HL incident on 2017-10-10 — TX

Operator
Permian Express Partners Llc
Cause
Other Outside Force Damage
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$42,000
Incident datetime
2017-10-10 02:46
Report number
Location
TX
Narrative
At approximately 2:46 am on 10/10/2017 the control center was notified by caddo parish, la sheriff of a petroleum odor complaint in the area of finney station. Control center notified local operating personnel and began shutting the station and the associated pipeline system down as a precaution. The system was down by approximately 3:09 am. Local operating personnel arrived on site at approximately 3:00 am. The sheriff and local fire dept. Were already on site. Additional operating personnel responded to the station to aid in the investigation of the odor. At approximately 4:15 am, a hole in the shell of tank 312 was identified. The hole in the shell was located at a height of approximately 30'. Control center was contacted and they began to pump out of tank 312 into other tanks at the station in order to get the product level below the hole in the shell to stop the active leak. The tank was locked out after being pumped out to a level below the hole and clean up began. Upon investigation the hole in the tank shell appeared to have been caused by a bullet due to its extremely symmetrical and clean nature. Tsa and PHMSA were notified of the accident. To date, no party has been identified as a suspect in this matter. The tank remained locked out and the station was restarted at approximately 19:03 on 10/10/17. Clean up continued and on 10/13/17 it was determined that environmental clean-up costs would cause total costs for the accident to exceed $50,000 and nrc was notified. Report no. 1193186 was issued. Required 48 hour update was provided to nrc and report no. 1193392 was issued. The hole in the tank shell was repaired according to API 653 standards by a qualified contractor and was returned to service on 11/6/2017. Supplemental/final report submitted to address PHMSA accident investigation division request for updates to certain sections of report previously submitted as orginal/final.
Detailed record list
Report Received Date
2017-11-08 00:00:00
Iyear
2017
Report Number
20170361
Supplemental Number
30188
Report Type
Supplemental Final
Operator Id
Name
Permian Express Partners Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-10-10 02:46:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
10
Recovered Bbls
10
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Emergency Responder
Incident Identified Datetime
2017-10-10 02:46:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-10-10 03:09:00
Restart Datetime
2017-10-10 19:03:00
On Site Datetime
2017-10-10 03:00:00
Nrc Rpt Datetime
2017-10-13 13:59:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Finney Station Tank 312
Segment Name
26010-16"/18" Texoma To Finney
Onshore State Abbreviation
La
Onshore Postal Code
71115
Onshore City Name
Shreveport
Onshore County Name
Caddo
Designated Location
Milepost/valve Station
Designated Name
68
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Tank Shell
Tank Type
Atmospheric
Installation Year
1953
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Bullet Hole In Tank Shell
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
260
Est Cost Prop Damage
42000
Est Cost Emergency
104637
Est Cost Environmental
98856
Est Cost Other
0
Prpty
245753
Accident Psig
25
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Intentional Damage
Outside Force Type
Intentional Damage
Intentional Subtype
Vandalism
Preparer Name
T*** G* N*******
Preparer Title
Sr. Manager-Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2018-04-12 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Sr. Manager-Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
At approximately 2:46 am on 10/10/2017 the control center was notified by caddo parish, la sheriff of a petroleum odor complaint in the area of finney station. Control center notified local operating personnel and began shutting the station and the associated pipeline system down as a precaution. The system was down by approximately 3:09 am. Local operating personnel arrived on site at approximately 3:00 am. The sheriff and local fire dept. Were already on site. Additional operating personnel responded to the station to aid in the investigation of the odor. At approximately 4:15 am, a hole in the shell of tank 312 was identified. The hole in the shell was located at a height of approximately 30'. Control center was contacted and they began to pump out of tank 312 into other tanks at the station in order to get the product level below the hole in the shell to stop the active leak. The tank was locked out after being pumped out to a level below the hole and clean up began. Upon investigation the hole in the tank shell appeared to have been caused by a bullet due to its extremely symmetrical and clean nature. Tsa and PHMSA were notified of the accident. To date, no party has been identified as a suspect in this matter. The tank remained locked out and the station was restarted at approximately 19:03 on 10/10/17. Clean up continued and on 10/13/17 it was determined that environmental clean-up costs would cause total costs for the accident to exceed $50,000 and nrc was notified. Report no. 1193186 was issued. Required 48 hour update was provided to nrc and report no. 1193392 was issued. The hole in the tank shell was repaired according to API 653 standards by a qualified contractor and was returned to service on 11/6/2017. Supplemental/final report submitted to address PHMSA accident investigation division request for updates to certain sections of report previously submitted as orginal/final.
Report Received Date 2017-11-08 00:00:00
Iyear 2017
Report Number 20170361
Supplemental Number 30188
Report Type Supplemental Final
Operator Id 39596 PHMSA Enforcement
Name Permian Express Partners Llc
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-10-10 02:46:00
Location Latitude 32.35204 Google Maps OpenStreetMap
Location Longitude -93.68041 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 10
Recovered Bbls 10
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Emergency Responder
Incident Identified Datetime 2017-10-10 02:46:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-10-10 03:09:00
Restart Datetime 2017-10-10 19:03:00
On Site Datetime 2017-10-10 03:00:00
Nrc Rpt Datetime 2017-10-13 13:59:00
Nrc Rpt Num 1193186 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Finney Station Tank 312
Segment Name 26010-16"/18" Texoma To Finney
Onshore State Abbreviation La
Onshore Postal Code 71115
Onshore City Name Shreveport
Onshore County Name Caddo
Designated Location Milepost/valve Station
Designated Name 68
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Tank Vessel Subtype Tank Shell
Tank Type Atmospheric
Installation Year 1953
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Bullet Hole In Tank Shell
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 260
Est Cost Prop Damage 42000
Est Cost Emergency 104637
Est Cost Environmental 98856
Est Cost Other 0
Prpty 245753
Accident Psig 25
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Intentional Damage
Outside Force Type Intentional Damage
Intentional Subtype Vandalism
Preparer Name T*** G* N*******
Preparer Title Sr. Manager-Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2018-04-12 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Sr. Manager-Dot Compliance
Authorizer Email T************@e*************.com
Narrative At approximately 2:46 am on 10/10/2017 the control center was notified by caddo parish, la sheriff of a petroleum odor complaint in the area of finney station. Control center notified local operating personnel and began shutting the station and the associated pipeline system down as a precaution. The system was down by approximately 3:09 am. Local operating personnel arrived on site at approximately 3:00 am. The sheriff and local fire dept. Were already on site. Additional operating personnel responded to the station to aid in the investigation of the odor. At approximately 4:15 am, a hole in the shell of tank 312 was identified. The hole in the shell was located at a height of approximately 30'. Control center was contacted and they began to pump out of tank 312 into other tanks at the station in order to get the product level below the hole in the shell to stop the active leak. The tank was locked out after being pumped out to a level below the hole and clean up began. Upon investigation the hole in the tank shell appeared to have been caused by a bullet due to its extremely symmetrical and clean nature. Tsa and PHMSA were notified of the accident. To date, no party has been identified as a suspect in this matter. The tank remained locked out and the station was restarted at approximately 19:03 on 10/10/17. Clean up continued and on 10/13/17 it was determined that environmental clean-up costs would cause total costs for the accident to exceed $50,000 and nrc was notified. Report no. 1193186 was issued. Required 48 hour update was provided to nrc and report no. 1193392 was issued. The hole in the tank shell was repaired according to API 653 standards by a qualified contractor and was returned to service on 11/6/2017. Supplemental/final report submitted to address PHMSA accident investigation division request for updates to certain sections of report previously submitted as orginal/final.

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