HL incident on 2017-10-03 — TX

Operator
Inland Corporation
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$115,000
Incident datetime
2017-10-03 16:30
Report number
Location
TX
Narrative
On 10/3/2017 at 16:30, oregon, oh public works and fire chief notified local operator personnel of an odor complaint coming from the storm water sewers in the area. Between the dates of 10/3 and 10/8, operator personnel investigated the odor complaint. On 10/8/2017 at 14:33 operator verified a pin-hole leak in the 10" lima-toledo pipeline (line id 13201). After discovery of release, due to water impact, nrc was notified at 15:34 local time on 10/8 and report no. 1192655 was issued. Operator assessed adjacent pipeline near point of pinhole leak, cut out the section of failed piping and replaced with new piping. Required 48 hour update to nrc was made on 10/10/2017 and report no. 1192855 was issued. Failed pipe was sent to 3rd party laboratory for metallurgical analysis. Metallurgical analysis confirmed the cause of the failure as external corrosion pitting and thinning of the pipe wall. The failure was accompanied by a 1.5" linear feature on the internal diameter of the pipe likely due to the corrosion thinning of the pipe wall. The external corrosion was likely caused by disbonded coating and resultant sheilding of cathodic protection to the pipe. After the realease ili data was reexamined and an additional four (4) features with similar calls to that of the failed feature were excavated, investigated and determined the be within tool spec. Local areas of disbonded coating were also repaired at these locations.
Detailed record list
Report Received Date
2017-11-07 00:00:00
Iyear
2017
Report Number
20170357
Supplemental Number
30248
Report Type
Supplemental Final
Operator Id
Name
Inland Corporation
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-10-03 16:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
10
Recovered Bbls
1.2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2017-10-03 16:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-10-07 16:00:00
Restart Datetime
2017-10-13 12:21:00
On Site Datetime
2017-10-03 16:30:00
Nrc Rpt Datetime
2017-10-08 15:34:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
13201-10" Toledo-Fostoria-Tr10
Segment Name
13201-10"-Toledo-Fostoria-Tr10
Onshore State Abbreviation
Oh
Onshore Postal Code
43616
Onshore City Name
Oregon
Onshore County Name
Lucas
Designated Location
Survey Station No.
Designated Name
134+75
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
60
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10
Pipe Wall Thickness
0.25
Pipe Smys
46000
Pipe Specification
5l X46
Pipe Seam Type
Seamless
Pipe Manufacturer
National Tube
Pipe Coating Type
Coal Tar
Installation Year
1955
Manufactured Year
1955
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
Yes
Fish Aquatic Impact Ind
Yes
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Groundwater Contam Ind
Yes
Amount Released
0.2
Rel Water Name
Driftmeyer Ditch
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
8000
Est Cost Gas Released
2000
Est Cost Prop Damage
115000
Est Cost Emergency
864901
Est Cost Environmental
200000
Est Cost Other
15000
Est Cost Other Details
3rd Party Failure Analysis
Prpty
1204901
Accident Psig
954
Mop Psig
1200
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
39960
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Galvanic Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Metallurgical Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1955
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Cp Annual Survey Year
2017
Close Interval Survey Year
2015
Prior Damage
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2017
Geometry Recent Year
2017
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1969
Hydrtst Most Rcnt Pressure
1785
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
T*** G* N*******
Preparer Title
Sr. Manager-Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2018-04-29 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Sr. Manager-Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
On 10/3/2017 at 16:30, oregon, oh public works and fire chief notified local operator personnel of an odor complaint coming from the storm water sewers in the area. Between the dates of 10/3 and 10/8, operator personnel investigated the odor complaint. On 10/8/2017 at 14:33 operator verified a pin-hole leak in the 10" lima-toledo pipeline (line id 13201). After discovery of release, due to water impact, nrc was notified at 15:34 local time on 10/8 and report no. 1192655 was issued. Operator assessed adjacent pipeline near point of pinhole leak, cut out the section of failed piping and replaced with new piping. Required 48 hour update to nrc was made on 10/10/2017 and report no. 1192855 was issued. Failed pipe was sent to 3rd party laboratory for metallurgical analysis. Metallurgical analysis confirmed the cause of the failure as external corrosion pitting and thinning of the pipe wall. The failure was accompanied by a 1.5" linear feature on the internal diameter of the pipe likely due to the corrosion thinning of the pipe wall. The external corrosion was likely caused by disbonded coating and resultant sheilding of cathodic protection to the pipe. After the realease ili data was reexamined and an additional four (4) features with similar calls to that of the failed feature were excavated, investigated and determined the be within tool spec. Local areas of disbonded coating were also repaired at these locations.
