HL incident on 2017-09-05 — TX

Operator
Dcp Midstream
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000
Incident datetime
2017-09-05 09:15
Report number
Location
TX
Narrative
Valve body bleeder connection (underground) was found to be loose to the point of leaking slightly after 49 years in service. No specific root cause was identified. Fitting showed no signs of damage, corrosion, or unusual wear. Fitting was replaced as a pre-cautionary measure.
Detailed record list
Report Received Date
2017-09-14 00:00:00
Iyear
2017
Report Number
20170289
Supplemental Number
22640
Report Type
Original Final
Operator Id
Name
Dcp Midstream
Operator Street Address
2331 Citywest Blvd. Hq-08-S812-02
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2017-09-05 20:12:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.4
Intentional Release Bbls
0.4
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2017-09-05 09:15:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Shutdown Of Pipeline Was Not Necessary. Leak Was On Valve Body Vent Fitting.
On Site Datetime
2017-09-05 17:00:00
Nrc Rpt Datetime
2017-09-05 20:26:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Blacklake Ngl System
Segment Name
Blk-1
Onshore State Abbreviation
Tx
Onshore Postal Code
75932
Onshore City Name
Not Within A Municipality
Onshore County Name
Newton
Designated Location
Survey Station No.
Designated Name
433569
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
30
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
M&j
Installation Year
1968
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
25
Est Cost Prop Damage
1000
Est Cost Emergency
12000
Est Cost Environmental
0
Est Cost Other
0
Prpty
13025
Accident Psig
1180
Mop Psig
1641
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
1
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak so minor control center could not be expected to detect an issue.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Threaded Fitting
Eq Additional Other Ind
Yes
Eq Additional Other Details
Tubing Connection Was Found Loose.
Preparer Name
R****** T* S****
Preparer Title
Senior Pipeline Compliance Specialist
Preparer Email
R******@d***********.com
Preparer Telephone
979-242-6913
Prepared Date
2017-09-14 00:00:00
Authorizer Name
B*** S********
Authorizer Telephone
713-268-7491
Authorizer Title
Operations Supervisor
Authorizer Email
N**********@d***********.com
Narrative
Valve body bleeder connection (underground) was found to be loose to the point of leaking slightly after 49 years in service. No specific root cause was identified. Fitting showed no signs of damage, corrosion, or unusual wear. Fitting was replaced as a pre-cautionary measure.
Report Received Date 2017-09-14 00:00:00
Iyear 2017
Report Number 20170289
Supplemental Number 22640
Report Type Original Final
Operator Id 31130 PHMSA Enforcement
Name Dcp Midstream
Operator Street Address 2331 Citywest Blvd. Hq-08-S812-02
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2017-09-05 20:12:00
Location Latitude 30.98035 Google Maps OpenStreetMap
Location Longitude -93.714949 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 0.4
Intentional Release Bbls 0.4
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2017-09-05 09:15:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Shutdown Of Pipeline Was Not Necessary. Leak Was On Valve Body Vent Fitting.
On Site Datetime 2017-09-05 17:00:00
Nrc Rpt Datetime 2017-09-05 20:26:00
Nrc Rpt Num 1189486 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Blacklake Ngl System
Segment Name Blk-1
Onshore State Abbreviation Tx
Onshore Postal Code 75932
Onshore City Name Not Within A Municipality
Onshore County Name Newton
Designated Location Survey Station No.
Designated Name 433569
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 30
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer M&j
Installation Year 1968
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 25
Est Cost Prop Damage 1000
Est Cost Emergency 12000
Est Cost Environmental 0
Est Cost Other 0
Prpty 13025
Accident Psig 1180
Mop Psig 1641
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 1
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak so minor control center could not be expected to detect an issue.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Threaded Fitting
Eq Additional Other Ind Yes
Eq Additional Other Details Tubing Connection Was Found Loose.
Preparer Name R****** T* S****
Preparer Title Senior Pipeline Compliance Specialist
Preparer Email R******@d***********.com
Preparer Telephone 979-242-6913
Prepared Date 2017-09-14 00:00:00
Authorizer Name B*** S********
Authorizer Telephone 713-268-7491
Authorizer Title Operations Supervisor
Authorizer Email N**********@d***********.com
Narrative Valve body bleeder connection (underground) was found to be loose to the point of leaking slightly after 49 years in service. No specific root cause was identified. Fitting showed no signs of damage, corrosion, or unusual wear. Fitting was replaced as a pre-cautionary measure.

All rights reserved. Copyright © by ClearPHMSA