HL incident on 2017-11-16 — PA

Operator
Buckeye Partners, Lp
Cause
Natural Force Damage
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$200
Incident datetime
2017-11-16 10:21
Report number
Location
PA
Narrative
On 11/16/17 at approximately 1021 hours, the local operator went out to the yard to tank 126 to open the tank drain valve (tap the tank) and drain any settled water in preparation for an outbound movement scheduled for later in the day. Upon entering the tank basin, some stained stone and a small amount of ulsd product was discovered in the dike. The facility received product that contained a high amount of corrosion inhibitor. Local operations personnel allowed the product to settle and periodically opened the tank drain valve at the bottom of the tank to remove the emulsion / water until they saw clean product (tapping). This process continued for several days. It is believed that water passed through the valve during this process. This water froze due to low temperatures. The ice caused the sight glass in the valve to crack allowing product to drip out. Internal and external notifications were completed. Linden fire and linden police departments arrived on site and were satisfied with the response. All free product was recovered during cleaning operations by osro. All repairs have been completed.
Detailed record list
Report Received Date
2017-12-13 00:00:00
Iyear
2017
Report Number
20170409
Supplemental Number
22941
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2017-11-16 10:21:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.24
Recovered Bbls
0.24
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-11-16 10:21:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Was Not Being Used At Time Of Discovery
On Site Datetime
2017-11-16 10:21:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Linden Tank 126
Segment Name
Ln 126
Onshore State Abbreviation
Nj
Onshore Postal Code
07036
Onshore City Name
Linden
Onshore County Name
Union County
Designated Location
Milepost/valve Station
Designated Name
Ln126
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Tank Type
Atmospheric
Installation Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Sight Glass
Release Type
Other
Release Type Details
Water Was Entrained In The Sight Glass On Water Draw System Which Froze And Cracked Sight Glass.
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
200
Est Cost Emergency
4100
Est Cost Environmental
0
Est Cost Other
1000
Est Cost Other Details
Cost For Disposal / Stone Replacement
Prpty
5300
Accident Psig
35
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release was not large enough to be detected through mechanical methods.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Temperature
Natural Force Type
Temperature
Temperature Subtype
Frozen Components
Nf Extreme Weather Ind
No
Preparer Name
D*** C*****
Preparer Title
Specialist District Compliance
Preparer Email
D******@b******.com
Preparer Telephone
215-262-2348
Prepared Date
2017-12-14 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
610 904 4113
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
On 11/16/17 at approximately 1021 hours, the local operator went out to the yard to tank 126 to open the tank drain valve (tap the tank) and drain any settled water in preparation for an outbound movement scheduled for later in the day. Upon entering the tank basin, some stained stone and a small amount of ulsd product was discovered in the dike. The facility received product that contained a high amount of corrosion inhibitor. Local operations personnel allowed the product to settle and periodically opened the tank drain valve at the bottom of the tank to remove the emulsion / water until they saw clean product (tapping). This process continued for several days. It is believed that water passed through the valve during this process. This water froze due to low temperatures. The ice caused the sight glass in the valve to crack allowing product to drip out. Internal and external notifications were completed. Linden fire and linden police departments arrived on site and were satisfied with the response. All free product was recovered during cleaning operations by osro. All repairs have been completed.
Report Received Date 2017-12-13 00:00:00
Iyear 2017
Report Number 20170409
Supplemental Number 22941
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2017-11-16 10:21:00
Location Latitude 40.608257 Google Maps OpenStreetMap
Location Longitude -74.238076 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.24
Recovered Bbls 0.24
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-11-16 10:21:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank Was Not Being Used At Time Of Discovery
On Site Datetime 2017-11-16 10:21:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Linden Tank 126
Segment Name Ln 126
Onshore State Abbreviation Nj
Onshore Postal Code 07036
Onshore City Name Linden
Onshore County Name Union County
Designated Location Milepost/valve Station
Designated Name Ln126
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Tank Type Atmospheric
Installation Year Unknown
Material Involved Material Other Than Carbon Steel
Material Details Sight Glass
Release Type Other
Release Type Details Water Was Entrained In The Sight Glass On Water Draw System Which Froze And Cracked Sight Glass.
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 200
Est Cost Emergency 4100
Est Cost Environmental 0
Est Cost Other 1000
Est Cost Other Details Cost For Disposal / Stone Replacement
Prpty 5300
Accident Psig 35
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release was not large enough to be detected through mechanical methods.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details Temperature
Natural Force Type Temperature
Temperature Subtype Frozen Components
Nf Extreme Weather Ind No
Preparer Name D*** C*****
Preparer Title Specialist District Compliance
Preparer Email D******@b******.com
Preparer Telephone 215-262-2348
Prepared Date 2017-12-14 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 610 904 4113
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative On 11/16/17 at approximately 1021 hours, the local operator went out to the yard to tank 126 to open the tank drain valve (tap the tank) and drain any settled water in preparation for an outbound movement scheduled for later in the day. Upon entering the tank basin, some stained stone and a small amount of ulsd product was discovered in the dike. The facility received product that contained a high amount of corrosion inhibitor. Local operations personnel allowed the product to settle and periodically opened the tank drain valve at the bottom of the tank to remove the emulsion / water until they saw clean product (tapping). This process continued for several days. It is believed that water passed through the valve during this process. This water froze due to low temperatures. The ice caused the sight glass in the valve to crack allowing product to drip out. Internal and external notifications were completed. Linden fire and linden police departments arrived on site and were satisfied with the response. All free product was recovered during cleaning operations by osro. All repairs have been completed.

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