HL incident on 2017-07-27 — PA

Operator
Buckeye Partners, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2017-07-27 06:15
Report number
Location
PA
Narrative
During a terminal inspection, a release from the body bleed piping of a double block and bleed valve on the suction valve to the booster, pumping from tank 1 was found. All the required internal and external notification were made. All contaminated soil was removed and drummed from disposal. It was determined that the valves on the body bleed piping were incorrectly aligned. 12/20/2017 the source of the release was a valve that was installed in 2012 on a tank during a 653 inspection. The tank was not placed back into service upon completion due to business needs. The valve was equipped with a body relief needle check valve. Local operators did not verify valve positioning on the relief system when the tank was returned to service. The needle check valve was left in the open position allowing diesel fuel to release through the test fitting, which was not plugged at the time of discovery.
Detailed record list
Report Received Date
2017-08-25 00:00:00
Iyear
2017
Report Number
20170262
Supplemental Number
22976
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2017-07-27 06:15:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.6
Recovered Bbls
0.6
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2017-07-27 06:15:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
System Was Not Running When The Release Was Found.
On Site Datetime
2017-07-27 06:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Niles West
Segment Name
Betnt
Onshore State Abbreviation
Mi
Onshore Postal Code
49120
Onshore City Name
Niles
Onshore County Name
Berrien
Designated Location
Milepost/valve Station
Designated Name
Betnt
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2012
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Improperly Alligned Valves
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
65
Est Cost Prop Damage
0
Est Cost Emergency
6000
Est Cost Environmental
5000
Est Cost Other
0
Prpty
11065
Accident Psig
15
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Control center does not monitor this operation.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Failure Follow Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
No
Preparer Name
M***** E*****
Preparer Title
Senior District Compliance Specialist
Preparer Email
M******@b******.com
Preparer Telephone
219796-8230
Prepared Date
2017-12-20 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
610-904-4113
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
During a terminal inspection, a release from the body bleed piping of a double block and bleed valve on the suction valve to the booster, pumping from tank 1 was found. All the required internal and external notification were made. All contaminated soil was removed and drummed from disposal. It was determined that the valves on the body bleed piping were incorrectly aligned. 12/20/2017 the source of the release was a valve that was installed in 2012 on a tank during a 653 inspection. The tank was not placed back into service upon completion due to business needs. The valve was equipped with a body relief needle check valve. Local operators did not verify valve positioning on the relief system when the tank was returned to service. The needle check valve was left in the open position allowing diesel fuel to release through the test fitting, which was not plugged at the time of discovery.
Report Received Date 2017-08-25 00:00:00
Iyear 2017
Report Number 20170262
Supplemental Number 22976
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2017-07-27 06:15:00
Location Latitude 41.789885 Google Maps OpenStreetMap
Location Longitude -86.258061 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.6
Recovered Bbls 0.6
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2017-07-27 06:15:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain System Was Not Running When The Release Was Found.
On Site Datetime 2017-07-27 06:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Niles West
Segment Name Betnt
Onshore State Abbreviation Mi
Onshore Postal Code 49120
Onshore City Name Niles
Onshore County Name Berrien
Designated Location Milepost/valve Station
Designated Name Betnt
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2012
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Improperly Alligned Valves
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 65
Est Cost Prop Damage 0
Est Cost Emergency 6000
Est Cost Environmental 5000
Est Cost Other 0
Prpty 11065
Accident Psig 15
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Control center does not monitor this operation.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Failure Follow Ind Yes
Category Type Normal Operating Conditions
Operator Qualification Ind No
Preparer Name M***** E*****
Preparer Title Senior District Compliance Specialist
Preparer Email M******@b******.com
Preparer Telephone 219796-8230
Prepared Date 2017-12-20 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 610-904-4113
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative During a terminal inspection, a release from the body bleed piping of a double block and bleed valve on the suction valve to the booster, pumping from tank 1 was found. All the required internal and external notification were made. All contaminated soil was removed and drummed from disposal. It was determined that the valves on the body bleed piping were incorrectly aligned. 12/20/2017 the source of the release was a valve that was installed in 2012 on a tank during a 653 inspection. The tank was not placed back into service upon completion due to business needs. The valve was equipped with a body relief needle check valve. Local operators did not verify valve positioning on the relief system when the tank was returned to service. The needle check valve was left in the open position allowing diesel fuel to release through the test fitting, which was not plugged at the time of discovery.

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