HL incident on 2017-08-15 — KS

Operator
Koch Pipeline Company, L.p.
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2017-08-15 14:15
Report number
Location
KS
Narrative
On august 15, 2017, koch pipeline company's contractor, tdw, was performing a hot tap on the inv-orange 4" segment line in orange county, texas. Once the weld was made on the tor, koch pipeline then followed the procedure to pressure test the weld and the hot tap machine. Operations personnel verified that the pressure held. Tdw then tapped the line. Following the tap and verification of pressures, operations personnel blocked in the valve and de-pressured the tapping machine. Tdw then took the machine off of the valve and inserted the plug to plug to tor. Once tdw reinstalled the machine back to the valve, personnel tried to open the valve to thread the plug in. At this point, product began to leak out of the stem. The line was then blocked in and isolated. Pressured dropped sufficiently to safely thread the plug in, which stopped the product from leaking. The 2-inch ball valve was visually examined and found to have no significant external mechanical or corrosion damage. The valve was disassembled and the individual parts were visually examined, documented, and compared to the specified materials of the manufacturer's product catalog. A discrepancy observed during disassembly was the absence of a packing washer in the packing gland. Analysis of the polymeric components revealed discrepancies in the specified materials of the stem packing seals. An analysis report concluded that the cause of the packing leak was most likely due to the combination of 1) the absence of a packing washer in the packing gland, and 2) the ptfe material used for the packing seal contained no detectable reinforcing material via ftir spectroscopy (ftir - fourier transform infrared). No other discernable damage, wear, or uneven loading was observed in the valve components.
Detailed record list
Report Received Date
2017-09-14 00:00:00
Iyear
2017
Report Number
20170288
Supplemental Number
22779
Report Type
Supplemental Final
Operator Id
Name
Koch Pipeline Company, L.p.
Operator Street Address
4111 East 37th Street North
Operator City Name
Wichita
Operator State Abbreviation
KS
Operator Postal Code
67220
Local Datetime
2017-08-15 14:15:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Anhydrous Ammonia
Unintentional Release Bbls
0.26
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-08-15 14:15:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2017-08-15 14:17:00
Restart Datetime
2017-08-15 17:20:00
On Site Datetime
2017-08-15 14:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Inv-Orange 4" M Segment
Segment Name
80302110
Onshore State Abbreviation
Tx
Onshore Postal Code
77639
Onshore City Name
Not Within A Municipality
Onshore County Name
Orange
Designated Location
Survey Station No.
Designated Name
698+20
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
60
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2017
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
28
Est Cost Prop Damage
0
Est Cost Emergency
21000
Est Cost Environmental
0
Est Cost Other
0
Prpty
21028
Accident Psig
375
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
28420
Internal Inspection Ind
Yes
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
4" P/l Transporting Anhydrous Ammonia
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Release occurred during field work. Pcc management team determined neither the controller, nor the pcc, was a contributing factor to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Failure Of Valve Stem Seal Mechanism Of 2 Inch Ball Valve.
Eq Additional Other Ind
Yes
Eq Additional Other Details
Currently Waiting On Results Of Valve Inspection.
Preparer Name
M**** T*****
Preparer Title
Dot Compliance Specialist
Preparer Email
M***********@k***********.com
Preparer Telephone
409-989-6346
Prepared Date
2017-11-03 00:00:00
Authorizer Name
M**** T*****
Authorizer Telephone
409-989-6346
Authorizer Title
Dot Compliance Specialist
Authorizer Email
M***********@k***********.com
Narrative
On august 15, 2017, koch pipeline company's contractor, tdw, was performing a hot tap on the inv-orange 4" segment line in orange county, texas. Once the weld was made on the tor, koch pipeline then followed the procedure to pressure test the weld and the hot tap machine. Operations personnel verified that the pressure held. Tdw then tapped the line. Following the tap and verification of pressures, operations personnel blocked in the valve and de-pressured the tapping machine. Tdw then took the machine off of the valve and inserted the plug to plug to tor. Once tdw reinstalled the machine back to the valve, personnel tried to open the valve to thread the plug in. At this point, product began to leak out of the stem. The line was then blocked in and isolated. Pressured dropped sufficiently to safely thread the plug in, which stopped the product from leaking. The 2-inch ball valve was visually examined and found to have no significant external mechanical or corrosion damage. The valve was disassembled and the individual parts were visually examined, documented, and compared to the specified materials of the manufacturer's product catalog. A discrepancy observed during disassembly was the absence of a packing washer in the packing gland. Analysis of the polymeric components revealed discrepancies in the specified materials of the stem packing seals. An analysis report concluded that the cause of the packing leak was most likely due to the combination of 1) the absence of a packing washer in the packing gland, and 2) the ptfe material used for the packing seal contained no detectable reinforcing material via ftir spectroscopy (ftir - fourier transform infrared). No other discernable damage, wear, or uneven loading was observed in the valve components.
