HL incident on 2017-09-13 — OH

Operator
Marathon Pipe Line Llc
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$9,912
Incident datetime
2017-09-13 15:20
Report number
Location
OH
Narrative
On september 13, 2017, contract crews were on-site performing a project to remove a casing. While drilling through the casing, the contractor drilled a hole into the pipe, resulting in a release of liquid natural gasoline. Approximately six barrels were released into the excavation trench. All product was immediately cleaned up and repairs were made. The cause of this release was incorrect operations. As a result of this release, future casing removal projects were immediately suspended until procedures were improved. 2/8/18 update: part c, question 3a. - corrected the nominal diameter to 8 inches. Part c, question 6 - changed the type of accident involved from "other" to "leak".
Detailed record list
Report Received Date
2017-10-06 00:00:00
Iyear
2017
Report Number
20170331
Supplemental Number
23109
Report Type
Supplemental Final
Operator Id
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2017-09-13 15:20:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Other
Commodity Details
Liquid Natural Gasoline
Unintentional Release Bbls
6
Recovered Bbls
6
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2017-09-13 15:20:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-09-13 15:28:00
Restart Datetime
2017-09-14 06:25:00
On Site Datetime
2017-09-13 16:20:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Rio 8" Products
Segment Name
Speedway Rio - Clermont 8"
Onshore State Abbreviation
In
Onshore Postal Code
46234
Onshore City Name
Indianapolis
Onshore County Name
Marion
Designated Location
Milepost/valve Station
Designated Name
145.8
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
60
Crossing
Yes
Road Crossing Ind
Yes
Road Type
Cased
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8
Pipe Wall Thickness
0.277
Pipe Smys
35000
Pipe Specification
Api 5l
Pipe Seam Type
Seamless
Pipe Manufacturer
Unkown
Pipe Coating Type
Coal Tar
Installation Year
1952
Manufactured Year
1952
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Contractor Drilled Thru Pipe.
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
300
Est Cost Prop Damage
9912
Est Cost Emergency
27512
Est Cost Environmental
0
Est Cost Other
0
Prpty
37724
Accident Psig
700
Mop Psig
1491
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
45558
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
Yes
Num Contractors Tested
2
Num Contractors Failed
0
Cause
Incorrect Operation
Cause Details
Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Operation Type
Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Related Inadequate Proc Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
No
Preparer Name
D******* S***
Preparer Title
Hes Professional
Preparer Email
D*****@m****************.com
Preparer Telephone
419-421-2121
Prepared Date
2018-02-08 00:00:00
Authorizer Name
R****** W* B*****
Authorizer Telephone
419-421-2121
Authorizer Title
Regulatory And Compliance Supervisor
Authorizer Email
R*******@m****************.com
Narrative
On september 13, 2017, contract crews were on-site performing a project to remove a casing. While drilling through the casing, the contractor drilled a hole into the pipe, resulting in a release of liquid natural gasoline. Approximately six barrels were released into the excavation trench. All product was immediately cleaned up and repairs were made. The cause of this release was incorrect operations. As a result of this release, future casing removal projects were immediately suspended until procedures were improved. 2/8/18 update: part c, question 3a. - corrected the nominal diameter to 8 inches. Part c, question 6 - changed the type of accident involved from "other" to "leak".
Report Received Date 2017-10-06 00:00:00
Iyear 2017
Report Number 20170331
Supplemental Number 23109
Report Type Supplemental Final
Operator Id 32147 PHMSA Enforcement
Name Marathon Pipe Line Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2017-09-13 15:20:00
Location Latitude 39.798322 Google Maps OpenStreetMap
Location Longitude -86.322916 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Other
Commodity Details Liquid Natural Gasoline
Unintentional Release Bbls 6
Recovered Bbls 6
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2017-09-13 15:20:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-09-13 15:28:00
Restart Datetime 2017-09-14 06:25:00
On Site Datetime 2017-09-13 16:20:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Rio 8" Products
Segment Name Speedway Rio - Clermont 8"
Onshore State Abbreviation In
Onshore Postal Code 46234
Onshore City Name Indianapolis
Onshore County Name Marion
Designated Location Milepost/valve Station
Designated Name 145.8
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 60
Crossing Yes
Road Crossing Ind Yes
Road Type Cased
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8
Pipe Wall Thickness 0.277
Pipe Smys 35000
Pipe Specification Api 5l
Pipe Seam Type Seamless
Pipe Manufacturer Unkown
Pipe Coating Type Coal Tar
Installation Year 1952
Manufactured Year 1952
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Contractor Drilled Thru Pipe.
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 300
Est Cost Prop Damage 9912
Est Cost Emergency 27512
Est Cost Environmental 0
Est Cost Other 0
Prpty 37724
Accident Psig 700
Mop Psig 1491
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 45558
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind Yes
Num Contractors Tested 2
Num Contractors Failed 0
Cause Incorrect Operation
Cause Details Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Operation Type Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Related Inadequate Proc Ind Yes
Category Type Other Maintenance
Operator Qualification Ind No
Preparer Name D******* S***
Preparer Title Hes Professional
Preparer Email D*****@m****************.com
Preparer Telephone 419-421-2121
Prepared Date 2018-02-08 00:00:00
Authorizer Name R****** W* B*****
Authorizer Telephone 419-421-2121
Authorizer Title Regulatory And Compliance Supervisor
Authorizer Email R*******@m****************.com
Narrative On september 13, 2017, contract crews were on-site performing a project to remove a casing. While drilling through the casing, the contractor drilled a hole into the pipe, resulting in a release of liquid natural gasoline. Approximately six barrels were released into the excavation trench. All product was immediately cleaned up and repairs were made. The cause of this release was incorrect operations. As a result of this release, future casing removal projects were immediately suspended until procedures were improved. 2/8/18 update: part c, question 3a. - corrected the nominal diameter to 8 inches. Part c, question 6 - changed the type of accident involved from "other" to "leak".

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