HL incident on 2017-09-23 — NJ

Operator
Torrance Valley Pipeline Company Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$35,000
Incident datetime
2017-09-23 09:45
Report number
Location
NJ
Narrative
Description of incident: while making scheduled remote pump station inspections the operator discovered what appeared to be a pump seal leak. With oil confined mostly to the pump containment pad and some overspray. Actions taken: shutdown and isolated the pump from a distance, stood up local incident command system with logistics personnel and made regulatory notifications per code of federal and state regulations performed clean up and remediation, completed 9/24 sent pump into manufacturer for failure analysis. Root cause determined to be gasket failure due to improper installation. It was installed at pump shop and was either damaged prior to install or installed improperly which damaged the gasket resulting in premature failure. .
Detailed record list
Report Received Date
2017-10-20 00:00:00
Iyear
2017
Report Number
20170344
Supplemental Number
22854
Report Type
Supplemental Final
Operator Id
Name
Torrance Valley Pipeline Company Llc
Operator Street Address
1 Sylvan Way 2nd Floor
Operator City Name
Parsippany
Operator State Abbreviation
NJ
Operator Postal Code
07054
Local Datetime
2017-09-23 09:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
11.21
Recovered Bbls
11.21
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-09-23 09:45:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Pipeline And Station Was Not Shutdown. The Pump Was Shutdown And Isolated.
On Site Datetime
2017-09-23 09:45:00
Nrc Rpt Datetime
2017-09-23 10:39:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lebec Station
Segment Name
Pump 3
Onshore State Abbreviation
Ca
Onshore Postal Code
93243
Onshore City Name
Lebec
Onshore County Name
Kern
Designated Location
Milepost/valve Station
Designated Name
Lebec Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pump
Installation Year
2017
Material Involved
Material Other Than Carbon Steel
Material Details
Case Gasket Failure
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
35000
Est Cost Emergency
7000
Est Cost Environmental
20000
Est Cost Other
0
Prpty
62000
Accident Psig
900
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Mechanical failure during normal operations
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Additional Defect Ind
Yes
Preparer Name
T***** S******
Preparer Title
Regulatory Advisor
Preparer Email
T*************@p********.com
Preparer Telephone
9496479921
Prepared Date
2017-12-01 00:00:00
Authorizer Name
H**** C******
Authorizer Telephone
2816024200
Authorizer Title
Senior Director Of Engineering - Logistics
Authorizer Email
H************@p********.com
Narrative
Description of incident: while making scheduled remote pump station inspections the operator discovered what appeared to be a pump seal leak. With oil confined mostly to the pump containment pad and some overspray. Actions taken: shutdown and isolated the pump from a distance, stood up local incident command system with logistics personnel and made regulatory notifications per code of federal and state regulations performed clean up and remediation, completed 9/24 sent pump into manufacturer for failure analysis. Root cause determined to be gasket failure due to improper installation. It was installed at pump shop and was either damaged prior to install or installed improperly which damaged the gasket resulting in premature failure. .
Report Received Date 2017-10-20 00:00:00
Iyear 2017
Report Number 20170344
Supplemental Number 22854
Report Type Supplemental Final
Operator Id 39534 PHMSA Enforcement
Name Torrance Valley Pipeline Company Llc
Operator Street Address 1 Sylvan Way 2nd Floor
Operator City Name Parsippany
Operator State Abbreviation NJ
Operator Postal Code 07054
Local Datetime 2017-09-23 09:45:00
Location Latitude 34.860589 Google Maps OpenStreetMap
Location Longitude -118.880706 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 11.21
Recovered Bbls 11.21
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-09-23 09:45:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Pipeline And Station Was Not Shutdown. The Pump Was Shutdown And Isolated.
On Site Datetime 2017-09-23 09:45:00
Nrc Rpt Datetime 2017-09-23 10:39:00
Nrc Rpt Num 1191292 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Lebec Station
Segment Name Pump 3
Onshore State Abbreviation Ca
Onshore Postal Code 93243
Onshore City Name Lebec
Onshore County Name Kern
Designated Location Milepost/valve Station
Designated Name Lebec Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pump
Installation Year 2017
Material Involved Material Other Than Carbon Steel
Material Details Case Gasket Failure
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 35000
Est Cost Emergency 7000
Est Cost Environmental 20000
Est Cost Other 0
Prpty 62000
Accident Psig 900
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Mechanical failure during normal operations
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Additional Defect Ind Yes
Preparer Name T***** S******
Preparer Title Regulatory Advisor
Preparer Email T*************@p********.com
Preparer Telephone 9496479921
Prepared Date 2017-12-01 00:00:00
Authorizer Name H**** C******
Authorizer Telephone 2816024200
Authorizer Title Senior Director Of Engineering - Logistics
Authorizer Email H************@p********.com
Narrative Description of incident: while making scheduled remote pump station inspections the operator discovered what appeared to be a pump seal leak. With oil confined mostly to the pump containment pad and some overspray. Actions taken: shutdown and isolated the pump from a distance, stood up local incident command system with logistics personnel and made regulatory notifications per code of federal and state regulations performed clean up and remediation, completed 9/24 sent pump into manufacturer for failure analysis. Root cause determined to be gasket failure due to improper installation. It was installed at pump shop and was either damaged prior to install or installed improperly which damaged the gasket resulting in premature failure. .

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