HL incident on 2017-11-13 — TX

Operator
Sunoco Pipeline L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2017-11-13 07:22
Report number
Location
TX
Narrative
On 11/13/2017 a contract mobile meter prover was proving a meter at little tank farm. During the proving process the camlock connection fitting from the prover truck failed at the locking ear and came loose from the meter allowing approximately 15 barrels of crude oil to be released. Company operating personnel were on site and contacted the control center to immediately shut down the system and the prover inlet was capped to stop the release. All oil was recovered via vacuum truck and affected soil and gravel was placed in roll off containers for offsite disposal. Supplemental/final submitted 12/12/2017 to correct part a, 5 per PHMSA request.
Detailed record list
Report Received Date
2017-12-06 00:00:00
Iyear
2017
Report Number
20170403
Supplemental Number
22924
Report Type
Supplemental Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-11-13 07:22:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
15
Recovered Bbls
15
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-11-13 07:22:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-11-13 07:25:00
Restart Datetime
2017-11-13 08:00:00
On Site Datetime
2017-11-13 07:22:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing-Little Tank Farm
Segment Name
24012-30" Cushing To Little Tank Farm
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Payne
Designated Location
Milepost/valve Station
Designated Name
3
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Meter/prover
Installation Year
2010
Material Involved
Material Other Than Carbon Steel
Material Details
Brass
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Vegetation Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
799
Est Cost Prop Damage
0
Est Cost Emergency
5000
Est Cost Environmental
5000
Est Cost Other
0
Prpty
10799
Accident Psig
50
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
Yes
Num Contractors Tested
1
Num Contractors Failed
0
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Mechanical Coupling
Eq Additional Other Ind
Yes
Eq Additional Other Details
Camlock Fitting Connection From Prover Truck Failed At The Locking Ear.
Preparer Name
T*** G* N*******
Preparer Title
Sr. Manager-Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2017-12-12 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Sr. Manager-Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
On 11/13/2017 a contract mobile meter prover was proving a meter at little tank farm. During the proving process the camlock connection fitting from the prover truck failed at the locking ear and came loose from the meter allowing approximately 15 barrels of crude oil to be released. Company operating personnel were on site and contacted the control center to immediately shut down the system and the prover inlet was capped to stop the release. All oil was recovered via vacuum truck and affected soil and gravel was placed in roll off containers for offsite disposal. Supplemental/final submitted 12/12/2017 to correct part a, 5 per PHMSA request.
Report Received Date 2017-12-06 00:00:00
Iyear 2017
Report Number 20170403
Supplemental Number 22924
Report Type Supplemental Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-11-13 07:22:00
Location Latitude 35.986976 Google Maps OpenStreetMap
Location Longitude -96.745748 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 15
Recovered Bbls 15
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-11-13 07:22:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-11-13 07:25:00
Restart Datetime 2017-11-13 08:00:00
On Site Datetime 2017-11-13 07:22:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cushing-Little Tank Farm
Segment Name 24012-30" Cushing To Little Tank Farm
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Cushing
Onshore County Name Payne
Designated Location Milepost/valve Station
Designated Name 3
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Meter/prover
Installation Year 2010
Material Involved Material Other Than Carbon Steel
Material Details Brass
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Vegetation Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 799
Est Cost Prop Damage 0
Est Cost Emergency 5000
Est Cost Environmental 5000
Est Cost Other 0
Prpty 10799
Accident Psig 50
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind Yes
Num Contractors Tested 1
Num Contractors Failed 0
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Mechanical Coupling
Eq Additional Other Ind Yes
Eq Additional Other Details Camlock Fitting Connection From Prover Truck Failed At The Locking Ear.
Preparer Name T*** G* N*******
Preparer Title Sr. Manager-Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2017-12-12 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Sr. Manager-Dot Compliance
Authorizer Email T************@e*************.com
Narrative On 11/13/2017 a contract mobile meter prover was proving a meter at little tank farm. During the proving process the camlock connection fitting from the prover truck failed at the locking ear and came loose from the meter allowing approximately 15 barrels of crude oil to be released. Company operating personnel were on site and contacted the control center to immediately shut down the system and the prover inlet was capped to stop the release. All oil was recovered via vacuum truck and affected soil and gravel was placed in roll off containers for offsite disposal. Supplemental/final submitted 12/12/2017 to correct part a, 5 per PHMSA request.

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