HL incident on 2017-09-05 — OK

Operator
Magellan Ammonia Pipeline, L.p.
Cause
Material Failure Of Pipe Or Weld
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$4,000
Incident datetime
2017-09-05 13:30
Report number
Location
OK
Narrative
Local technician received notification from a third party regarding a potential dead spot in a farm field. Upon investigation from magellan employee, an area of dead vegetation was observed with an anhydrous ammonia odor. The investigation event was initiated at 13:30. The pipeline was not active at the time of event. The technician closed the manual valves at mp 226 and 217.5. Upon excavation of the pipe, the release was determined to be a pinhole in the longitudinal seam. A plidco clamp was bolted to the pipe to stop the release and was subsequently welded to make the repair permanent. Approximately 44 cubic yards of affected soil was removed
Detailed record list
Report Received Date
2017-10-04 00:00:00
Iyear
2017
Report Number
20170325
Supplemental Number
22708
Report Type
Original Final
Operator Id
Name
Magellan Ammonia Pipeline, L.p.
Operator Street Address
One Williams Center, Otc-9 P.o. Box 22186
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74172
Local Datetime
2017-09-05 13:30:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Anhydrous Ammonia
Unintentional Release Bbls
44
Intentional Release Bbls
0
Recovered Bbls
44
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2017-09-05 13:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Shut Down Prior To The Time Of The Incident
On Site Datetime
2017-09-05 13:30:00
Nrc Rpt Datetime
2017-09-05 14:10:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Nh3 Garner Lateral 6'
Segment Name
Line Id 510
Onshore State Abbreviation
Mn
Onshore Postal Code
56034
Onshore City Name
Not Within A Municipality
Onshore County Name
Blue Earth
Designated Location
Milepost/valve Station
Designated Name
225.3
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
6.625
Pipe Wall Thickness
0.156
Pipe Smys
46000
Pipe Specification
Api5lx 46
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Republic Steel
Pipe Coating Type
Polyolefin
Installation Year
1978
Manufactured Year
1978
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
5000
Est Cost Gas Released
1640
Est Cost Prop Damage
4000
Est Cost Emergency
25000
Est Cost Environmental
0
Est Cost Other
0
Prpty
35640
Accident Psig
322
Mop Psig
1152
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
45201
Internal Inspection Ind
Yes
Operation Complications Ind
Yes
Incompat Commod Ind
Yes
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
There were no scada indications of a release, and the line was down at the time of the report.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Field Exam Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor
Yes
Other Factor Details
None
Pwf Additional Other Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2017
Geometry Recent Year
2016
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2011
Hydrtst Most Rcnt Pressure
1966
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
9185747327
Preparer Fax
9185747376
Prepared Date
2017-10-04 00:00:00
Authorizer Name
S****** L******
Authorizer Telephone
9185747327
Authorizer Title
Ai Analyst
Authorizer Email
S**************@m*********.com
Narrative
Local technician received notification from a third party regarding a potential dead spot in a farm field. Upon investigation from magellan employee, an area of dead vegetation was observed with an anhydrous ammonia odor. The investigation event was initiated at 13:30. The pipeline was not active at the time of event. The technician closed the manual valves at mp 226 and 217.5. Upon excavation of the pipe, the release was determined to be a pinhole in the longitudinal seam. A plidco clamp was bolted to the pipe to stop the release and was subsequently welded to make the repair permanent. Approximately 44 cubic yards of affected soil was removed
Report Received Date 2017-10-04 00:00:00
Iyear 2017
Report Number 20170325
Supplemental Number 22708
Report Type Original Final
Operator Id 12105 PHMSA Enforcement
Name Magellan Ammonia Pipeline, L.p.
Operator Street Address One Williams Center, Otc-9 P.o. Box 22186
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74172
Local Datetime 2017-09-05 13:30:00
Location Latitude 43.931441 Google Maps OpenStreetMap
Location Longitude -94.113196 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Anhydrous Ammonia
Unintentional Release Bbls 44
Intentional Release Bbls 0
Recovered Bbls 44
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2017-09-05 13:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Was Shut Down Prior To The Time Of The Incident
On Site Datetime 2017-09-05 13:30:00
Nrc Rpt Datetime 2017-09-05 14:10:00
Nrc Rpt Num 1189436 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Nh3 Garner Lateral 6'
Segment Name Line Id 510
Onshore State Abbreviation Mn
Onshore Postal Code 56034
Onshore City Name Not Within A Municipality
Onshore County Name Blue Earth
Designated Location Milepost/valve Station
Designated Name 225.3
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 6.625
Pipe Wall Thickness 0.156
Pipe Smys 46000
Pipe Specification Api5lx 46
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Republic Steel
Pipe Coating Type Polyolefin
Installation Year 1978
Manufactured Year 1978
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 5000
Est Cost Gas Released 1640
Est Cost Prop Damage 4000
Est Cost Emergency 25000
Est Cost Environmental 0
Est Cost Other 0
Prpty 35640
Accident Psig 322
Mop Psig 1152
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 45201
Internal Inspection Ind Yes
Operation Complications Ind Yes
Incompat Commod Ind Yes
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details There were no scada indications of a release, and the line was down at the time of the report.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Field Exam Ind Yes
Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor Yes
Other Factor Details None
Pwf Additional Other Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2017
Geometry Recent Year 2016
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2011
Hydrtst Most Rcnt Pressure 1966
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name S****** L******
Preparer Title Ai Analyst
Preparer Email S**************@m*********.com
Preparer Telephone 9185747327
Preparer Fax 9185747376
Prepared Date 2017-10-04 00:00:00
Authorizer Name S****** L******
Authorizer Telephone 9185747327
Authorizer Title Ai Analyst
Authorizer Email S**************@m*********.com
Narrative Local technician received notification from a third party regarding a potential dead spot in a farm field. Upon investigation from magellan employee, an area of dead vegetation was observed with an anhydrous ammonia odor. The investigation event was initiated at 13:30. The pipeline was not active at the time of event. The technician closed the manual valves at mp 226 and 217.5. Upon excavation of the pipe, the release was determined to be a pinhole in the longitudinal seam. A plidco clamp was bolted to the pipe to stop the release and was subsequently welded to make the repair permanent. Approximately 44 cubic yards of affected soil was removed

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