HL incident on 2017-09-11 — TX

Operator
Energy Transfer Company
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2017-09-11 21:47
Report number
Location
TX
Narrative
On september 11, 2017 at approximately 21:47 hrs., energy transfer liquid control detected a loss in flow and increase of pressure on the rio bravo crude system in corpus christi, tx. Liquid control immediately shut in the pumps at mcmullen pump station at approximately 21:47 hrs. Thus shutting in the pipeline. Operations technician was dispatched to investigate and arrived on site at 22:40 hrs. The technician verified the spill at the ef-90 station and ensured the pipeline was shut in and the leak was stopped. It was discovered that approximately 35 gallons of crude was released at the ef-90 station. Environmental remediation crews were immediately dispatched to commence containment/clean up activities. Remediation of affected site and surrounding areas is ongoing and will be completed within 30 days. An investigation concluded that the leak occurred due to an improperly installed cap coming loose on a ralston fitting on an instrument test port. The pipeline was brought back into service at 8:30 hrs. On september 13, 2017. Local operations is removing instrument test ports and installing "bull plugs" in their area to prevent reoccurrence of this issue in the future. This pipeline is under the jurisdiction of the tx rrc as intrastate (system id 963373). This leak was telephonically reported to the tx rrc on 01:00 on september 12, 2017 a 48 hr. Nrc update was made on september 13, 2017 at 14:48 hrs. Incident report # 1190184 report updated on 10/18/17 report updated on 10/19/17
Detailed record list
Report Received Date
2017-10-06 00:00:00
Iyear
2017
Report Number
20170330
Supplemental Number
22741
Report Type
Supplemental Final
Operator Id
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-09-11 21:47:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.83
Recovered Bbls
0.83
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2017-09-11 21:47:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-09-11 21:47:00
Restart Datetime
2017-09-13 08:30:00
On Site Datetime
2017-09-11 22:40:00
Nrc Rpt Datetime
2017-09-11 23:59:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Rio Bravo Crude Pipeline
Segment Name
Ef-90 / Buckeye Terminal
Onshore State Abbreviation
Tx
Onshore Postal Code
78022-0000
Onshore City Name
Corpus Christi
Onshore County Name
Nueces
Designated Location
Survey Station No.
Designated Name
139+32.6
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Instrumentation
Installation Year
2014
Material Involved
Material Other Than Carbon Steel
Material Details
Brass Fitting(Ralston)
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
35
Est Cost Prop Damage
0
Est Cost Emergency
1000
Est Cost Environmental
30000
Est Cost Other
0
Prpty
31035
Accident Psig
861
Mop Psig
1000
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controllers actions were in accordance with energy transfer crm (control room management) procedures
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Additional Installation Ind
Yes
Preparer Name
C**** K*****
Preparer Title
Manager Of Intrastate Regulatory Compliance
Preparer Email
C***********@e*************.com
Preparer Telephone
713.989.7077
Preparer Fax
713.989.1122
Prepared Date
2017-10-19 00:00:00
Authorizer Name
D**** N******
Authorizer Telephone
713.989.7232
Authorizer Title
Director Of Regulatory Compliance
Authorizer Email
D************@e*************.com
Narrative
On september 11, 2017 at approximately 21:47 hrs., energy transfer liquid control detected a loss in flow and increase of pressure on the rio bravo crude system in corpus christi, tx. Liquid control immediately shut in the pumps at mcmullen pump station at approximately 21:47 hrs. Thus shutting in the pipeline. Operations technician was dispatched to investigate and arrived on site at 22:40 hrs. The technician verified the spill at the ef-90 station and ensured the pipeline was shut in and the leak was stopped. It was discovered that approximately 35 gallons of crude was released at the ef-90 station. Environmental remediation crews were immediately dispatched to commence containment/clean up activities. Remediation of affected site and surrounding areas is ongoing and will be completed within 30 days. An investigation concluded that the leak occurred due to an improperly installed cap coming loose on a ralston fitting on an instrument test port. The pipeline was brought back into service at 8:30 hrs. On september 13, 2017. Local operations is removing instrument test ports and installing "bull plugs" in their area to prevent reoccurrence of this issue in the future. This pipeline is under the jurisdiction of the tx rrc as intrastate (system id 963373). This leak was telephonically reported to the tx rrc on 01:00 on september 12, 2017 a 48 hr. Nrc update was made on september 13, 2017 at 14:48 hrs. Incident report # 1190184 report updated on 10/18/17 report updated on 10/19/17
