HL incident on 2017-10-14 — LA

Operator
Epl Pipeline, Llc
Cause
Natural Force Damage
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,544,300
Incident datetime
2017-10-14 06:50
Report number
Location
LA
Narrative
Notified by operator of a large sheen on the water. Operators currently investigating the cause of the sheen. East division. Call recieved from tim brazer: updated flyover was conducted at 08:00 cdt, and the spill volume is now at 147 gallons, direction current dimensions: 36, 960 feet (7 miles) length, 5280 feet (1 mile) wide, 40% coverage, colors: 10% barely visible, 80% silvery, 10% slightly colored, moving toward the northwest. Update: caller confirmed source is from energy xxi and coming from 10 inch pipeline, currently isolated, sheen has dissipated, located 1.5 miles south of south pass 77a and south pass 57a. Pipeline segment# 15008. Updated nrc# 119-3261. Divers located separated pipe, which is believed to be caused by a mudslide due to the aftermath of hurricane nate. Pipeline was found approximately 250 feet south of original known location. For part a, question #9: the volume calculation for how much commodity was released is based off of the estimated square footage of the sheen multiplied by the estimated coverage determined by the appearance of the sheen. For part e, question #1: platform was brought back online at roughly 7 pm on 10/13. Pump was cycled up to 100 psig from 10/13 at 7:30 pm until shut-in at 6:30 am on 10/14 when sheen was spotted. Max pressure was 100 psig. Scada is not installed on this pipeline section, therefore no scada indications to report. For part g2: the pipeline was found to be buried 10-20 feet below the mud line eliminating the initial thought of an anchor drag. This pipeline is in a mudslide area and found to be approximately 250 ft south of its original location. In october of 2017 10" oil pipeline psn-15008 parted in a mudslide area between platform sp-77a and sp-55a. The scope of work entailed survey boat pipeline locating, and diver recon of the subsurface area, excavation of the pipeline at leak source with approximately 15' mud cover over the pipeline. Deep ditch excavation was required with a 3:1 safety factor on ditch wall utilizing diver's handjet, airlift, and toyo-pump. The diving contractor located leak path and installed a repair spool piece to repair the severed pipeline. Project duration was approximately 5 weeks.
Detailed record list
Report Received Date
2017-11-09 00:00:00
Iyear
2017
Report Number
20170362
Supplemental Number
31523
Report Type
Supplemental Final
Operator Id
Name
Epl Pipeline, Llc
Operator Street Address
1615 Poydras St. Suite 830
Operator City Name
New Orleans
Operator State Abbreviation
LA
Operator Postal Code
70112
Local Datetime
2017-10-14 06:50:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
3.5
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Offshore Production Operator Employee
Incident Identified Datetime
2017-10-14 06:50:00
System Part Involved
Offshore Pipeline, Including Riser And Riser Bend
On Off Shore
Offshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-10-14 06:55:00
Restart Datetime
2017-11-18 13:45:00
On Site Datetime
2017-10-15 09:00:00
Nrc Rpt Datetime
2017-10-14 08:01:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Off Water Depth
240
Off Accident Origin
On The Outer Continental Shelf (Ocs)
Off Ocs Area
South Pass
Off Ocs Block
56
Off Area Accident Type
Below Water, Pipe Buried Or Jetted Below Seabed
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10
Pipe Wall Thickness
0.5
Pipe Smys
35000
Pipe Specification
Api 5l
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
2006
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Circumferential
Rupture Width
12
Rupture Length
90.7
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
Yes
Ocean Seawater Ind
Yes
Amount Released
3.5
Rel Water Name
Gulf Of Mexico
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
175
Est Cost Prop Damage
2544300
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
2544475
Accident Psig
100
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
46094
Internal Inspection Ind
Yes
Operation Complications Ind
Yes
Excessive Debris Ind
Yes
Low Op Pressure Ind
Yes
Low Flow Ind
Yes
Pipeline Function
=< 20% Smys Regulated Gathering
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Heavy Rains/floods
Natural Force Type
Heavy Rains/floods
Heavy Rains Subtype
Mudslide
Nf Extreme Weather Ind
Yes
Nf Hurricane Ind
Yes
Preparer Name
D***** P***
Preparer Email
D****@r**.com
Preparer Telephone
713-655-8080
Prepared Date
2019-01-21 00:00:00
Authorizer Name
S****** H*****
Authorizer Telephone
713-396-4196
Authorizer Email
S******@e********.com
Narrative
Notified by operator of a large sheen on the water. Operators currently investigating the cause of the sheen. East division. Call recieved from tim brazer: updated flyover was conducted at 08:00 cdt, and the spill volume is now at 147 gallons, direction current dimensions: 36, 960 feet (7 miles) length, 5280 feet (1 mile) wide, 40% coverage, colors: 10% barely visible, 80% silvery, 10% slightly colored, moving toward the northwest. Update: caller confirmed source is from energy xxi and coming from 10 inch pipeline, currently isolated, sheen has dissipated, located 1.5 miles south of south pass 77a and south pass 57a. Pipeline segment# 15008. Updated nrc# 119-3261. Divers located separated pipe, which is believed to be caused by a mudslide due to the aftermath of hurricane nate. Pipeline was found approximately 250 feet south of original known location. For part a, question #9: the volume calculation for how much commodity was released is based off of the estimated square footage of the sheen multiplied by the estimated coverage determined by the appearance of the sheen. For part e, question #1: platform was brought back online at roughly 7 pm on 10/13. Pump was cycled up to 100 psig from 10/13 at 7:30 pm until shut-in at 6:30 am on 10/14 when sheen was spotted. Max pressure was 100 psig. Scada is not installed on this pipeline section, therefore no scada indications to report. For part g2: the pipeline was found to be buried 10-20 feet below the mud line eliminating the initial thought of an anchor drag. This pipeline is in a mudslide area and found to be approximately 250 ft south of its original location. In october of 2017 10" oil pipeline psn-15008 parted in a mudslide area between platform sp-77a and sp-55a. The scope of work entailed survey boat pipeline locating, and diver recon of the subsurface area, excavation of the pipeline at leak source with approximately 15' mud cover over the pipeline. Deep ditch excavation was required with a 3:1 safety factor on ditch wall utilizing diver's handjet, airlift, and toyo-pump. The diving contractor located leak path and installed a repair spool piece to repair the severed pipeline. Project duration was approximately 5 weeks.
