HL incident on 2017-11-29 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$25
Incident datetime
2017-11-29 19:45
Report number
Location
TX
Narrative
On 11-29-17 at approximately 19:45 local operating personnel discovered the sample pot for meter-skid 350 had overflowed. The sample pot was isolated from the active movement and clean-up began. After the sample probe was removed it was discovered that an o-ring had failed. The o-ring was replaced, sample probe reinstalled, and sample skid returned to service. Accidents/incidents caused by equipment failure are trended and tracked in our operational containment program.
Detailed record list
Report Received Date
2017-12-06 00:00:00
Iyear
2017
Report Number
20170402
Supplemental Number
30816
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-11-29 19:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2017-11-29 19:45:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Sample System Was Isolated
On Site Datetime
2017-11-29 19:45:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Sealy Station
Segment Name
Ms 350 Sample Pot
Onshore State Abbreviation
Tx
Onshore Postal Code
77474
Onshore City Name
Sealy
Onshore County Name
Austin
Designated Location
Milepost/valve Station
Designated Name
Sealy Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Instrumentation
Installation Year
2011
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
55
Est Cost Prop Damage
25
Est Cost Emergency
2500
Est Cost Environmental
0
Est Cost Other
0
Prpty
2580
Accident Psig
94
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller nor control room were a contributing factor
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
Mechanical Failure
Preparer Name
L**** W*******
Preparer Title
Pipeline Compliance Senior Engineer
Preparer Email
L*********@e****.com
Preparer Telephone
713-381-6748
Prepared Date
2018-08-17 00:00:00
Authorizer Name
L**** W*******
Authorizer Telephone
713-381-6748
Authorizer Title
Pipeline Compliance Senior Engineer
Authorizer Email
L*********@e****.com
Narrative
On 11-29-17 at approximately 19:45 local operating personnel discovered the sample pot for meter-skid 350 had overflowed. The sample pot was isolated from the active movement and clean-up began. After the sample probe was removed it was discovered that an o-ring had failed. The o-ring was replaced, sample probe reinstalled, and sample skid returned to service. Accidents/incidents caused by equipment failure are trended and tracked in our operational containment program.
Report Received Date 2017-12-06 00:00:00
Iyear 2017
Report Number 20170402
Supplemental Number 30816
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-11-29 19:45:00
Location Latitude 29.759805 Google Maps OpenStreetMap
Location Longitude -96.148241 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2017-11-29 19:45:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Sample System Was Isolated
On Site Datetime 2017-11-29 19:45:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Sealy Station
Segment Name Ms 350 Sample Pot
Onshore State Abbreviation Tx
Onshore Postal Code 77474
Onshore City Name Sealy
Onshore County Name Austin
Designated Location Milepost/valve Station
Designated Name Sealy Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Instrumentation
Installation Year 2011
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 55
Est Cost Prop Damage 25
Est Cost Emergency 2500
Est Cost Environmental 0
Est Cost Other 0
Prpty 2580
Accident Psig 94
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller nor control room were a contributing factor
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Eq Additional Other Ind Yes
Eq Additional Other Details Mechanical Failure
Preparer Name L**** W*******
Preparer Title Pipeline Compliance Senior Engineer
Preparer Email L*********@e****.com
Preparer Telephone 713-381-6748
Prepared Date 2018-08-17 00:00:00
Authorizer Name L**** W*******
Authorizer Telephone 713-381-6748
Authorizer Title Pipeline Compliance Senior Engineer
Authorizer Email L*********@e****.com
Narrative On 11-29-17 at approximately 19:45 local operating personnel discovered the sample pot for meter-skid 350 had overflowed. The sample pot was isolated from the active movement and clean-up began. After the sample probe was removed it was discovered that an o-ring had failed. The o-ring was replaced, sample probe reinstalled, and sample skid returned to service. Accidents/incidents caused by equipment failure are trended and tracked in our operational containment program.

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