HL incident on 2017-08-04 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2017-08-04 11:06
Report number
Location
TX
Narrative
On august 4, 2017 at approximately 11:06 am edt, the bay city plm supervisor received a call from the bay city electrical technician stating that the line 5 sending trap door was leaking. Approximately 30 gallons of product leaked onto the ground and remained on site in the immediate area of the sending trap. The bay city plm crew was dispatched immediately to drain and repair the trap door. Preliminary investigation determined that the o-ring on the trap door had failed resulting in the release. A gemini smart tool had been launched successfully the day prior and the o-ring replaced by the bay city plm. During the re-pressurization on august 3, 2017, a visual inspection of the door was completed and the trap was brought back up to line pressure and monitored for approximately two hours with no issues. Further investigation determined that there were metal burs on the trap door that damaged the new o-ring during installation. The burs were removed using hand files and sand paper and the o-ring was replaced. Approximately 10 cubic yards of contaminated soil was removed from the release site.
Detailed record list
Report Received Date
2017-09-01 00:00:00
Iyear
2017
Report Number
20170273
Supplemental Number
22610
Report Type
Original Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2017-08-04 11:06:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.71
Recovered Bbls
0.71
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-08-04 11:06:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Operations Did Not Contribute To Or Cause The Release
On Site Datetime
2017-08-04 11:06:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Bay City Station
Segment Name
Line 5 Scrapper Trap
Onshore State Abbreviation
Mi
Onshore Postal Code
48706
Onshore City Name
Bay City
Onshore County Name
Bay
Designated Location
Milepost/valve Station
Designated Name
1636.7
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Scraper/pig Trap
Installation Year
2017
Material Involved
Material Other Than Carbon Steel
Material Details
Buna-N/nitrile
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
100
Est Cost Emergency
6000
Est Cost Environmental
5000
Est Cost Other
0
Prpty
11100
Accident Psig
451
Mop Psig
882
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Lack of control center involvement
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
O-Ring Was Damaged During Installation
Eq Additional Other Ind
Yes
Eq Additional Other Details
Metal On Trap Door Contacted O-Ring Resulting In Damage
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Preparer Fax
715-398-4802
Prepared Date
2017-09-01 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
715-395-3619
Authorizer Title
Supervisor Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
On august 4, 2017 at approximately 11:06 am edt, the bay city plm supervisor received a call from the bay city electrical technician stating that the line 5 sending trap door was leaking. Approximately 30 gallons of product leaked onto the ground and remained on site in the immediate area of the sending trap. The bay city plm crew was dispatched immediately to drain and repair the trap door. Preliminary investigation determined that the o-ring on the trap door had failed resulting in the release. A gemini smart tool had been launched successfully the day prior and the o-ring replaced by the bay city plm. During the re-pressurization on august 3, 2017, a visual inspection of the door was completed and the trap was brought back up to line pressure and monitored for approximately two hours with no issues. Further investigation determined that there were metal burs on the trap door that damaged the new o-ring during installation. The burs were removed using hand files and sand paper and the o-ring was replaced. Approximately 10 cubic yards of contaminated soil was removed from the release site.
Report Received Date 2017-09-01 00:00:00
Iyear 2017
Report Number 20170273
Supplemental Number 22610
Report Type Original Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2017-08-04 11:06:00
Location Latitude 43.629243 Google Maps OpenStreetMap
Location Longitude -83.98516 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.71
Recovered Bbls 0.71
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-08-04 11:06:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Operations Did Not Contribute To Or Cause The Release
On Site Datetime 2017-08-04 11:06:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Bay City Station
Segment Name Line 5 Scrapper Trap
Onshore State Abbreviation Mi
Onshore Postal Code 48706
Onshore City Name Bay City
Onshore County Name Bay
Designated Location Milepost/valve Station
Designated Name 1636.7
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Scraper/pig Trap
Installation Year 2017
Material Involved Material Other Than Carbon Steel
Material Details Buna-N/nitrile
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 100
Est Cost Emergency 6000
Est Cost Environmental 5000
Est Cost Other 0
Prpty 11100
Accident Psig 451
Mop Psig 882
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Lack of control center involvement
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details O-Ring Was Damaged During Installation
Eq Additional Other Ind Yes
Eq Additional Other Details Metal On Trap Door Contacted O-Ring Resulting In Damage
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Preparer Fax 715-398-4802
Prepared Date 2017-09-01 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 715-395-3619
Authorizer Title Supervisor Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative On august 4, 2017 at approximately 11:06 am edt, the bay city plm supervisor received a call from the bay city electrical technician stating that the line 5 sending trap door was leaking. Approximately 30 gallons of product leaked onto the ground and remained on site in the immediate area of the sending trap. The bay city plm crew was dispatched immediately to drain and repair the trap door. Preliminary investigation determined that the o-ring on the trap door had failed resulting in the release. A gemini smart tool had been launched successfully the day prior and the o-ring replaced by the bay city plm. During the re-pressurization on august 3, 2017, a visual inspection of the door was completed and the trap was brought back up to line pressure and monitored for approximately two hours with no issues. Further investigation determined that there were metal burs on the trap door that damaged the new o-ring during installation. The burs were removed using hand files and sand paper and the o-ring was replaced. Approximately 10 cubic yards of contaminated soil was removed from the release site.

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