3/8" tubing onto the sample house floor and flowing off onto adjacent soil. The valve from the tubing was immediately closed and the pipeline shutdown. Telephonic notifications were made. The release resulted in impacted/stained soil 10 feet long by 2 feet wide. Approximately 1.5 feet of impacted soil was removed down to a clay bottom with diesel product sitting on top of the clay which was removed via absorbents. Subsequent investigation determined the release amount to be 14.5 gallons (0.35 bbl) all of which was recovered. The 3/8-inch stainless steel tubing separated at the nut and bulk-head fitting at the sample house. Inspection of the nut, ferrule and the bulkhead showed signs of wear due, most likely, to incorrect installation. Vibration due to the loose ferrule on the tubing contributed to the failure. Note: part c, 4. Year item involved in accident was installed: tubing/fitting installed as part of a larger project in the mid-eighties. We are not exactly sure when this particular system was added.

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