Report Received Date 2017-11-07 00:00:00
Iyear 2017
Report Number 20170357
Supplemental Number 30248
Report Type Supplemental Final
Operator Id 32683 PHMSA Enforcement
Name Inland Corporation
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-10-03 16:30:00
Location Latitude 41.63756 Google Maps OpenStreetMap
Location Longitude -83.44773 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 10
Recovered Bbls 1.2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2017-10-03 16:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-10-07 16:00:00
Restart Datetime 2017-10-13 12:21:00
On Site Datetime 2017-10-03 16:30:00
Nrc Rpt Datetime 2017-10-08 15:34:00
Nrc Rpt Num 1192655 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name 13201-10" Toledo-Fostoria-Tr10
Segment Name 13201-10"-Toledo-Fostoria-Tr10
Onshore State Abbreviation Oh
Onshore Postal Code 43616
Onshore City Name Oregon
Onshore County Name Lucas
Designated Location Survey Station No.
Designated Name 134+75
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 60
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10
Pipe Wall Thickness 0.25
Pipe Smys 46000
Pipe Specification 5l X46
Pipe Seam Type Seamless
Pipe Manufacturer National Tube
Pipe Coating Type Coal Tar
Installation Year 1955
Manufactured Year 1955
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind Yes
Fish Aquatic Impact Ind Yes
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Surface Water Remed Ind Yes
Groundwater Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Groundwater Contam Ind Yes
Amount Released 0.2
Rel Water Name Driftmeyer Ditch
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 8000
Est Cost Gas Released 2000
Est Cost Prop Damage 115000
Est Cost Emergency 864901
Est Cost Environmental 200000
Est Cost Other 15000
Est Cost Other Details 3rd Party Failure Analysis
Prpty 1204901
Accident Psig 954
Mop Psig 1200
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 39960
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Galvanic Corrosion Ind Yes
Field Exam Basis Ind Yes
Metallurgical Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1955
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Close Interval Survey Ind Yes
Cp Annual Survey Year 2017
Close Interval Survey Year 2015
Prior Damage Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2017
Geometry Recent Year 2017
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1969
Hydrtst Most Rcnt Pressure 1785
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name T*** G* N*******
Preparer Title Sr. Manager-Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2018-04-29 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Sr. Manager-Dot Compliance
Authorizer Email T************@e*************.com
Narrative On 10/3/2017 at 16:30, oregon, oh public works and fire chief notified local operator personnel of an odor complaint coming from the storm water sewers in the area. Between the dates of 10/3 and 10/8, operator personnel investigated the odor complaint. On 10/8/2017 at 14:33 operator verified a pin-hole leak in the 10" lima-toledo pipeline (line id 13201). After discovery of release, due to water impact, nrc was notified at 15:34 local time on 10/8 and report no. 1192655 was issued. Operator assessed adjacent pipeline near point of pinhole leak, cut out the section of failed piping and replaced with new piping. Required 48 hour update to nrc was made on 10/10/2017 and report no. 1192855 was issued. Failed pipe was sent to 3rd party laboratory for metallurgical analysis. Metallurgical analysis confirmed the cause of the failure as external corrosion pitting and thinning of the pipe wall. The failure was accompanied by a 1.5" linear feature on the internal diameter of the pipe likely due to the corrosion thinning of the pipe wall. The external corrosion was likely caused by disbonded coating and resultant sheilding of cathodic protection to the pipe. After the realease ili data was reexamined and an additional four (4) features with similar calls to that of the failed feature were excavated, investigated and determined the be within tool spec. Local areas of disbonded coating were also repaired at these locations.

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