Report Received Date 2017-10-06 00:00:00
Iyear 2017
Report Number 20170330
Supplemental Number 22741
Report Type Supplemental Final
Operator Id 32099 PHMSA Enforcement
Name Energy Transfer Company
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-09-11 21:47:00
Location Latitude 27.8125 Google Maps OpenStreetMap
Location Longitude -97.5036 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.83
Recovered Bbls 0.83
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2017-09-11 21:47:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-09-11 21:47:00
Restart Datetime 2017-09-13 08:30:00
On Site Datetime 2017-09-11 22:40:00
Nrc Rpt Datetime 2017-09-11 23:59:00
Nrc Rpt Num 1189978 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Rio Bravo Crude Pipeline
Segment Name Ef-90 / Buckeye Terminal
Onshore State Abbreviation Tx
Onshore Postal Code 78022-0000
Onshore City Name Corpus Christi
Onshore County Name Nueces
Designated Location Survey Station No.
Designated Name 139+32.6
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Instrumentation
Installation Year 2014
Material Involved Material Other Than Carbon Steel
Material Details Brass Fitting(Ralston)
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 35
Est Cost Prop Damage 0
Est Cost Emergency 1000
Est Cost Environmental 30000
Est Cost Other 0
Prpty 31035
Accident Psig 861
Mop Psig 1000
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind Yes
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controllers actions were in accordance with energy transfer crm (control room management) procedures
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Equipment Failure
Cause Details Defective Or Loose Tubing Or Fitting
Eq Failure Type Defective Or Loose Tubing Or Fitting
Additional Installation Ind Yes
Preparer Name C**** K*****
Preparer Title Manager Of Intrastate Regulatory Compliance
Preparer Email C***********@e*************.com
Preparer Telephone 713.989.7077
Preparer Fax 713.989.1122
Prepared Date 2017-10-19 00:00:00
Authorizer Name D**** N******
Authorizer Telephone 713.989.7232
Authorizer Title Director Of Regulatory Compliance
Authorizer Email D************@e*************.com
Narrative On september 11, 2017 at approximately 21:47 hrs., energy transfer liquid control detected a loss in flow and increase of pressure on the rio bravo crude system in corpus christi, tx. Liquid control immediately shut in the pumps at mcmullen pump station at approximately 21:47 hrs. Thus shutting in the pipeline. Operations technician was dispatched to investigate and arrived on site at 22:40 hrs. The technician verified the spill at the ef-90 station and ensured the pipeline was shut in and the leak was stopped. It was discovered that approximately 35 gallons of crude was released at the ef-90 station. Environmental remediation crews were immediately dispatched to commence containment/clean up activities. Remediation of affected site and surrounding areas is ongoing and will be completed within 30 days. An investigation concluded that the leak occurred due to an improperly installed cap coming loose on a ralston fitting on an instrument test port. The pipeline was brought back into service at 8:30 hrs. On september 13, 2017. Local operations is removing instrument test ports and installing "bull plugs" in their area to prevent reoccurrence of this issue in the future. This pipeline is under the jurisdiction of the tx rrc as intrastate (system id 963373). This leak was telephonically reported to the tx rrc on 01:00 on september 12, 2017 a 48 hr. Nrc update was made on september 13, 2017 at 14:48 hrs. Incident report # 1190184 report updated on 10/18/17 report updated on 10/19/17

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