HL incident on 2017-09-03 — TX

Operator
Kinder Morgan Liquid Terminals, Llc
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2017-09-03 11:00
Report number
Location
TX
Narrative
Incident occurred during hurricane harvey. The actuator was being taken out during the recovery. Maintenance was removing the actuator from the valve in explorer pit 2 with a cherry picker. Once the actuator disconnected from the motor it swung due to the sudden imbalance and struck the nearby tubing on the plug valve. The line was immediately cleared of product and the leaked product was recovered by the vacuum truck. The damaged tubing was repaired and the line was back in service that night. 9/28/2017 - report opened in error - no changes made - d. Stephens
Detailed record list
Report Received Date
2017-09-26 00:00:00
Iyear
2017
Report Number
20170305
Supplemental Number
22691
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Liquid Terminals, Llc
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-09-03 11:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-09-03 11:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-09-03 11:00:00
Restart Datetime
2017-09-03 23:00:00
On Site Datetime
2017-09-03 11:05:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
28" Explorer
Segment Name
Pit 2
Onshore State Abbreviation
Tx
Onshore Postal Code
77502
Onshore City Name
Pasadena
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Plug
Valve Manufacturer
M And J Wedge Gate.
Installation Year
2000
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
185
Est Cost Prop Damage
500
Est Cost Emergency
1500
Est Cost Environmental
0
Est Cost Other
0
Prpty
2185
Accident Psig
5
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
No
Scada Functional Ind
No
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Immediately after hurricane harvey scada was not operational
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Operation Type
Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Related Other Ind
Yes
Operation Related Details
Disconnect Of Actuator From The Motor Caused An Imbalance Which Swung The Actuator Into The Tubing On The Nearby Plug Valve.
Category Type
Other Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
D******* S*******
Preparer Title
Director Compliance Codes And Standards
Preparer Email
D****************@k***********.com
Preparer Telephone
7137250147
Preparer Fax
303.984.3048
Prepared Date
2017-09-28 00:00:00
Authorizer Name
D******* S*******
Authorizer Telephone
713.725.0147
Authorizer Title
Director Compliance Codes And Standards
Authorizer Email
D****************@k***********.com
Narrative
Incident occurred during hurricane harvey. The actuator was being taken out during the recovery. Maintenance was removing the actuator from the valve in explorer pit 2 with a cherry picker. Once the actuator disconnected from the motor it swung due to the sudden imbalance and struck the nearby tubing on the plug valve. The line was immediately cleared of product and the leaked product was recovered by the vacuum truck. The damaged tubing was repaired and the line was back in service that night. 9/28/2017 - report opened in error - no changes made - d. Stephens
Report Received Date 2017-09-26 00:00:00
Iyear 2017
Report Number 20170305
Supplemental Number 22691
Report Type Supplemental Final
Operator Id 26041 PHMSA Enforcement
Name Kinder Morgan Liquid Terminals, Llc
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-09-03 11:00:00
Location Latitude 29.73093 Google Maps OpenStreetMap
Location Longitude -95.20397 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-09-03 11:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-09-03 11:00:00
Restart Datetime 2017-09-03 23:00:00
On Site Datetime 2017-09-03 11:05:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name 28" Explorer
Segment Name Pit 2
Onshore State Abbreviation Tx
Onshore Postal Code 77502
Onshore City Name Pasadena
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Plug
Valve Manufacturer M And J Wedge Gate.
Installation Year 2000
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 185
Est Cost Prop Damage 500
Est Cost Emergency 1500
Est Cost Environmental 0
Est Cost Other 0
Prpty 2185
Accident Psig 5
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind No
Scada Functional Ind No
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Immediately after hurricane harvey scada was not operational
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Operation Type Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Related Other Ind Yes
Operation Related Details Disconnect Of Actuator From The Motor Caused An Imbalance Which Swung The Actuator Into The Tubing On The Nearby Plug Valve.
Category Type Other Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name D******* S*******
Preparer Title Director Compliance Codes And Standards
Preparer Email D****************@k***********.com
Preparer Telephone 7137250147
Preparer Fax 303.984.3048
Prepared Date 2017-09-28 00:00:00
Authorizer Name D******* S*******
Authorizer Telephone 713.725.0147
Authorizer Title Director Compliance Codes And Standards
Authorizer Email D****************@k***********.com
Narrative Incident occurred during hurricane harvey. The actuator was being taken out during the recovery. Maintenance was removing the actuator from the valve in explorer pit 2 with a cherry picker. Once the actuator disconnected from the motor it swung due to the sudden imbalance and struck the nearby tubing on the plug valve. The line was immediately cleared of product and the leaked product was recovered by the vacuum truck. The damaged tubing was repaired and the line was back in service that night. 9/28/2017 - report opened in error - no changes made - d. Stephens

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