HL incident on 2017-10-22 — TX

Operator
Enbridge Storage (Cushing) L.l.c.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$78,300
Incident datetime
2017-10-22 13:29
Report number
Location
TX
Narrative
On october 22, 2017 at 13:29 cdt, a maintenance technician discovered crude oil on the ground in the cushing north terminal at manifold 153. The cushing control center was notified of the release and appropriate notifications were made. The system was shutdown at this time due to normal operations, but additional isolating steps were taken to secure the area. The source of the release was located on a 6" below grade piping near valve 153-v-cr3. A clamp was installed to prevent any further release of product as a temporary repair. The release is estimated at 2 barrels and was fully contained on-site. Clean-up was completed on october 23, 2017 and approximately 9 yards of contaminated soil was properly disposed of. Ut was conducted on the pipe by an nde technician and the leak cause was confirmed to be due to internal corrosion. The damaged line segment was removed and a new fabrication was installed and put back in service on november 8, 2017. The nrc was notified on october 22, 2017 (#1193991) when it was determined costs would exceed the $50,000 threshold. The nrc follow-up call was made at 9:59 cdt on october 24, 2017 (#1194136).
Detailed record list
Report Received Date
2017-11-17 00:00:00
Iyear
2017
Report Number
20170377
Supplemental Number
22824
Report Type
Original Final
Operator Id
Name
Enbridge Storage (Cushing) L.l.c.
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2017-10-22 13:29:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-10-22 13:29:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
System Already Shutdown Due To Normal Operations
On Site Datetime
2017-10-22 13:29:00
Nrc Rpt Datetime
2017-10-22 14:44:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing North Terminal
Segment Name
Manifold 153
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Payne
Designated Location
Milepost/valve Station
Designated Name
Cushing
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
12
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6
Pipe Wall Thickness
0.25
Pipe Smys
24000
Pipe Specification
Api 5l
Pipe Seam Type
Flash Welded
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
78300
Est Cost Emergency
27500
Est Cost Environmental
10960
Est Cost Other
0
Prpty
116860
Accident Psig
131
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Lack of control center involvement
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
General Corrosion
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Preparer Fax
715-398-4802
Prepared Date
2017-11-16 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
715-395-3619
Authorizer Title
Supervisor Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
On october 22, 2017 at 13:29 cdt, a maintenance technician discovered crude oil on the ground in the cushing north terminal at manifold 153. The cushing control center was notified of the release and appropriate notifications were made. The system was shutdown at this time due to normal operations, but additional isolating steps were taken to secure the area. The source of the release was located on a 6" below grade piping near valve 153-v-cr3. A clamp was installed to prevent any further release of product as a temporary repair. The release is estimated at 2 barrels and was fully contained on-site. Clean-up was completed on october 23, 2017 and approximately 9 yards of contaminated soil was properly disposed of. Ut was conducted on the pipe by an nde technician and the leak cause was confirmed to be due to internal corrosion. The damaged line segment was removed and a new fabrication was installed and put back in service on november 8, 2017. The nrc was notified on october 22, 2017 (#1193991) when it was determined costs would exceed the $50,000 threshold. The nrc follow-up call was made at 9:59 cdt on october 24, 2017 (#1194136).
Report Received Date 2017-11-17 00:00:00
Iyear 2017
Report Number 20170377
Supplemental Number 22824
Report Type Original Final
Operator Id 39145 PHMSA Enforcement
Name Enbridge Storage (Cushing) L.l.c.
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2017-10-22 13:29:00
Location Latitude 35.958915 Google Maps OpenStreetMap
Location Longitude -96.753261 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-10-22 13:29:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain System Already Shutdown Due To Normal Operations
On Site Datetime 2017-10-22 13:29:00
Nrc Rpt Datetime 2017-10-22 14:44:00
Nrc Rpt Num 1193991 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cushing North Terminal
Segment Name Manifold 153
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Cushing
Onshore County Name Payne
Designated Location Milepost/valve Station
Designated Name Cushing
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 12
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6
Pipe Wall Thickness 0.25
Pipe Smys 24000
Pipe Specification Api 5l
Pipe Seam Type Flash Welded
Pipe Manufacturer Unknown
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 100
Est Cost Prop Damage 78300
Est Cost Emergency 27500
Est Cost Environmental 10960
Est Cost Other 0
Prpty 116860
Accident Psig 131
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Lack of control center involvement
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results General Corrosion
Int Microbiological Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Preparer Fax 715-398-4802
Prepared Date 2017-11-16 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 715-395-3619
Authorizer Title Supervisor Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative On october 22, 2017 at 13:29 cdt, a maintenance technician discovered crude oil on the ground in the cushing north terminal at manifold 153. The cushing control center was notified of the release and appropriate notifications were made. The system was shutdown at this time due to normal operations, but additional isolating steps were taken to secure the area. The source of the release was located on a 6" below grade piping near valve 153-v-cr3. A clamp was installed to prevent any further release of product as a temporary repair. The release is estimated at 2 barrels and was fully contained on-site. Clean-up was completed on october 23, 2017 and approximately 9 yards of contaminated soil was properly disposed of. Ut was conducted on the pipe by an nde technician and the leak cause was confirmed to be due to internal corrosion. The damaged line segment was removed and a new fabrication was installed and put back in service on november 8, 2017. The nrc was notified on october 22, 2017 (#1193991) when it was determined costs would exceed the $50,000 threshold. The nrc follow-up call was made at 9:59 cdt on october 24, 2017 (#1194136).

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