HL incident on 2017-10-04 — PA

Operator
Buckeye Partners, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2017-10-04 16:40
Report number
Location
PA
Narrative
On october 4th, 2017 at 1632, buckeye field operations received high and high/high lima station sump alarms. Local operations responded to the alarms and discovered the station sump overflowing. All pipeline activity in lima station was shut down. The source of the overflow was determined to be a partially open drain valve on the discharge side of a mainline pump, the valve was closed and affected area was assessed. All internal and external notifications were made. The volume is estimated to be 10 barrels of a gas/jet fuel mixture released onto company property. Local resources and osro responded to remediate the affected area.
Detailed record list
Report Received Date
2017-10-17 00:00:00
Iyear
2017
Report Number
20170338
Supplemental Number
22775
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2017-10-04 16:40:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
10
Recovered Bbls
10
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2017-10-04 16:40:00
System Part Involved
Onshore Equipment And Piping Associated With Belowground Storage
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-10-04 16:54:00
Restart Datetime
2017-10-05 00:04:00
On Site Datetime
2017-10-04 16:40:00
Nrc Rpt Datetime
2017-10-04 17:20:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lima Station
Segment Name
Terminal Sump Tank
Onshore State Abbreviation
Oh
Onshore Postal Code
45802
Onshore City Name
Lima
Onshore County Name
Allen
Designated Location
Milepost/valve Station
Designated Name
Lima Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Sump
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1000
Est Cost Prop Damage
0
Est Cost Emergency
40000
Est Cost Environmental
15000
Est Cost Other
0
Prpty
56000
Accident Psig
975
Mop Psig
1140
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
2
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Valve Misalignment
Related Failure Follow Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
G***** G*****
Preparer Title
Compliance Specialist
Preparer Email
G******@b******.com
Preparer Telephone
412-716-8250
Preparer Fax
412-264-1433
Prepared Date
2017-11-02 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
610-904-4113
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
On october 4th, 2017 at 1632, buckeye field operations received high and high/high lima station sump alarms. Local operations responded to the alarms and discovered the station sump overflowing. All pipeline activity in lima station was shut down. The source of the overflow was determined to be a partially open drain valve on the discharge side of a mainline pump, the valve was closed and affected area was assessed. All internal and external notifications were made. The volume is estimated to be 10 barrels of a gas/jet fuel mixture released onto company property. Local resources and osro responded to remediate the affected area.
Report Received Date 2017-10-17 00:00:00
Iyear 2017
Report Number 20170338
Supplemental Number 22775
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2017-10-04 16:40:00
Location Latitude 40.6972223 Google Maps OpenStreetMap
Location Longitude -84.1272224 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 10
Recovered Bbls 10
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2017-10-04 16:40:00
System Part Involved Onshore Equipment And Piping Associated With Belowground Storage
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-10-04 16:54:00
Restart Datetime 2017-10-05 00:04:00
On Site Datetime 2017-10-04 16:40:00
Nrc Rpt Datetime 2017-10-04 17:20:00
Nrc Rpt Num 1192304 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Lima Station
Segment Name Terminal Sump Tank
Onshore State Abbreviation Oh
Onshore Postal Code 45802
Onshore City Name Lima
Onshore County Name Allen
Designated Location Milepost/valve Station
Designated Name Lima Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Sump
Installation Year Unknown
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 1000
Est Cost Prop Damage 0
Est Cost Emergency 40000
Est Cost Environmental 15000
Est Cost Other 0
Prpty 56000
Accident Psig 975
Mop Psig 1140
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 2
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Valve Misalignment
Related Failure Follow Ind Yes
Category Type Normal Operating Conditions
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name G***** G*****
Preparer Title Compliance Specialist
Preparer Email G******@b******.com
Preparer Telephone 412-716-8250
Preparer Fax 412-264-1433
Prepared Date 2017-11-02 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 610-904-4113
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative On october 4th, 2017 at 1632, buckeye field operations received high and high/high lima station sump alarms. Local operations responded to the alarms and discovered the station sump overflowing. All pipeline activity in lima station was shut down. The source of the overflow was determined to be a partially open drain valve on the discharge side of a mainline pump, the valve was closed and affected area was assessed. All internal and external notifications were made. The volume is estimated to be 10 barrels of a gas/jet fuel mixture released onto company property. Local resources and osro responded to remediate the affected area.

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