Report Received Date 2017-09-14 00:00:00
Iyear 2017
Report Number 20170288
Supplemental Number 22779
Report Type Supplemental Final
Operator Id 22855 PHMSA Enforcement
Name Koch Pipeline Company, L.p.
Operator Street Address 4111 East 37th Street North
Operator City Name Wichita
Operator State Abbreviation KS
Operator Postal Code 67220
Local Datetime 2017-08-15 14:15:00
Location Latitude 30.05642 Google Maps OpenStreetMap
Location Longitude -93.84246 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Anhydrous Ammonia
Unintentional Release Bbls 0.26
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-08-15 14:15:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2017-08-15 14:17:00
Restart Datetime 2017-08-15 17:20:00
On Site Datetime 2017-08-15 14:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Inv-Orange 4" M Segment
Segment Name 80302110
Onshore State Abbreviation Tx
Onshore Postal Code 77639
Onshore City Name Not Within A Municipality
Onshore County Name Orange
Designated Location Survey Station No.
Designated Name 698+20
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 60
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2017
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 28
Est Cost Prop Damage 0
Est Cost Emergency 21000
Est Cost Environmental 0
Est Cost Other 0
Prpty 21028
Accident Psig 375
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 28420
Internal Inspection Ind Yes
Operation Complications Ind Yes
Other Complications Ind Yes
Inspect Comp Details 4" P/l Transporting Anhydrous Ammonia
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Release occurred during field work. Pcc management team determined neither the controller, nor the pcc, was a contributing factor to the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Failure Of Valve Stem Seal Mechanism Of 2 Inch Ball Valve.
Eq Additional Other Ind Yes
Eq Additional Other Details Currently Waiting On Results Of Valve Inspection.
Preparer Name M**** T*****
Preparer Title Dot Compliance Specialist
Preparer Email M***********@k***********.com
Preparer Telephone 409-989-6346
Prepared Date 2017-11-03 00:00:00
Authorizer Name M**** T*****
Authorizer Telephone 409-989-6346
Authorizer Title Dot Compliance Specialist
Authorizer Email M***********@k***********.com
Narrative On august 15, 2017, koch pipeline company's contractor, tdw, was performing a hot tap on the inv-orange 4" segment line in orange county, texas. Once the weld was made on the tor, koch pipeline then followed the procedure to pressure test the weld and the hot tap machine. Operations personnel verified that the pressure held. Tdw then tapped the line. Following the tap and verification of pressures, operations personnel blocked in the valve and de-pressured the tapping machine. Tdw then took the machine off of the valve and inserted the plug to plug to tor. Once tdw reinstalled the machine back to the valve, personnel tried to open the valve to thread the plug in. At this point, product began to leak out of the stem. The line was then blocked in and isolated. Pressured dropped sufficiently to safely thread the plug in, which stopped the product from leaking. The 2-inch ball valve was visually examined and found to have no significant external mechanical or corrosion damage. The valve was disassembled and the individual parts were visually examined, documented, and compared to the specified materials of the manufacturer's product catalog. A discrepancy observed during disassembly was the absence of a packing washer in the packing gland. Analysis of the polymeric components revealed discrepancies in the specified materials of the stem packing seals. An analysis report concluded that the cause of the packing leak was most likely due to the combination of 1) the absence of a packing washer in the packing gland, and 2) the ptfe material used for the packing seal contained no detectable reinforcing material via ftir spectroscopy (ftir - fourier transform infrared). No other discernable damage, wear, or uneven loading was observed in the valve components.

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