Report Received Date 2017-11-09 00:00:00
Iyear 2017
Report Number 20170362
Supplemental Number 31523
Report Type Supplemental Final
Operator Id 31983 PHMSA Enforcement
Name Epl Pipeline, Llc
Operator Street Address 1615 Poydras St. Suite 830
Operator City Name New Orleans
Operator State Abbreviation LA
Operator Postal Code 70112
Local Datetime 2017-10-14 06:50:00
Location Latitude 28.843 Google Maps OpenStreetMap
Location Longitude -89.354 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 3.5
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Offshore Production Operator Employee
Incident Identified Datetime 2017-10-14 06:50:00
System Part Involved Offshore Pipeline, Including Riser And Riser Bend
On Off Shore Offshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-10-14 06:55:00
Restart Datetime 2017-11-18 13:45:00
On Site Datetime 2017-10-15 09:00:00
Nrc Rpt Datetime 2017-10-14 08:01:00
Nrc Rpt Num 1193233 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Off Water Depth 240
Off Accident Origin On The Outer Continental Shelf (Ocs)
Off Ocs Area South Pass
Off Ocs Block 56
Off Area Accident Type Below Water, Pipe Buried Or Jetted Below Seabed
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10
Pipe Wall Thickness 0.5
Pipe Smys 35000
Pipe Specification Api 5l
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year 2006
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Circumferential
Rupture Width 12
Rupture Length 90.7
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind Yes
Ocean Seawater Ind Yes
Amount Released 3.5
Rel Water Name Gulf Of Mexico
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 175
Est Cost Prop Damage 2544300
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 2544475
Accident Psig 100
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 46094
Internal Inspection Ind Yes
Operation Complications Ind Yes
Excessive Debris Ind Yes
Low Op Pressure Ind Yes
Low Flow Ind Yes
Pipeline Function =< 20% Smys Regulated Gathering
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details Heavy Rains/floods
Natural Force Type Heavy Rains/floods
Heavy Rains Subtype Mudslide
Nf Extreme Weather Ind Yes
Nf Hurricane Ind Yes
Preparer Name D***** P***
Preparer Email D****@r**.com
Preparer Telephone 713-655-8080
Prepared Date 2019-01-21 00:00:00
Authorizer Name S****** H*****
Authorizer Telephone 713-396-4196
Authorizer Email S******@e********.com
Narrative Notified by operator of a large sheen on the water. Operators currently investigating the cause of the sheen. East division. Call recieved from tim brazer: updated flyover was conducted at 08:00 cdt, and the spill volume is now at 147 gallons, direction current dimensions: 36, 960 feet (7 miles) length, 5280 feet (1 mile) wide, 40% coverage, colors: 10% barely visible, 80% silvery, 10% slightly colored, moving toward the northwest. Update: caller confirmed source is from energy xxi and coming from 10 inch pipeline, currently isolated, sheen has dissipated, located 1.5 miles south of south pass 77a and south pass 57a. Pipeline segment# 15008. Updated nrc# 119-3261. Divers located separated pipe, which is believed to be caused by a mudslide due to the aftermath of hurricane nate. Pipeline was found approximately 250 feet south of original known location. For part a, question #9: the volume calculation for how much commodity was released is based off of the estimated square footage of the sheen multiplied by the estimated coverage determined by the appearance of the sheen. For part e, question #1: platform was brought back online at roughly 7 pm on 10/13. Pump was cycled up to 100 psig from 10/13 at 7:30 pm until shut-in at 6:30 am on 10/14 when sheen was spotted. Max pressure was 100 psig. Scada is not installed on this pipeline section, therefore no scada indications to report. For part g2: the pipeline was found to be buried 10-20 feet below the mud line eliminating the initial thought of an anchor drag. This pipeline is in a mudslide area and found to be approximately 250 ft south of its original location. In october of 2017 10" oil pipeline psn-15008 parted in a mudslide area between platform sp-77a and sp-55a. The scope of work entailed survey boat pipeline locating, and diver recon of the subsurface area, excavation of the pipeline at leak source with approximately 15' mud cover over the pipeline. Deep ditch excavation was required with a 3:1 safety factor on ditch wall utilizing diver's handjet, airlift, and toyo-pump. The diving contractor located leak path and installed a repair spool piece to repair the severed pipeline. Project duration was approximately 5 weeks.

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