HL incident on 2017-08-14 — TX

Operator
Fairway Energy Partners, Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2017-08-14 13:35
Report number
Location
TX
Narrative
During the process of filling crude oil pumps with oil, a pump body drain valve was left open. Crude oil flowed through the open drain valve into the sump. The sump overflowed and backed up through other attached drain lines releasing 4 barrels of oil onto the ground. The overflow was identified immediately by on-site fairway personnel, the drain valve closed, and the release stopped. Contract cleanup personnel were immediately dispatched to remediate the soil surrounding the sump. Cleanup was completed within 48 hours and the sump was isolated to prevent recurrence. The sump has now been commissioned and is working as designed with level alarms and a sump pump that is activated when sump levels reach 25%. The sump is monitored by console operators 24/7 locally onsite via a scada system and fairway has an onsite outside operator 24/7 to perform field isolations. Additionally, the inspection of the sump is included in the operator rounds sheet. Rounds are conducted at least twice per 12 hour shift.
Detailed record list
Report Received Date
2017-09-12 00:00:00
Iyear
2017
Report Number
20170283
Supplemental Number
22704
Report Type
Supplemental Final
Operator Id
Name
Fairway Energy Partners, Llc
Operator Street Address
1000 Louisiana Suite 1450
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-08-14 13:30:00
Location Latitude
Location Longitude
-95.41201329
Commodity Released Type
Crude Oil
Unintentional Release Bbls
4
Recovered Bbls
4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-08-14 13:35:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pump Being Filled For Commissioning
On Site Datetime
2017-08-14 13:35:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Pierce Junction Facility
Segment Name
Crude Pump Drain Line
Onshore State Abbreviation
Tx
Onshore Postal Code
77045
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Pierce Jct
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Sump
Installation Year
2017
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
200
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
17000
Est Cost Other
0
Prpty
17200
Accident Psig
6
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
No
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller actions did not contribute to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Valve Misalignment
Related Failure Follow Ind
Yes
Category Type
Commissioning
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
B** H*****
Preparer Title
Vp Hse And Regulatory
Preparer Email
B*********@f***************.com
Preparer Telephone
832-714-2720
Prepared Date
2017-10-03 00:00:00
Authorizer Name
B** H*****
Authorizer Telephone
832-714-2720
Authorizer Title
Vp Hse And Regulatory
Authorizer Email
B*********@f***************.com
Narrative
During the process of filling crude oil pumps with oil, a pump body drain valve was left open. Crude oil flowed through the open drain valve into the sump. The sump overflowed and backed up through other attached drain lines releasing 4 barrels of oil onto the ground. The overflow was identified immediately by on-site fairway personnel, the drain valve closed, and the release stopped. Contract cleanup personnel were immediately dispatched to remediate the soil surrounding the sump. Cleanup was completed within 48 hours and the sump was isolated to prevent recurrence. The sump has now been commissioned and is working as designed with level alarms and a sump pump that is activated when sump levels reach 25%. The sump is monitored by console operators 24/7 locally onsite via a scada system and fairway has an onsite outside operator 24/7 to perform field isolations. Additionally, the inspection of the sump is included in the operator rounds sheet. Rounds are conducted at least twice per 12 hour shift.
Report Received Date 2017-09-12 00:00:00
Iyear 2017
Report Number 20170283
Supplemental Number 22704
Report Type Supplemental Final
Operator Id 39360 PHMSA Enforcement
Name Fairway Energy Partners, Llc
Operator Street Address 1000 Louisiana Suite 1450
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2017-08-14 13:30:00
Location Latitude 29.6509223 Google Maps OpenStreetMap
Location Longitude -95.41201329 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 4
Recovered Bbls 4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-08-14 13:35:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pump Being Filled For Commissioning
On Site Datetime 2017-08-14 13:35:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Pierce Junction Facility
Segment Name Crude Pump Drain Line
Onshore State Abbreviation Tx
Onshore Postal Code 77045
Onshore City Name Houston
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Pierce Jct
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Sump
Installation Year 2017
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 200
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 17000
Est Cost Other 0
Prpty 17200
Accident Psig 6
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind No
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller actions did not contribute to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Valve Misalignment
Related Failure Follow Ind Yes
Category Type Commissioning
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name B** H*****
Preparer Title Vp Hse And Regulatory
Preparer Email B*********@f***************.com
Preparer Telephone 832-714-2720
Prepared Date 2017-10-03 00:00:00
Authorizer Name B** H*****
Authorizer Telephone 832-714-2720
Authorizer Title Vp Hse And Regulatory
Authorizer Email B*********@f***************.com
Narrative During the process of filling crude oil pumps with oil, a pump body drain valve was left open. Crude oil flowed through the open drain valve into the sump. The sump overflowed and backed up through other attached drain lines releasing 4 barrels of oil onto the ground. The overflow was identified immediately by on-site fairway personnel, the drain valve closed, and the release stopped. Contract cleanup personnel were immediately dispatched to remediate the soil surrounding the sump. Cleanup was completed within 48 hours and the sump was isolated to prevent recurrence. The sump has now been commissioned and is working as designed with level alarms and a sump pump that is activated when sump levels reach 25%. The sump is monitored by console operators 24/7 locally onsite via a scada system and fairway has an onsite outside operator 24/7 to perform field isolations. Additionally, the inspection of the sump is included in the operator rounds sheet. Rounds are conducted at least twice per 12 hour shift.

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