HL incident on 2017-10-10 — TX

Operator
Centurion Pipeline L.p.
Cause
Excavation Issue
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$15,000
Incident datetime
2017-10-10 16:40
Report number
Location
TX
Narrative
On october 10th, 2017, a contractor working for plains all american pipeline (plains) was performing final grading of the right-of-way following backfill of the plains-centurion pipeline crossing site. The contracting company equipment operator, who was not authorized to perform any excavation at the site, struck the centurion's 16'' slaughter to cushing system #2 pipeline with a bulldozer. The subsequent pipeline strike punctured the line causing a loss onto the right-of-way approximately 377 barrels of crude oil. Approximately 164 barrels of crude oil were unrecovered, requiring soil remediation. Currently, the contaminated soil has been removed from the incident site and remediation efforts are ongoing. With remediation efforts still in progress, the reported cost estimates reflect the current total but may change after this report is filed. Any significant changes to the cost estimate will be reported in a supplemental report. Nrc report number 1192883 corresponds to the initial telephonic report for this accident, and nrc report number 1193089 corresponds to the 48 hour update report. The centurion pipeline was clearly and properly marked by qualified centurion personnel, and the contract excavation personnel were aware of the location of the line. All centurion policies and procedures were followed. The pipeline was placed back into service at 2:40 pm on october 12th, 2017. There were no associated injuries or fatalities. No oil reached a waterway and environmental remediation is anticipated to be successful. January 15, 2018: centurion pipeline, l.P. Is filing an additional supplemental and final report at PHMSA's request to change question a.4 to 16:40.
Detailed record list
Report Received Date
2017-11-08 00:00:00
Iyear
2017
Report Number
20170360
Supplemental Number
23045
Report Type
Supplemental Final
Operator Id
Name
Centurion Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-10-10 16:40:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
377
Recovered Bbls
377
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2017-10-10 16:40:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-10-10 16:40:00
Restart Datetime
2017-10-12 14:40:00
On Site Datetime
2017-10-10 17:15:00
Nrc Rpt Datetime
2017-10-10 17:55:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Slaughter To Cushing #2
Segment Name
Edmond Jct - Cushing #2
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Not Within A Municipality
Onshore County Name
Lincoln
Designated Location
Milepost/valve Station
Designated Name
Mp11.63
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
24
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
16
Pipe Wall Thickness
0.247
Pipe Smys
42000
Pipe Specification
Api 5lx, X42
Pipe Seam Type
Flash Welded
Pipe Manufacturer
A.o. Smith
Pipe Coating Type
Asphalt
Installation Year
1948
Manufactured Year
1948
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
3
Puncture Circum
2
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
8905
Est Cost Prop Damage
15000
Est Cost Emergency
40000
Est Cost Environmental
3000000
Est Cost Other
0
Prpty
3063905
Accident Psig
272
Mop Psig
857
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
204336
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
Yes
Private Row Ind
Yes
Private Subtype
Private Easement
Pipeline Easement Row Ind
Yes
Excavator Type
Contractor
Excavator Equipment
Grader/scraper
Work Performed
Grading
One Call Notified Ind
Yes
One Call Ticket Num
1.71003e+13
Locator Type
Utility Owner
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
46
Root Cause Category
Excavation Issue
Root Cause Type
Improper Backfilling Practices
Preparer Name
J***** M* M********
Preparer Title
Project Engineer - Pipeline Compliance
Preparer Email
J***************@o**.com
Preparer Telephone
713-552-8915
Preparer Fax
713-215-7445
Prepared Date
2018-01-15 00:00:00
Authorizer Name
D**** K* M****
Authorizer Telephone
713-366-5130
Authorizer Title
Pipeline Compliance Regulatory Consultant
Authorizer Email
D**********@o**.com
Narrative
On october 10th, 2017, a contractor working for plains all american pipeline (plains) was performing final grading of the right-of-way following backfill of the plains-centurion pipeline crossing site. The contracting company equipment operator, who was not authorized to perform any excavation at the site, struck the centurion's 16'' slaughter to cushing system #2 pipeline with a bulldozer. The subsequent pipeline strike punctured the line causing a loss onto the right-of-way approximately 377 barrels of crude oil. Approximately 164 barrels of crude oil were unrecovered, requiring soil remediation. Currently, the contaminated soil has been removed from the incident site and remediation efforts are ongoing. With remediation efforts still in progress, the reported cost estimates reflect the current total but may change after this report is filed. Any significant changes to the cost estimate will be reported in a supplemental report. Nrc report number 1192883 corresponds to the initial telephonic report for this accident, and nrc report number 1193089 corresponds to the 48 hour update report. The centurion pipeline was clearly and properly marked by qualified centurion personnel, and the contract excavation personnel were aware of the location of the line. All centurion policies and procedures were followed. The pipeline was placed back into service at 2:40 pm on october 12th, 2017. There were no associated injuries or fatalities. No oil reached a waterway and environmental remediation is anticipated to be successful. January 15, 2018: centurion pipeline, l.P. Is filing an additional supplemental and final report at PHMSA's request to change question a.4 to 16:40.
