HL incident on 2017-11-07 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$15,000
Incident datetime
2017-11-07 20:30
Report number
Location
TX
Narrative
On november 7, 2017 at approximately 20:30 the pipeline operator at the north port arthur terminal was making rounds and found approximately .4 bbls of diesel on the ground by sump 5350. All pipelines that feed into that sump were shut down. The cause of the release was determined to be a leaking 1" valve on the drain line of the strainer on the meter run of the p113 pipeline. The hi hi alarm device on the sump did not activate as designed which caused the product that filled the sump to spill over onto the ground. The product was promptly cleaned up. To prevent recurrence of this type of release, the leaking 1" drain line valve was replaced, new level switches were installed on the sumps at the north port arthur terminal, and new software was deployed to ensure all alarms are received by the control room.
Detailed record list
Report Received Date
2017-12-05 00:00:00
Iyear
2017
Report Number
20170397
Supplemental Number
22869
Report Type
Original Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-11-07 20:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.4
Recovered Bbls
0.4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-11-07 20:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-11-07 20:30:00
Restart Datetime
2017-11-08 11:30:00
On Site Datetime
2017-11-07 20:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Port Arthur Terminal
Segment Name
P113
Onshore State Abbreviation
Tx
Onshore Postal Code
77640
Onshore City Name
Port Arthur
Onshore County Name
Jefferson
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2009
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
30
Est Cost Prop Damage
15000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
15030
Accident Psig
422
Mop Psig
740
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller not control room were a contributing factor
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Wear And Tear
Preparer Name
E**** W*******
Preparer Title
Pipeline Compliance Engineer
Preparer Email
E********@e****.com
Preparer Telephone
713-381-5757
Prepared Date
2017-12-05 00:00:00
Authorizer Name
E**** W*******
Authorizer Telephone
713-381-5757
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
E********@e****.com
Narrative
On november 7, 2017 at approximately 20:30 the pipeline operator at the north port arthur terminal was making rounds and found approximately .4 bbls of diesel on the ground by sump 5350. All pipelines that feed into that sump were shut down. The cause of the release was determined to be a leaking 1" valve on the drain line of the strainer on the meter run of the p113 pipeline. The hi hi alarm device on the sump did not activate as designed which caused the product that filled the sump to spill over onto the ground. The product was promptly cleaned up. To prevent recurrence of this type of release, the leaking 1" drain line valve was replaced, new level switches were installed on the sumps at the north port arthur terminal, and new software was deployed to ensure all alarms are received by the control room.
Report Received Date 2017-12-05 00:00:00
Iyear 2017
Report Number 20170397
Supplemental Number 22869
Report Type Original Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-11-07 20:30:00
Location Latitude 29.91201 Google Maps OpenStreetMap
Location Longitude -94.00891 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.4
Recovered Bbls 0.4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-11-07 20:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-11-07 20:30:00
Restart Datetime 2017-11-08 11:30:00
On Site Datetime 2017-11-07 20:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Port Arthur Terminal
Segment Name P113
Onshore State Abbreviation Tx
Onshore Postal Code 77640
Onshore City Name Port Arthur
Onshore County Name Jefferson
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2009
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 30
Est Cost Prop Damage 15000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 15030
Accident Psig 422
Mop Psig 740
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller not control room were a contributing factor
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind Yes
Eq Additional Other Details Wear And Tear
Preparer Name E**** W*******
Preparer Title Pipeline Compliance Engineer
Preparer Email E********@e****.com
Preparer Telephone 713-381-5757
Prepared Date 2017-12-05 00:00:00
Authorizer Name E**** W*******
Authorizer Telephone 713-381-5757
Authorizer Title Pipeline Compliance Engineer
Authorizer Email E********@e****.com
Narrative On november 7, 2017 at approximately 20:30 the pipeline operator at the north port arthur terminal was making rounds and found approximately .4 bbls of diesel on the ground by sump 5350. All pipelines that feed into that sump were shut down. The cause of the release was determined to be a leaking 1" valve on the drain line of the strainer on the meter run of the p113 pipeline. The hi hi alarm device on the sump did not activate as designed which caused the product that filled the sump to spill over onto the ground. The product was promptly cleaned up. To prevent recurrence of this type of release, the leaking 1" drain line valve was replaced, new level switches were installed on the sumps at the north port arthur terminal, and new software was deployed to ensure all alarms are received by the control room.

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