HL incident on 2017-11-14 — TX

Operator
Dapl-Etco Operations Management, Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$19,119
Incident datetime
2017-11-14 07:10
Report number
Location
TX
Narrative
Operator employee discovered the leak during routine morning walkdown of facility at approximately 07:10 am. Call was placed immediately to the control center to isolate the station from the main line. After leak was isolated and stopped all free product was recovered and cleaned up inside pump house. Inspection determined leak came from a crack in a butt weld connection of a flange to a 2" thermal relief line around the discharge main line valve. Cause of the crack was determined to be excessive vibration. Subsequent to the release the welded connection was repaired. To prevent recurrence the thermal relief line has been redesigned so that the ends on either side of the main line valve remain blind flanged during normal operations. If the discharge valve is going to be closed a spool piece of 2" piping will be installed to complete the relief circuit while the valve remains closed. This design eliminates the stresses on the welds caused by the vibration. Other stations were inspected for similar design and circumstances. Where it was determined that vibration could be an issue temporary bracing was installed on the thermal relief lines until such time a permanent, engineered solution is designed and implemented.
Detailed record list
Report Received Date
2017-12-11 00:00:00
Iyear
2017
Report Number
20170407
Supplemental Number
22920
Report Type
Original Final
Operator Id
Name
Dapl-Etco Operations Management, Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-11-14 07:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.5
Recovered Bbls
0.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-11-14 07:10:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-11-14 07:24:00
Restart Datetime
2017-11-15 21:44:00
On Site Datetime
2017-11-14 07:10:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Dapl-Cambridge Pump Station
Segment Name
29004-30" Watford City To Patoka
Onshore State Abbreviation
Ia
Onshore Postal Code
50014
Onshore City Name
Cambridge
Onshore County Name
Styory
Designated Location
Survey Station No.
Designated Name
673.73
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Weld Subtype
Other Butt Weld
Installation Year
2016
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
19119
Est Cost Emergency
19000
Est Cost Environmental
0
Est Cost Other
0
Prpty
38119
Accident Psig
400
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Fatigue Vibr Related
Yes
Failure Subtype
Mechanical Vibration
Additional Crack Ind
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
Yes
Exm Radiography Rcnt Year
2016
Exm Radiography Rcnt Ind
Yes
Preparer Name
T*** G* N*******
Preparer Title
Sr. Manager-Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2017-12-11 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Sr. Manager-Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
Operator employee discovered the leak during routine morning walkdown of facility at approximately 07:10 am. Call was placed immediately to the control center to isolate the station from the main line. After leak was isolated and stopped all free product was recovered and cleaned up inside pump house. Inspection determined leak came from a crack in a butt weld connection of a flange to a 2" thermal relief line around the discharge main line valve. Cause of the crack was determined to be excessive vibration. Subsequent to the release the welded connection was repaired. To prevent recurrence the thermal relief line has been redesigned so that the ends on either side of the main line valve remain blind flanged during normal operations. If the discharge valve is going to be closed a spool piece of 2" piping will be installed to complete the relief circuit while the valve remains closed. This design eliminates the stresses on the welds caused by the vibration. Other stations were inspected for similar design and circumstances. Where it was determined that vibration could be an issue temporary bracing was installed on the thermal relief lines until such time a permanent, engineered solution is designed and implemented.
Report Received Date 2017-12-11 00:00:00
Iyear 2017
Report Number 20170407
Supplemental Number 22920
Report Type Original Final
Operator Id 39205 PHMSA Enforcement
Name Dapl-Etco Operations Management, Llc
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-11-14 07:00:00
Location Latitude 41.916909 Google Maps OpenStreetMap
Location Longitude -93.567881 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.5
Recovered Bbls 0.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-11-14 07:10:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-11-14 07:24:00
Restart Datetime 2017-11-15 21:44:00
On Site Datetime 2017-11-14 07:10:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Dapl-Cambridge Pump Station
Segment Name 29004-30" Watford City To Patoka
Onshore State Abbreviation Ia
Onshore Postal Code 50014
Onshore City Name Cambridge
Onshore County Name Styory
Designated Location Survey Station No.
Designated Name 673.73
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Inside A Building
Crossing No
Pipe Facility Type Interstate
Item Involved Weld, Including Heat-Affected Zone
Weld Subtype Other Butt Weld
Installation Year 2016
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 19119
Est Cost Emergency 19000
Est Cost Environmental 0
Est Cost Other 0
Prpty 38119
Accident Psig 400
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind Yes
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Fatigue Vibr Related Yes
Failure Subtype Mechanical Vibration
Additional Crack Ind Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind Yes
Exm Radiography Rcnt Year 2016
Exm Radiography Rcnt Ind Yes
Preparer Name T*** G* N*******
Preparer Title Sr. Manager-Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2017-12-11 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Sr. Manager-Dot Compliance
Authorizer Email T************@e*************.com
Narrative Operator employee discovered the leak during routine morning walkdown of facility at approximately 07:10 am. Call was placed immediately to the control center to isolate the station from the main line. After leak was isolated and stopped all free product was recovered and cleaned up inside pump house. Inspection determined leak came from a crack in a butt weld connection of a flange to a 2" thermal relief line around the discharge main line valve. Cause of the crack was determined to be excessive vibration. Subsequent to the release the welded connection was repaired. To prevent recurrence the thermal relief line has been redesigned so that the ends on either side of the main line valve remain blind flanged during normal operations. If the discharge valve is going to be closed a spool piece of 2" piping will be installed to complete the relief circuit while the valve remains closed. This design eliminates the stresses on the welds caused by the vibration. Other stations were inspected for similar design and circumstances. Where it was determined that vibration could be an issue temporary bracing was installed on the thermal relief lines until such time a permanent, engineered solution is designed and implemented.

All rights reserved. Copyright © by ClearPHMSA