Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2017-08-09 — TX
Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2017-08-09 03:00
Report number
Location
TX
Narrative
On 08-09-17 at approximately 03:00 local operations found 1 barrel of crude oil near the differential pressure gauge for jizkoot pump. At the time of discovery there was not an active leak and the clean-up process began immediately. The tubing we tightening and the pump was returned to normal operation. Operational rounds will continue to be made to prevent reoccurrence. The rrc was contacted at 03:40 on 08-09-17 and given incident report number 1600.
Detailed record list
Report Received Date
2017-09-05 00:00:00
Iyear
2017
Report Number
20170275
Supplemental Number
22750
Report Type
Supplemental Final
Operator Id
30829
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2017-08-09 03:00:00
Location Latitude
29.747992
Location Longitude
-95.128881
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-08-09 03:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Equipment Was Already Shutdown
On Site Datetime
2017-08-09 03:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
100 Manifold
Segment Name
Jizkoot Pump
Onshore State Abbreviation
Tx
Onshore Postal Code
77015
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Hsc
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tubing
Installation Year
2015
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
45
Est Cost Prop Damage
0
Est Cost Emergency
9887
Est Cost Environmental
0
Est Cost Other
0
Prpty
9932
Accident Psig
0
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller nor control room were a contributing factor
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Additional Vibration Ind
Yes
Preparer Name
C**** A******
Preparer Email
C*******@e****.com
Preparer Telephone
713-381-6426
Prepared Date
2017-10-23 00:00:00
Authorizer Name
C**** A******
Authorizer Telephone
713-381-6426
Authorizer Title
Pipeline Compliance
Authorizer Email
C*******@e****.com
Narrative
On 08-09-17 at approximately 03:00 local operations found 1 barrel of crude oil near the differential pressure gauge for jizkoot pump. At the time of discovery there was not an active leak and the clean-up process began immediately. The tubing we tightening and the pump was returned to normal operation. Operational rounds will continue to be made to prevent reoccurrence. The rrc was contacted at 03:40 on 08-09-17 and given incident report number 1600.
| Report Received Date | 2017-09-05 00:00:00 |
|---|---|
| Iyear | 2017 |
| Report Number | 20170275 |
| Supplemental Number | 22750 |
| Report Type | Supplemental Final |
| Operator Id | 30829 PHMSA Enforcement |
| Name | Enterprise Crude Pipeline Llc |
| Operator Street Address | 1100 Louisiana Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2017-08-09 03:00:00 |
| Location Latitude | 29.747992 Google Maps OpenStreetMap |
| Location Longitude | -95.128881 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 1 |
| Recovered Bbls | 1 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2017-08-09 03:00:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Equipment Was Already Shutdown |
| On Site Datetime | 2017-08-09 03:00:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | 100 Manifold |
| Segment Name | Jizkoot Pump |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 77015 |
| Onshore City Name | Houston |
| Onshore County Name | Harris |
| Designated Location | Milepost/valve Station |
| Designated Name | Hsc |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Tubing |
| Installation Year | 2015 |
| Material Involved | Material Other Than Carbon Steel |
| Material Details | Stainless Steel |
| Release Type | Leak |
| Leak Type | Connection Failure |
| Wildlife Impact Ind | No |
| Soil Contamination | No |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 45 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 9887 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 9932 |
| Accident Psig | 0 |
| Mop Psig | 275 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | Controller nor control room were a contributing factor |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Defective Or Loose Tubing Or Fitting |
| Eq Failure Type | Defective Or Loose Tubing Or Fitting |
| Additional Vibration Ind | Yes |
| Preparer Name | C**** A****** |
| Preparer Email | C*******@e****.com |
| Preparer Telephone | 713-381-6426 |
| Prepared Date | 2017-10-23 00:00:00 |
| Authorizer Name | C**** A****** |
| Authorizer Telephone | 713-381-6426 |
| Authorizer Title | Pipeline Compliance |
| Authorizer Email | C*******@e****.com |
| Narrative | On 08-09-17 at approximately 03:00 local operations found 1 barrel of crude oil near the differential pressure gauge for jizkoot pump. At the time of discovery there was not an active leak and the clean-up process began immediately. The tubing we tightening and the pump was returned to normal operation. Operational rounds will continue to be made to prevent reoccurrence. The rrc was contacted at 03:40 on 08-09-17 and given incident report number 1600. |
External Resources
PHMSA pipeline safety insights.
Product
Features
Company
All rights reserved. Copyright © by ClearPHMSA