Report Received Date 2017-11-08 00:00:00
Iyear 2017
Report Number 20170360
Supplemental Number 23045
Report Type Supplemental Final
Operator Id 31888 PHMSA Enforcement
Name Centurion Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-10-10 16:40:00
Location Latitude 35.92762 Google Maps OpenStreetMap
Location Longitude -96.76167 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 377
Recovered Bbls 377
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2017-10-10 16:40:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-10-10 16:40:00
Restart Datetime 2017-10-12 14:40:00
On Site Datetime 2017-10-10 17:15:00
Nrc Rpt Datetime 2017-10-10 17:55:00
Nrc Rpt Num 1192883 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Slaughter To Cushing #2
Segment Name Edmond Jct - Cushing #2
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Not Within A Municipality
Onshore County Name Lincoln
Designated Location Milepost/valve Station
Designated Name Mp11.63
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 24
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 16
Pipe Wall Thickness 0.247
Pipe Smys 42000
Pipe Specification Api 5lx, X42
Pipe Seam Type Flash Welded
Pipe Manufacturer A.o. Smith
Pipe Coating Type Asphalt
Installation Year 1948
Manufactured Year 1948
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 3
Puncture Circum 2
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 8905
Est Cost Prop Damage 15000
Est Cost Emergency 40000
Est Cost Environmental 3000000
Est Cost Other 0
Prpty 3063905
Accident Psig 272
Mop Psig 857
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 204336
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind Yes
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt Yes
Private Row Ind Yes
Private Subtype Private Easement
Pipeline Easement Row Ind Yes
Excavator Type Contractor
Excavator Equipment Grader/scraper
Work Performed Grading
One Call Notified Ind Yes
One Call Ticket Num 1.71003e+13
Locator Type Utility Owner
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 46
Root Cause Category Excavation Issue
Root Cause Type Improper Backfilling Practices
Preparer Name J***** M* M********
Preparer Title Project Engineer - Pipeline Compliance
Preparer Email J***************@o**.com
Preparer Telephone 713-552-8915
Preparer Fax 713-215-7445
Prepared Date 2018-01-15 00:00:00
Authorizer Name D**** K* M****
Authorizer Telephone 713-366-5130
Authorizer Title Pipeline Compliance Regulatory Consultant
Authorizer Email D**********@o**.com
Narrative On october 10th, 2017, a contractor working for plains all american pipeline (plains) was performing final grading of the right-of-way following backfill of the plains-centurion pipeline crossing site. The contracting company equipment operator, who was not authorized to perform any excavation at the site, struck the centurion's 16'' slaughter to cushing system #2 pipeline with a bulldozer. The subsequent pipeline strike punctured the line causing a loss onto the right-of-way approximately 377 barrels of crude oil. Approximately 164 barrels of crude oil were unrecovered, requiring soil remediation. Currently, the contaminated soil has been removed from the incident site and remediation efforts are ongoing. With remediation efforts still in progress, the reported cost estimates reflect the current total but may change after this report is filed. Any significant changes to the cost estimate will be reported in a supplemental report. Nrc report number 1192883 corresponds to the initial telephonic report for this accident, and nrc report number 1193089 corresponds to the 48 hour update report. The centurion pipeline was clearly and properly marked by qualified centurion personnel, and the contract excavation personnel were aware of the location of the line. All centurion policies and procedures were followed. The pipeline was placed back into service at 2:40 pm on october 12th, 2017. There were no associated injuries or fatalities. No oil reached a waterway and environmental remediation is anticipated to be successful. January 15, 2018: centurion pipeline, l.P. Is filing an additional supplemental and final report at PHMSA's request to change question a.4 to 16:40.

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