HL incident on 2017-11-07 — TX

Operator
Express Holdings (Usa), Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$8,000
Incident datetime
2017-11-07 15:55
Report number
Location
TX
Narrative
On november 7, 2017 the gower station main pump 4 had been online for 30 minutes. At approximately 14:46 cst main pump 3 was started, at that approximate time main pump 4 shut down due to seal fail. Valves 4s and 4d automatically closed to isolate main pump 4. A local technician was called to respond to the alarm. The technician arrived at gower station at 15:55 cst and confirmed a release of product inside the pump building due to a pump seal failure. All released product remained in the building.
Detailed record list
Report Received Date
2017-12-06 00:00:00
Iyear
2017
Report Number
20170401
Supplemental Number
22893
Report Type
Original Final
Operator Id
Name
Express Holdings (Usa), Llc
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2017-11-07 14:46:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.25
Recovered Bbls
0.25
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2017-11-07 15:55:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Facility Remained Online While Pump Was Isolated
On Site Datetime
2017-11-07 15:55:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Platte Gower Station
Segment Name
Unit #4
Onshore State Abbreviation
Mo
Onshore Postal Code
64454
Onshore City Name
Gower
Onshore County Name
Buchanan
Designated Location
Milepost/valve Station
Designated Name
Gower Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
2017
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
8000
Est Cost Emergency
2600
Est Cost Environmental
0
Est Cost Other
0
Prpty
10600
Accident Psig
832
Mop Psig
1036
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Pump seal failure not related to an operator action
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Eq Additional Other Ind
Yes
Eq Additional Other Details
Seal Failed 3 Weeks After Being Returned From Vendor After Rebuild
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Preparer Fax
715-398-4802
Prepared Date
2017-12-06 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
715-395-3619
Authorizer Title
Supervisor Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
On november 7, 2017 the gower station main pump 4 had been online for 30 minutes. At approximately 14:46 cst main pump 3 was started, at that approximate time main pump 4 shut down due to seal fail. Valves 4s and 4d automatically closed to isolate main pump 4. A local technician was called to respond to the alarm. The technician arrived at gower station at 15:55 cst and confirmed a release of product inside the pump building due to a pump seal failure. All released product remained in the building.
Report Received Date 2017-12-06 00:00:00
Iyear 2017
Report Number 20170401
Supplemental Number 22893
Report Type Original Final
Operator Id 31720 PHMSA Enforcement
Name Express Holdings (Usa), Llc
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2017-11-07 14:46:00
Location Latitude 39.643181 Google Maps OpenStreetMap
Location Longitude -94.618246 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.25
Recovered Bbls 0.25
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2017-11-07 15:55:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Facility Remained Online While Pump Was Isolated
On Site Datetime 2017-11-07 15:55:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Platte Gower Station
Segment Name Unit #4
Onshore State Abbreviation Mo
Onshore Postal Code 64454
Onshore City Name Gower
Onshore County Name Buchanan
Designated Location Milepost/valve Station
Designated Name Gower Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Inside A Building
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Installation Year 2017
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 8000
Est Cost Emergency 2600
Est Cost Environmental 0
Est Cost Other 0
Prpty 10600
Accident Psig 832
Mop Psig 1036
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Pump seal failure not related to an operator action
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Eq Additional Other Ind Yes
Eq Additional Other Details Seal Failed 3 Weeks After Being Returned From Vendor After Rebuild
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Preparer Fax 715-398-4802
Prepared Date 2017-12-06 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 715-395-3619
Authorizer Title Supervisor Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative On november 7, 2017 the gower station main pump 4 had been online for 30 minutes. At approximately 14:46 cst main pump 3 was started, at that approximate time main pump 4 shut down due to seal fail. Valves 4s and 4d automatically closed to isolate main pump 4. A local technician was called to respond to the alarm. The technician arrived at gower station at 15:55 cst and confirmed a release of product inside the pump building due to a pump seal failure. All released product remained in the building.

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