HL incident on 2017-08-17 — TX

Operator
Shell Pipeline Co., L.p.
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2017-08-17 16:10
Report number
Location
TX
Narrative
Tank jet fuel #57 had been returned to service and was being filled with jet fuel. During jet fuel tank filling from 4.5 feet to 13 feet the local operator found a 1/4 turn valve open. There was no plug on the tubing that would have provided an additional barrier. Tank 57 was receiving jet fuel from the west shore pl. The operator closed the 1/4 turn valve stopping the jet fuel release and continued to receive from west shore pl. The pipeline delivery was not shut down. There was no clear individual to drug test. The valve was put back into service 3 weeks prior. The operators on duty that day performed their duties as per roles description. That is why the release was so small
Detailed record list
Report Received Date
2017-09-13 00:00:00
Iyear
2017
Report Number
20170286
Supplemental Number
22653
Report Type
Supplemental Final
Operator Id
Name
Shell Pipeline Co., L.p.
Operator Street Address
150 North Dairy Ashford Road Wck Bldg. A
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2017-08-17 16:10:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.19
Recovered Bbls
0.19
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-08-17 16:10:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Jet Fuel #57 Had Been Returned To Service And Was Being Filled With Jet Fue
On Site Datetime
2017-08-17 16:10:00
Nrc Rpt Datetime
2017-08-17 21:30:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Des Plaines Tank Farm
Onshore State Abbreviation
Il
Onshore Postal Code
60016
Onshore City Name
Des Plaines
Onshore County Name
Cook
Designated Location
Milepost/valve Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2017
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Incorrect Operation- Valve Was Left At The Wrong Position.
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
5000
Est Cost Environmental
15000
Est Cost Other
0
Prpty
20000
Accident Psig
0
Mop Psig
0
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller followed operating procedures. There were no indications from the scada system to alert the controller of any issue.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Other Ind
Yes
Operation Related Details
Incorrect Operations -Operator Error.
Category Type
Normal Operating Conditions
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
S**** I****
Preparer Title
Intergrity Management And Regulatory Engineer
Preparer Email
S**********@s****.com
Preparer Telephone
832-762-2666
Preparer Fax
832-337-5011
Prepared Date
2017-09-20 00:00:00
Authorizer Name
D****** P****
Authorizer Telephone
832-762-2553
Authorizer Title
Pipeline Ops Regulatory Manager
Authorizer Email
D************@s****.com
Narrative
Tank jet fuel #57 had been returned to service and was being filled with jet fuel. During jet fuel tank filling from 4.5 feet to 13 feet the local operator found a 1/4 turn valve open. There was no plug on the tubing that would have provided an additional barrier. Tank 57 was receiving jet fuel from the west shore pl. The operator closed the 1/4 turn valve stopping the jet fuel release and continued to receive from west shore pl. The pipeline delivery was not shut down. There was no clear individual to drug test. The valve was put back into service 3 weeks prior. The operators on duty that day performed their duties as per roles description. That is why the release was so small
Report Received Date 2017-09-13 00:00:00
Iyear 2017
Report Number 20170286
Supplemental Number 22653
Report Type Supplemental Final
Operator Id 31174 PHMSA Enforcement
Name Shell Pipeline Co., L.p.
Operator Street Address 150 North Dairy Ashford Road Wck Bldg. A
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2017-08-17 16:10:00
Location Latitude 42.026176 Google Maps OpenStreetMap
Location Longitude -87.950416 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.19
Recovered Bbls 0.19
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-08-17 16:10:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank Jet Fuel #57 Had Been Returned To Service And Was Being Filled With Jet Fue
On Site Datetime 2017-08-17 16:10:00
Nrc Rpt Datetime 2017-08-17 21:30:00
Nrc Rpt Num 1187631 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Des Plaines Tank Farm
Onshore State Abbreviation Il
Onshore Postal Code 60016
Onshore City Name Des Plaines
Onshore County Name Cook
Designated Location Milepost/valve Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2017
Material Involved Carbon Steel
Release Type Other
Release Type Details Incorrect Operation- Valve Was Left At The Wrong Position.
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 5000
Est Cost Environmental 15000
Est Cost Other 0
Prpty 20000
Accident Psig 0
Mop Psig 0
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller followed operating procedures. There were no indications from the scada system to alert the controller of any issue.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Other Ind Yes
Operation Related Details Incorrect Operations -Operator Error.
Category Type Normal Operating Conditions
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name S**** I****
Preparer Title Intergrity Management And Regulatory Engineer
Preparer Email S**********@s****.com
Preparer Telephone 832-762-2666
Preparer Fax 832-337-5011
Prepared Date 2017-09-20 00:00:00
Authorizer Name D****** P****
Authorizer Telephone 832-762-2553
Authorizer Title Pipeline Ops Regulatory Manager
Authorizer Email D************@s****.com
Narrative Tank jet fuel #57 had been returned to service and was being filled with jet fuel. During jet fuel tank filling from 4.5 feet to 13 feet the local operator found a 1/4 turn valve open. There was no plug on the tubing that would have provided an additional barrier. Tank 57 was receiving jet fuel from the west shore pl. The operator closed the 1/4 turn valve stopping the jet fuel release and continued to receive from west shore pl. The pipeline delivery was not shut down. There was no clear individual to drug test. The valve was put back into service 3 weeks prior. The operators on duty that day performed their duties as per roles description. That is why the release was so small

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