HL incident on 2017-09-28 — TX

Operator
Ascend Performance Materials Texas Inc
Cause
Corrosion Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$4,600,000
Incident datetime
2017-09-28 06:17
Report number
Location
TX
Narrative
Continuation: ascend engaged a pipeline integrity management services company with expertise in direct assessments, cathodic protection, corrosion engineering, and metallurgical analysis to help investigate the root cause of the subsurface pipeline leak. Ascend also utilized a leading materials testing laboratory to perform metallographic and fractographic examinations and chemical analyses of the pipeline segment. The segment was inspected in the field, excised for off-site examination at the materials testing laboratory, and thoroughly analyzed at the lab. Additional post-incident field work, including a close-interval survey, was also conducted in support of the root cause analysis. Based on the various field and laboratory analyses, the root cause of the subsurface pipeline leak was determined to be accelerated, localized, stray direct current-induced corrosion caused by cathodic protection (cp) system interference (cp interference) on the pipeline. The pipeline has a cp system designed to protect the pipeline from corrosion; however, a nearby, private third-party (non-DOT / rrc jurisdiction) installation was found to have been constructed in the area and that included a cp system for its own protection. A missing / broken connection was found on the third-party cp system. The connection failure resulted in excess cathodic potential for the connected portion of the third-party installation, and the excess cp interfered with the pipeline cp system.
Detailed record list
Report Received Date
2017-10-27 00:00:00
Iyear
2017
Report Number
20170351
Supplemental Number
30216
Report Type
Supplemental Final
Operator Id
Name
Ascend Performance Materials Texas Inc
Operator Street Address
1010 Travis Street Suite 900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-09-28 06:17:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Anhydrous Ammonia
Unintentional Release Bbls
1369.7
Intentional Release Bbls
54.36
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Notified By Ineos (Landowner)
Incident Identified Datetime
2017-09-28 06:17:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-09-28 08:25:00
Restart Datetime
2017-10-21 00:26:00
On Site Datetime
2017-09-28 07:03:00
Nrc Rpt Datetime
2017-09-28 09:24:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Manual
Num Pub Evacuated
7
Pipe Fac Name
Ascend Ammonia (Oyster Creek) Pipeline
Segment Name
Vs13 To Vs14
Onshore State Abbreviation
Tx
Onshore Postal Code
77541
Onshore City Name
Not Within A Municipality
Onshore County Name
Brazoria
Designated Location
Survey Station No.
Designated Name
269220
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
88
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10
Pipe Wall Thickness
0.25
Pipe Smys
42000
Pipe Specification
Api-5l X42
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Us Steel
Pipe Coating Type
Coal Tar
Installation Year
1976
Manufactured Year
1974
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
120000
Est Cost Prop Damage
4600000
Est Cost Emergency
6500000
Est Cost Environmental
4080000
Est Cost Other
0
Prpty
15300000
Accident Psig
240
Mop Psig
390
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
15326
Internal Inspection Ind
No
Other Restrictions Ind
Yes
Other Inspection Ind
Yes
Internal Inspection Details
Two Historical Ili Attempts, By The Previous Owner, Failed For Unknown Reasons. Approx. 800-Ft. Of Pipeline Was Inspected In Late-2017 From Vs13 To Vs13a In Conjunction With The Ongoing Leak Investigation, By Use Of A Tethered Mfl-Type Ili Tool, Prior To Returning The Segment To Normal Service.
Operation Complications Ind
Yes
Low Flow Ind
Yes
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak was very small pinhole, and was judged non-detectable via the cpm system measurements.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Stray Current Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Other Basis Ind
Yes
Corrosion Basis Details
Ascends Review Of Failure Lab Photos
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1976
Shielding Evident
No
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Other Cp Survey Ind
Yes
Cp Annual Survey Year
2016
Close Interval Survey Year
2015
Other Cp Survey Year
2015
Prior Damage
No
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Axial Recent Year
2017
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2004
Hydrtst Most Rcnt Pressure
500
Direct Asmnt Conducted
Yes, But The Point Of The Accident Was Not Identified As A Dig Site
Direct Asmnt Pnt Not Idntf Yr
2015
Non Destructive Exam Ind
No
Preparer Name
M*** H*****
Preparer Title
Materials And Corrosion Engineer
Preparer Email
M******@a**************.com
Preparer Telephone
281-228-4595
Prepared Date
2018-04-19 00:00:00
Authorizer Name
J***** M*****
Authorizer Telephone
281-228-4464
Authorizer Title
Operations Manager Distribution Manager
Authorizer Email
J*****@a**************.com
Narrative
Continuation: ascend engaged a pipeline integrity management services company with expertise in direct assessments, cathodic protection, corrosion engineering, and metallurgical analysis to help investigate the root cause of the subsurface pipeline leak. Ascend also utilized a leading materials testing laboratory to perform metallographic and fractographic examinations and chemical analyses of the pipeline segment. The segment was inspected in the field, excised for off-site examination at the materials testing laboratory, and thoroughly analyzed at the lab. Additional post-incident field work, including a close-interval survey, was also conducted in support of the root cause analysis. Based on the various field and laboratory analyses, the root cause of the subsurface pipeline leak was determined to be accelerated, localized, stray direct current-induced corrosion caused by cathodic protection (cp) system interference (cp interference) on the pipeline. The pipeline has a cp system designed to protect the pipeline from corrosion; however, a nearby, private third-party (non-DOT / rrc jurisdiction) installation was found to have been constructed in the area and that included a cp system for its own protection. A missing / broken connection was found on the third-party cp system. The connection failure resulted in excess cathodic potential for the connected portion of the third-party installation, and the excess cp interfered with the pipeline cp system.
