HL incident on 2017-08-23 — TX

Operator
Phillips 66 Pipeline Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2017-08-23 18:15
Report number
Location
TX
Narrative
During a station checkout due to a callout, p66 pipeliner discovered the air conditioner in the control building at cr-02 westlake meter station had failed resulting in plc equipment fault due to the high temperature environment. In coordination with p66 technician and control center, the pipeliner initiated a station reset. The plc reset resulted in the meter backpressure control valve to close and subsequent hi/hi discharge pressure shutdown at the origination station. The meter station pressure did not exceed mop, however subsequent investigation found evidence of damage due to over-torqueing of the non-metallic paper flange gasket. Actions taken to prevent re-occurrence: 1. A temperature monitor with hi temp level alarm to control center was added to the meter station building to provide early warning of possible air conditioner failure that could have adverse effect on control equipment. 2. Phillips 66 pipeliners were re-qualified on oq for proper torqueing procedures. 3. The local workgroup conducted re-training on procedures for proper torqueing of flanged pipe joints and proper gasket selection 4. The failed gasket was replaced with the company preferred spiral wound metallic gasket and properly torqued by qualified individuals. 5. The similar origination station strainer gasket was replaced verified to be properly torqued (no evidence of over-torqueing found) 6. Control center modified operating procedures to shut down the pipeline system in the event of a plc communication failure.
Detailed record list
Report Received Date
2017-09-22 00:00:00
Iyear
2017
Report Number
20170301
Supplemental Number
22665
Report Type
Supplemental Final
Operator Id
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2017-08-23 18:15:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
6.6
Recovered Bbls
6.6
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-08-23 18:15:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-08-23 18:20:00
Restart Datetime
2017-08-24 21:30:00
On Site Datetime
2017-08-23 18:45:00
Nrc Rpt Datetime
2017-08-23 19:15:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cr-02 - Westlake Meter Station
Segment Name
Clifton Ridge To Lake Charles Refinery
Onshore State Abbreviation
La
Onshore Postal Code
70669
Onshore City Name
Westlake
Onshore County Name
Calcasieu
Designated Location
Milepost/valve Station
Designated Name
Meter Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
2016
Material Involved
Material Other Than Carbon Steel
Material Details
Composite "paper" Gasket
Release Type
Leak
Leak Type
Other
Leak Type Other
Strainer Lid Flange Gasket
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
1
Rel Water Name
Bayou Verdine
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
350
Est Cost Prop Damage
5000
Est Cost Emergency
125000
Est Cost Environmental
2500
Est Cost Other
5000
Est Cost Other Details
Cost Of Response. Cleanup, Repair, And Disposal Of Contaminated Soil And Boom.
Prpty
137850
Accident Psig
524
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Incorrect Procedure Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
J*** S*****
Preparer Title
Dot Coordinator
Preparer Email
J************@p**.com
Preparer Telephone
832-765-1858
Prepared Date
2017-09-22 00:00:00
Authorizer Name
T*** F****
Authorizer Telephone
832-765-1632
Authorizer Title
Director Dot Compliance
Authorizer Email
M***********@p**.com
Narrative
During a station checkout due to a callout, p66 pipeliner discovered the air conditioner in the control building at cr-02 westlake meter station had failed resulting in plc equipment fault due to the high temperature environment. In coordination with p66 technician and control center, the pipeliner initiated a station reset. The plc reset resulted in the meter backpressure control valve to close and subsequent hi/hi discharge pressure shutdown at the origination station. The meter station pressure did not exceed mop, however subsequent investigation found evidence of damage due to over-torqueing of the non-metallic paper flange gasket. Actions taken to prevent re-occurrence: 1. A temperature monitor with hi temp level alarm to control center was added to the meter station building to provide early warning of possible air conditioner failure that could have adverse effect on control equipment. 2. Phillips 66 pipeliners were re-qualified on oq for proper torqueing procedures. 3. The local workgroup conducted re-training on procedures for proper torqueing of flanged pipe joints and proper gasket selection 4. The failed gasket was replaced with the company preferred spiral wound metallic gasket and properly torqued by qualified individuals. 5. The similar origination station strainer gasket was replaced verified to be properly torqued (no evidence of over-torqueing found) 6. Control center modified operating procedures to shut down the pipeline system in the event of a plc communication failure.
Report Received Date 2017-09-22 00:00:00
Iyear 2017
Report Number 20170301
Supplemental Number 22665
Report Type Supplemental Final
Operator Id 31684 PHMSA Enforcement
Name Phillips 66 Pipeline Llc
Operator Street Address 2331 Citywest Blvd
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2017-08-23 18:15:00
Location Latitude 30.239249 Google Maps OpenStreetMap
Location Longitude -93.290104 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 6.6
Recovered Bbls 6.6
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-08-23 18:15:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-08-23 18:20:00
Restart Datetime 2017-08-24 21:30:00
On Site Datetime 2017-08-23 18:45:00
Nrc Rpt Datetime 2017-08-23 19:15:00
Nrc Rpt Num 1188206 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cr-02 - Westlake Meter Station
Segment Name Clifton Ridge To Lake Charles Refinery
Onshore State Abbreviation La
Onshore Postal Code 70669
Onshore City Name Westlake
Onshore County Name Calcasieu
Designated Location Milepost/valve Station
Designated Name Meter Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 2016
Material Involved Material Other Than Carbon Steel
Material Details Composite "paper" Gasket
Release Type Leak
Leak Type Other
Leak Type Other Strainer Lid Flange Gasket
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 1
Rel Water Name Bayou Verdine
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 350
Est Cost Prop Damage 5000
Est Cost Emergency 125000
Est Cost Environmental 2500
Est Cost Other 5000
Est Cost Other Details Cost Of Response. Cleanup, Repair, And Disposal Of Contaminated Soil And Boom.
Prpty 137850
Accident Psig 524
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Incorrect Procedure Ind Yes
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name J*** S*****
Preparer Title Dot Coordinator
Preparer Email J************@p**.com
Preparer Telephone 832-765-1858
Prepared Date 2017-09-22 00:00:00
Authorizer Name T*** F****
Authorizer Telephone 832-765-1632
Authorizer Title Director Dot Compliance
Authorizer Email M***********@p**.com
Narrative During a station checkout due to a callout, p66 pipeliner discovered the air conditioner in the control building at cr-02 westlake meter station had failed resulting in plc equipment fault due to the high temperature environment. In coordination with p66 technician and control center, the pipeliner initiated a station reset. The plc reset resulted in the meter backpressure control valve to close and subsequent hi/hi discharge pressure shutdown at the origination station. The meter station pressure did not exceed mop, however subsequent investigation found evidence of damage due to over-torqueing of the non-metallic paper flange gasket. Actions taken to prevent re-occurrence: 1. A temperature monitor with hi temp level alarm to control center was added to the meter station building to provide early warning of possible air conditioner failure that could have adverse effect on control equipment. 2. Phillips 66 pipeliners were re-qualified on oq for proper torqueing procedures. 3. The local workgroup conducted re-training on procedures for proper torqueing of flanged pipe joints and proper gasket selection 4. The failed gasket was replaced with the company preferred spiral wound metallic gasket and properly torqued by qualified individuals. 5. The similar origination station strainer gasket was replaced verified to be properly torqued (no evidence of over-torqueing found) 6. Control center modified operating procedures to shut down the pipeline system in the event of a plc communication failure.

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