HL incident on 2017-08-25 — TX

Operator
Nustar Permian Transportation And Storage, Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2017-08-25 04:16
Report number
Location
TX
Narrative
A stainless-steel tubing, providing thermal relief around an isolation valve on surge relief piping, failed at a connection. The tubing has been removed from service, and will be sent to a lab for analysis. Update - the failure occurred due to high cycle fatigue. Cracking initiated in a groove on the outside diameter of the tubing, created by the compression fitting back ferrule biting into the tubing wall.
Detailed record list
Report Received Date
2017-09-22 00:00:00
Iyear
2017
Report Number
20170298
Supplemental Number
23142
Report Type
Supplemental Final
Operator Id
Name
Nustar Permian Transportation And Storage, Llc
Operator Street Address
8111 Westchester Drive
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75225
Local Datetime
2017-08-25 04:16:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
29.05
Recovered Bbls
29.05
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2017-08-25 04:16:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-08-25 04:16:00
Restart Datetime
2017-08-25 07:19:00
On Site Datetime
2017-08-25 04:45:00
Nrc Rpt Datetime
2017-08-25 05:54:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
100p Trunkline Pipeline
Segment Name
Colorado City Terminal
Onshore State Abbreviation
Tx
Onshore Postal Code
79526
Onshore City Name
Not Within A Municipality
Onshore County Name
Scurry
Designated Location
Milepost/valve Station
Designated Name
214134
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tubing
Installation Year
2016
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel Tubing
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1429
Est Cost Prop Damage
0
Est Cost Emergency
21667
Est Cost Environmental
0
Est Cost Other
1000
Est Cost Other Details
Laboratory Costs
Prpty
24096
Accident Psig
171
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Neither controller actions nor control room issues contributed to the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Eq Additional Other Ind
Yes
Eq Additional Other Details
High Cycle Fatigue
Preparer Name
R****** P****
Preparer Title
Pipeline Safety Supervisor
Preparer Email
R************@n***********.com
Preparer Telephone
3612499417
Preparer Fax
2109187117
Prepared Date
2018-02-15 00:00:00
Authorizer Name
W** G***
Authorizer Telephone
3612499402
Authorizer Title
Vice President And General Manager
Authorizer Email
W*******@n***********.com
Narrative
A stainless-steel tubing, providing thermal relief around an isolation valve on surge relief piping, failed at a connection. The tubing has been removed from service, and will be sent to a lab for analysis. Update - the failure occurred due to high cycle fatigue. Cracking initiated in a groove on the outside diameter of the tubing, created by the compression fitting back ferrule biting into the tubing wall.
Report Received Date 2017-09-22 00:00:00
Iyear 2017
Report Number 20170298
Supplemental Number 23142
Report Type Supplemental Final
Operator Id 39348 PHMSA Enforcement
Name Nustar Permian Transportation And Storage, Llc
Operator Street Address 8111 Westchester Drive
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75225
Local Datetime 2017-08-25 04:16:00
Location Latitude 32.52912 Google Maps OpenStreetMap
Location Longitude -100.85401 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 29.05
Recovered Bbls 29.05
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2017-08-25 04:16:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-08-25 04:16:00
Restart Datetime 2017-08-25 07:19:00
On Site Datetime 2017-08-25 04:45:00
Nrc Rpt Datetime 2017-08-25 05:54:00
Nrc Rpt Num 1188323 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name 100p Trunkline Pipeline
Segment Name Colorado City Terminal
Onshore State Abbreviation Tx
Onshore Postal Code 79526
Onshore City Name Not Within A Municipality
Onshore County Name Scurry
Designated Location Milepost/valve Station
Designated Name 214134
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Tubing
Installation Year 2016
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel Tubing
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1429
Est Cost Prop Damage 0
Est Cost Emergency 21667
Est Cost Environmental 0
Est Cost Other 1000
Est Cost Other Details Laboratory Costs
Prpty 24096
Accident Psig 171
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Neither controller actions nor control room issues contributed to the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Defective Or Loose Tubing Or Fitting
Eq Failure Type Defective Or Loose Tubing Or Fitting
Eq Additional Other Ind Yes
Eq Additional Other Details High Cycle Fatigue
Preparer Name R****** P****
Preparer Title Pipeline Safety Supervisor
Preparer Email R************@n***********.com
Preparer Telephone 3612499417
Preparer Fax 2109187117
Prepared Date 2018-02-15 00:00:00
Authorizer Name W** G***
Authorizer Telephone 3612499402
Authorizer Title Vice President And General Manager
Authorizer Email W*******@n***********.com
Narrative A stainless-steel tubing, providing thermal relief around an isolation valve on surge relief piping, failed at a connection. The tubing has been removed from service, and will be sent to a lab for analysis. Update - the failure occurred due to high cycle fatigue. Cracking initiated in a groove on the outside diameter of the tubing, created by the compression fitting back ferrule biting into the tubing wall.

All rights reserved. Copyright © by ClearPHMSA