Report Received Date 2017-10-27 00:00:00
Iyear 2017
Report Number 20170351
Supplemental Number 30216
Report Type Supplemental Final
Operator Id 31517 PHMSA Enforcement
Name Ascend Performance Materials Texas Inc
Operator Street Address 1010 Travis Street Suite 900
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-09-28 06:17:00
Location Latitude 29.06948 Google Maps OpenStreetMap
Location Longitude -95.33939 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Anhydrous Ammonia
Unintentional Release Bbls 1369.7
Intentional Release Bbls 54.36
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Notified By Ineos (Landowner)
Incident Identified Datetime 2017-09-28 06:17:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-09-28 08:25:00
Restart Datetime 2017-10-21 00:26:00
On Site Datetime 2017-09-28 07:03:00
Nrc Rpt Datetime 2017-09-28 09:24:00
Nrc Rpt Num 1191738 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Manual
Num Pub Evacuated 7
Pipe Fac Name Ascend Ammonia (Oyster Creek) Pipeline
Segment Name Vs13 To Vs14
Onshore State Abbreviation Tx
Onshore Postal Code 77541
Onshore City Name Not Within A Municipality
Onshore County Name Brazoria
Designated Location Survey Station No.
Designated Name 269220
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 88
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10
Pipe Wall Thickness 0.25
Pipe Smys 42000
Pipe Specification Api-5l X42
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Us Steel
Pipe Coating Type Coal Tar
Installation Year 1976
Manufactured Year 1974
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 120000
Est Cost Prop Damage 4600000
Est Cost Emergency 6500000
Est Cost Environmental 4080000
Est Cost Other 0
Prpty 15300000
Accident Psig 240
Mop Psig 390
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 15326
Internal Inspection Ind No
Other Restrictions Ind Yes
Other Inspection Ind Yes
Internal Inspection Details Two Historical Ili Attempts, By The Previous Owner, Failed For Unknown Reasons. Approx. 800-Ft. Of Pipeline Was Inspected In Late-2017 From Vs13 To Vs13a In Conjunction With The Ongoing Leak Investigation, By Use Of A Tethered Mfl-Type Ili Tool, Prior To Returning The Segment To Normal Service.
Operation Complications Ind Yes
Low Flow Ind Yes
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak was very small pinhole, and was judged non-detectable via the cpm system measurements.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Stray Current Corrosion Ind Yes
Field Exam Basis Ind Yes
Other Basis Ind Yes
Corrosion Basis Details Ascends Review Of Failure Lab Photos
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1976
Shielding Evident No
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Close Interval Survey Ind Yes
Other Cp Survey Ind Yes
Cp Annual Survey Year 2016
Close Interval Survey Year 2015
Other Cp Survey Year 2015
Prior Damage No
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Axial Recent Year 2017
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2004
Hydrtst Most Rcnt Pressure 500
Direct Asmnt Conducted Yes, But The Point Of The Accident Was Not Identified As A Dig Site
Direct Asmnt Pnt Not Idntf Yr 2015
Non Destructive Exam Ind No
Preparer Name M*** H*****
Preparer Title Materials And Corrosion Engineer
Preparer Email M******@a**************.com
Preparer Telephone 281-228-4595
Prepared Date 2018-04-19 00:00:00
Authorizer Name J***** M*****
Authorizer Telephone 281-228-4464
Authorizer Title Operations Manager Distribution Manager
Authorizer Email J*****@a**************.com
Narrative Continuation: ascend engaged a pipeline integrity management services company with expertise in direct assessments, cathodic protection, corrosion engineering, and metallurgical analysis to help investigate the root cause of the subsurface pipeline leak. Ascend also utilized a leading materials testing laboratory to perform metallographic and fractographic examinations and chemical analyses of the pipeline segment. The segment was inspected in the field, excised for off-site examination at the materials testing laboratory, and thoroughly analyzed at the lab. Additional post-incident field work, including a close-interval survey, was also conducted in support of the root cause analysis. Based on the various field and laboratory analyses, the root cause of the subsurface pipeline leak was determined to be accelerated, localized, stray direct current-induced corrosion caused by cathodic protection (cp) system interference (cp interference) on the pipeline. The pipeline has a cp system designed to protect the pipeline from corrosion; however, a nearby, private third-party (non-DOT / rrc jurisdiction) installation was found to have been constructed in the area and that included a cp system for its own protection. A missing / broken connection was found on the third-party cp system. The connection failure resulted in excess cathodic potential for the connected portion of the third-party installation, and the excess cp interfered with the pipeline cp system.

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